Unsolved Jerk and acceleration settings cr-10s5
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; homeall.g
G91 ; relative positioning
G1 S2 X0.2 Y0.2 Z0.2 ; Move all axis 0.2 mm, clear stall status
M98 Pdeployprobe.g ; deploy mechanical Z probe; x and y Sensor less homing
M400 ; make sure everything has stopped before we make changes
M915 X S2 Y S3 R0 F0 ; set X and Y sensitivity, do nothing when stall, unfiltered
M574 X1 Y1 S3 ; set endstops to use motor stall
G1 S2 Z10 F1200 ; lift Z
G1 S1 X-265 Y-260 F5000 ; move X and Y back, stopping at the end stop
M400 ; make sure everything has stopped
G90 ; back to absolute mode;G1 X115 Y115 F12000 ; Move to center of bed and home Z
G1 X127 Y134 F6000 ; go to first bed probe point and home Z
G30 ; home Z by probing the bedM915 X S10 Y S10 R3 F0 ; set X and Y sensitivity to -0, when stall home XY and resume print, filtered so it takes 4 steps to figure out it has stalled
M98 Pretractprobe.g ; retract mechanical Z probe
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; homex.g
G91 ; relative positioning
G1 S2 X0.2 Y0.2 Z0.2 ; Move all axis 0.2 mm, clear stall status
M400 ; make sure everything has stopped before we make changes
M915 X S2 R0 F0 ; set X and Y sensitivity, do nothing when stall, unfiltered
M574 X0 S1 ; set endstops to use motor stall
G1 S1 X-265 F5000 ; move X, stopping at the end stop
G1 Z-0.2 ; Move all axis -0.2 mm,
M400 ; make sure everything has stopped
G90 ; back to absolute mode
M915 X S2 Y S3 R3 F0 ; set X and Y sensitivity to 0, when stall home XY and resume print, filtered so it takes 4 steps to figure out it has stalled -
; homey.g
G91 ; relative positioning
G1 S2 X0.2 Y0.2 Z0.2 ; Move all axis 0.2 mm, clear stall status
M400 ; make sure everything has stopped before we make changes
M915 Y S2 R0 F0 ; set X and Y sensitivity, do nothing when stall, unfiltered
M574 Y0 S1 ; set endstops to use motor stall
G1 S1 Y-260 F5000 ; move X, stopping at the end stop
G1 Z-0.2 ; Move z -0.2 mm,
M400 ; make sure everything has stopped
G90 ; back to absolute mode
M915 X S2 Y S3 R3 F0 ; set X and Y sensitivity to 0, when stall home XY and resume print, filtered so it takes 4 steps to figure out it has stalled -
thanks for looking
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@ziggymanpopo said in Jerk and acceleration settings cr-10s5:
; Enable Bed Leveling
G29 S1 ; Enable Mesh Bed LevelingYou should probably move this to the end of your homeall rather than the end of config.g. Having it enabled as soon as the printer is turned on means that you haven't yet defined where Z0 is, which can lead to frustrations with first layers.
@ziggymanpopo said in Jerk and acceleration settings cr-10s5:
G31 P500
Try G31 P25 instead for a tighter trigger threshold on theBLtouch.
@ziggymanpopo said in Jerk and acceleration settings cr-10s5:
M98 Pdeployprobe.g ; deploy mechanical Z probe
M98 Pretractprobe.g ; retract mechanical Z probeYou don't need to manually deploy or retract the pin. The Duet will do that on it's own as needed for probing.
@ziggymanpopo said in Jerk and acceleration settings cr-10s5:
M566 X600 Y600 Z24 E300 ; Set maximum instantaneous speed changes (mm/min)
M203 X30000 Y30000 Z300 E1500 ; Set maximum speeds (mm/min)
M201 X300 Y300 Z100 E5000 ; Set accelerations (mm/s^2X and Y jerk look fine, especially for a large bed like the S5.
Z jerk may be a bit low for mesh bed leveling. Try Z60.
E jerk is bit low at 300, especially if you intend to use pressure advance. Try adding an order of magnitude, 3000.
X and Y acceleration are a bit low. 600-900 for X wouldn't be too crazy. Given the size of the Y axis 600 would probably be appropriate. -
Yeah prob. Should have mentioned that i have an abl inductive sensor not a bl toutch ,, so i believe the person who helped me with the original files picked a generic file just to get me going. So fare so good but i have some serious clean up to do not sure where to start except "one thing at a time. " just like any kit printer i realize my learnig curve the printer has some issue because of the board configuration and the printer are not quite a match or set right. i will take one ore two items at a time . The info has been invaluable. And i think this will keep me focused i thank all for there input
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What is causing ghosting and ripples in the y axes ...its just in the y ??? Does it have to do woth the weight of my 500mm bed... Also if i turn up any settings won't it hit the end stop harder ...what in the setup made the end stops no longer function. Should i chainge it back so they do and will this stop hard hits when homming
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@ziggymanpopo said in Jerk and acceleration settings cr-10s5:
G1 S1 X-265 Y-260 F5000 ; move X and Y back, stopping at the end stop
It's stopping halfway because you're only moving half the distance of the full bed size. Increase those movements to more than 500 to ensure they hit the endstop.
I didn't realize you were not using the BLTouch. If the probe is working, leave the settings as is and disregard my comments.
If you're still getting ringing even with those conservative values I would look at belt tension and flex. Such a large and heavy bed is going to be difficult to tame.
The speed of the homing moves is set in the homing files. Since you're using sensorless homing you must use a fairly rapid move for the stall detection to trigger properly. Personally I'm not a fan of the idea of slamming my print head into a physical stop to home, but it seems to be all the rage these days.
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I agree??? slamming is no good. Is there an easy way to put endstops back in play ??? Did that happen when i activated the. Abl sensor in the gcode??? Is it advisable to reactivate the end stops...When i set up the board they worked ??? The second problem i have is with the stall feature is when it is at the home on x,,, and its not on home for y ans z . It makes an auful sound on x when homming y and z . "The rest of the way." "like when an print is done"it homes y and z... but x isballready homed.... So it grinds x because its allready homed....then it homes the other two. Any hints highly appreciated
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Would it be possable to increase the size of the belt to aid in the taming of my large bed. ???
Id thought about putting in linear screws and guides. as a solution for the y axes -
Well if the end stop switches are still in place and connected to the board you can change the config to use those instead of stall detection.
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@ziggymanpopo said in Jerk and acceleration settings cr-10s5:
Would it be possable to increase the size of the belt to aid in the taming of my large bed. ???
Id thought about putting in linear screws and guides. as a solution for the y axesLarger belts may help for belt stretch but so would higher quality belts. It still doesn't reduce the weight of the bed though.
Linear screws have their own rotational momentum to deal with so aren't actually a solution. You'd be limited to the same or lower acceleration.