Hey!
I am using the D2Wifi on a CR-10. Since I use both Z-motors independently, my X-gantry falls on the heavy side about 2mm when the power@steppers is switched off. Previously, when the steppers where in series, that didnt happen. Is that due to wrong wiring? I already tried to tighten the pulleys, but without success.
If I use then G32 to adjust the gantry, i must repeat ikt approx 5-6 times until it is leveled. Is that the algorithm, which makes no bigger compensation, or have I sth wrong in the command?
bed.g:
G0 X150 y150 Z5 F360
G30
G30 P0 X20 Y150 Z-99999 ; probe near a leadscrew, half way along Y axis
G30 P1 X280 Y150 Z-99999 S2 ; probe near a leadscrew and calibrate 2 motors
G0 X150 F24000
config.g:
M671 X-27:333 Y150:150 S5 P3 ; leadscrews at left and right of X axis