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    M116 Hanging after M568 Error

    Scheduled Pinned Locked Moved
    Firmware installation
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    • curieosundefined
      curieos
      last edited by

      I was able to break out of it by sending an M108 command, but I got an error in the console for an M568 command in this file to set the second layer temps.

      The errors:

      Error: CAN response timeout: board 20, req type 6013, RID 971
      Error:  at column 2: 
      Error: CAN response timeout: board 21, req type 6013, RID 969
      Error:  at column 2: M568:
      

      The code from the file at this line:

      ; stop printing object SECTIONED HULK BBC CARBON FOR MACHINING TEST.STL id:2 copy 0
      ;LAYER_CHANGE
      ;Z:0.6
      ;HEIGHT:0.3
      ;LAYER:1
      G1 E-1 F2400
      ;WIPE_START
      G1 F19200
      G1 X256.922 Y240.201 E-1
      ;WIPE_END
      G1 Z.6 F450
      
      M568 P0 S280 ; set temperature
      M568 P1 S215 ; set temperature
      M140 S60 ; set bed temperature
      ; printing object SECTIONED HULK BBC CARBON FOR MACHINING TEST.STL id:2 copy 0
      G1 Z1
      G1 X297.189 Y413.826 F24000
      G1 Z.6 F450
      G1 E2 F1800
      

      M122 outputs:

      M122
      === Diagnostics ===
      RepRapFirmware for Duet 3 MB6XD version 3.5.0-rc.3 (2024-01-24 17:59:29) running on Duet 3 MB6XD v1.01 or later (SBC mode)
      Board ID: 0JD2M-999AL-D25SW-6JKD0-3S06R-95ZB1
      Used output buffers: 12 of 40 (40 max)
      === RTOS ===
      Static ram: 153600
      Dynamic ram: 92880 of which 184 recycled
      Never used RAM 93072, free system stack 112 words
      Tasks: SBC(2,ready,23.8%,407) HEAT(3,nWait 6,0.4%,322) Move(4,nWait 6,13.9%,213) CanReceiv(6,nWait 1,44.1%,770) CanSender(5,nWait 7,0.3%,325) CanClock(7,delaying,0.1%,346) MAIN(2,running,17.0%,444) IDLE(0,ready,0.4%,30), total 100.0%
      Owned mutexes: Telnet(MAIN)
      === Platform ===
      Last reset 25:02:31 ago, cause: power up
      Last software reset at 2024-03-07 09:55, reason: User, Gcodes spinning, available RAM 95784, slot 0
      Software reset code 0x6003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0x00000000 Task SBC Freestk 0 n/a
      Error status: 0x04
      Aux0 errors 0,1,0
      MCU temperature: min 29.4, current 46.7, max 50.4
      Supply voltage: min 25.7, current 25.8, max 26.2, under voltage events: 0, over voltage events: 0, power good: yes
      12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
      Heap OK, handles allocated/used 99/40, heap memory allocated/used/recyclable 4096/2644/1884, gc cycles 11
      Events: 0 queued, 0 completed
      Driver 0: ok
      Driver 1: ok
      Driver 2: ok
      Driver 3: ok
      Driver 4: ok
      Driver 5: ok
      Date/time: 2024-03-20 11:35:37
      Slowest loop: 1226.17ms; fastest: 0.04ms
      === Storage ===
      Free file entries: 20
      SD card 0 not detected, interface speed: 37.5MBytes/sec
      SD card longest read time 0.0ms, write time 0.0ms, max retries 0
      === Move ===
      DMs created 125, segments created 56, maxWait 51691952ms, bed compensation in use: mesh, height map offset 0.000, max steps late 1, ebfmin 0.00, ebfmax 0.00
      no step interrupt scheduled
      Moves shaped first try 33337, on retry 20333, too short 109285, wrong shape 349661, maybepossible 18667
      === DDARing 0 ===
      Scheduled moves 7070, completed 7070, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 17], CDDA state -1
      === DDARing 1 ===
      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === Heat ===
      Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
      Heater 0 is on, I-accum = 0.2
      Heater 1 is on, I-accum = 0.0
      === GCodes ===
      Movement locks held by null, null
      HTTP* is doing "M25" in state(s) 0
      Telnet* is doing "M122" in state(s) 0
      File* is doing "M116 P"{state.currentTool}"" in state(s) 0 0 19, running macro
      USB is idle in state(s) 0
      Aux is doing "M25" in state(s) 0
      Trigger* is idle in state(s) 0
      Queue* is idle in state(s) 0
      LCD is idle in state(s) 0
      SBC* is idle in state(s) 0
      Daemon is idle in state(s) 0
      Aux2 is idle in state(s) 0
      Autopause is idle in state(s) 0
      File2* is doing "M116 P1 S5" in state(s) 0
      Queue2 is idle in state(s) 0
      Q0 segments left 0, axes/extruders owned 0x80000003
      Code queue 0 is empty
      Q1 segments left 0, axes/extruders owned 0x0000000
      Code queue 1 is empty
      === Filament sensors ===
      check 0 clear 0
      Extruder 0: no data received, errs: frame 0 parity 0 ovrun 0 pol 0 ovdue 0
      Extruder 1: no data received, errs: frame 0 parity 0 ovrun 0 pol 0 ovdue 0
      === CAN ===
      Messages queued 1547554, received 122035323, lost 0, errs 1, boc 0
      Longest wait 3ms for reply type 6013, peak Tx sync delay 765, free buffers 50 (min 47), ts 450758/450757/0
      Tx timeouts 0,0,0,3,0,0 last cancelled message type 6013 dest 21
      === SBC interface ===
      Transfer state: 5, failed transfers: 0, checksum errors: 0
      RX/TX seq numbers: 41823/41823
      SPI underruns 0, overruns 0
      State: 5, disconnects: 0, timeouts: 0 total, 0 by SBC, IAP RAM available 0x2600c
      Buffer RX/TX: 2220/3712-0, open files: 0
      === Duet Control Server ===
      Duet Control Server version 3.5.0-rc.3 (2024-01-26 12:34:19)
      File /opt/dsf/sd/gcodes/Jarvie/Sectioned Hulk Modifier Test_0.6n_NYLON_22h34m.gcode is selected, processing
      HTTP:
      Buffered code: M25
      Buffered code: M568 P0 A1
      Buffered code: M568 P1 A0
      Buffered codes: 104 bytes total
      File:
      Buffered code: M116 P{state.currentTool} ; wait for tool 0 heaters to reach operating temperature
      Buffered codes: 52 bytes total
      > Suspended code: M116 P0 S5
      > Suspended code: M572 D0 S0.006
      > Suspended code: ; printing object SECTIONED HULK BBC CARBON FOR MACHINING TEST.STL id:2 copy 0
      > Suspended code: G1 X389.242 Y468.798 F24000
      > Suspended code: G1 Z.6 F450
      > Suspended code: G1 E2 F1800
      > Suspended code: M204 P1000
      > Suspended code: G1 F4800
      > Suspended code: G1 X332.27 Y468.798 E3.95326
      > Suspended code: G1 X332.27 Y171.202 E20.65005
      > Suspended code: G1 X389.242 Y171.202 E3.95326
      > Suspended code: G1 X389.242 Y199.689 E1.9767
      > Suspended code: G1 X389.242 Y468.708 E18.6671
      > Suspended code: M204 P4000
      > Suspended code: G1 X389.242 Y468.708 F24000
      > Suspended code: M73 P2 R1314
      > Suspended code: G1 X389.828 Y469.383
      > Suspended code: M204 P1000
      > Suspended code: G1 F4800
      > Suspended code: G1 X331.684 Y469.383 E4.03459
      > Suspended code: G1 X331.684 Y170.617 E20.73124
      > Suspended code: G1 X389.828 Y170.617 E4.03459
      > Suspended code: G1 X389.828 Y199.689 E2.01729
      > Suspended code: G1 X389.828 Y469.293 E18.7077
      > Suspended code: M204 P4000
      > Suspended code: G1 X389.828 Y469.293 F24000
      > Suspended code: G1 X390.414 Y469.969
      > Suspended code: M204 P1000
      >> Doing macro tpost0.g, started by T0
      >>> Doing macro 0:/sys/System Macros/Tool Change/tpost.g, started by M98 P{"0:/sys"^"/System Macros/Tool Change/tpost.g"}
      >>> Number of flush requests: 1
      File2:
      Buffered code: M116 P1 S5
      Buffered code: M572 D1 S0.04
      Buffered code: ; printing object SECTIONED HULK BBC CARBON FOR MACHINING TEST.STL id:2 copy 0
      Buffered code: G1 X274.174 Y310.448 F24000
      Buffered code: G1 Z63.3 F450
      Buffered code: G1 E2 F1800
      Buffered code: G1 F4800
      Buffered code: G1 X274.623 Y311.463 E.06673
      Buffered code: G1 X275.389 Y312.452 E.07521
      Buffered code: G1 X276.265 Y313.197 E.06914
      Buffered code: G1 X276.876 Y313.561 E.04276
      Buffered code: G1 X277.353 Y313.744 E.03072
      Buffered code: G1 X275.617 Y316.744 E.2084
      Buffered code: G1 X271.225 Y316.744 E.26407
      Buffered code: G1 X269.493 Y313.744 E.20828
      Buffered code: G1 X269.225 Y313.744 E.01611
      Buffered code: G1 X269.227 Y313.208 E.03223
      Buffered code: G1 X269.493 Y313.208 E.01599
      Buffered code: G1 X271.225 Y310.208 E.20828
      Buffered code: G1 X274.055 Y310.208 E.17015
      Buffered code: G1 X273.852 Y309.672 E.03446
      Buffered code: G1 X271.225 Y309.672 E.15795
      Buffered code: G1 X269.493 Y306.672 E.20828
      Buffered code: G1 X269.26 Y306.672 E.01401
      Buffered code: G1 X269.263 Y306.137 E.03217
      Buffered code: G1 X269.493 Y306.137 E.01383
      Buffered code: G1 X271.225 Y303.137 E.20828
      Buffered code: G1 X274.923 Y303.137 E.22234
      Buffered code: G1 X274.135 Y304.532 E.09633
      Buffered codes: 1404 bytes total
      Code buffer space: 2220
      Configured SPI speed: 8000000Hz, TfrRdy pin glitches: 7
      Full transfers per second: 42.11, max time between full transfers: 121.4ms, max pin wait times: 74.9ms/23.6ms
      Codes per second: 28.78
      Maximum length of RX/TX data transfers: 5128/3328
      
      	M122 B20
      Diagnostics for board 20:
      Duet TOOL1LC rev 1.1 or later firmware version 3.5.0-rc.3 (2024-01-24 17:55:14)
      Bootloader ID: SAMC21 bootloader version 2.8 (2023-07-25)
      All averaging filters OK
      Never used RAM 1544, free system stack 55 words
      Tasks: Move(3,nWait 7,3.0%,79) HEAT(2,nWait 6,4.8%,91) CanAsync(5,nWait 4,0.0%,49) CanRecv(3,nWait 1,1.8%,65) CanClock(5,nWait 1,0.4%,59) ACCEL(3,nWait 6,0.0%,53) TMC(2,delaying,66.4%,53) MAIN(1,running,34.2%,315) IDLE(0,ready,19.3%,27) AIN(2,delaying,90.5%,112), total 220.5%
      Owned mutexes:
      Last reset 25:10:52 ago, cause: power up
      Last software reset data not available
      Driver 0: pos 0, 404.7 steps/mm, standstill, SG min 0, read errors 14, write errors 0, ifcnt 35, reads 59693, writes 35, timeouts 31, DMA errors 0, CC errors 0, failedOp 0x71, steps req 0 done 53253485
      Moves scheduled 605288, completed 605288, in progress 0, hiccups 1669, segs 57, step errors 0, maxLate 2 maxPrep 562, maxOverdue 164274, maxInc 132515, mcErrs 0, gcmErrs 0, ebfmin -1.00 max 1.00
      Peak sync jitter -1/15, peak Rx sync delay 260, resyncs 0/0, no timer interrupt scheduled
      VIN voltage: min 22.9, current 26.0, max 45.4
      MCU temperature: min 23.9C, current 69.5C, max 98.7C
      Last sensors broadcast 0x00006002 found 3 86 ticks ago, 0 ordering errs, loop time 0
      CAN messages queued 115277228, send timeouts 0, received 2151698, lost 0, errs 1, boc 0, free buffers 18, min 17, error reg 20000
      dup 0, oos 36/0/0/18, bm 0, wbm 0, rxMotionDelay 380, adv -164096/108406
      Accelerometer: LIS3DH, status: 00
      I2C bus errors 0, naks 3, contentions 0, other errors 0
      === Filament sensors ===
      Interrupt 4 to 134us, poll 8 to 2564us
      Driver 0: pos 2196.91, errs: frame 308 parity 0 ovrun 0 pol 0 ovdue 0
      
      	M122 B21
      Diagnostics for board 21:
      Duet TOOL1LC rev 1.1 or later firmware version 3.5.0-rc.3 (2024-01-24 17:55:14)
      Bootloader ID: SAMC21 bootloader version 2.8 (2023-07-25)
      All averaging filters OK
      Never used RAM 2192, free system stack 55 words
      Tasks: Move(3,nWait 7,0.1%,79) HEAT(2,nWait 6,3.7%,91) CanAsync(5,nWait 4,0.0%,49) CanRecv(3,nWait 1,1.0%,71) CanClock(5,nWait 1,0.4%,59) ACCEL(3,nWait 6,0.0%,53) TMC(2,delaying,65.6%,53) MAIN(1,running,41.8%,315) IDLE(0,ready,19.0%,27) AIN(2,delaying,88.9%,112), total 220.5%
      Owned mutexes:
      Last reset 25:10:53 ago, cause: power up
      Last software reset at 2024-02-01 11:32, reason: HardFault, available RAM 2016, slot 0
      Software reset code 0x0060 ICSR 0x00000003 SP 0x20002f08 Task MAIN Freestk 813 ok
      Stack: 200048c8 00000000 00000001 4aa36799 00000000 0000f3cb 4aa36798 21000000 20001488 0000f00d a5a5a5a5 0080bdc1 00000089 000001f4 20001ce0 0001285f 00000000 00000000 20004370 a5a5a5a5 a5a5a5a5 a5a5a5a5 a5a5a5a5 a5a5a5a5 a5a5a5a5 a5a5a5a5 a5a5a5a5
      Driver 0: pos 0, 404.8 steps/mm, standstill, SG min 0, read errors 0, write errors 0, ifcnt 16, reads 40538, writes 16, timeouts 8, DMA errors 0, CC errors 0, failedOp 0x41, steps req 0 done 1013751
      Moves scheduled 4732, completed 4732, in progress 0, hiccups 8, segs 31, step errors 0, maxLate 1 maxPrep 396, maxOverdue 3553, maxInc 2672, mcErrs 0, gcmErrs 0, ebfmin -0.93 max 1.00
      Peak sync jitter -1/7, peak Rx sync delay 243, resyncs 0/0, no timer interrupt scheduled
      VIN voltage: min 24.9, current 26.5, max 26.8
      MCU temperature: min 27.9C, current 75.6C, max 81.4C
      Last sensors broadcast 0x00018004 found 3 32 ticks ago, 0 ordering errs, loop time 0
      CAN messages queued 7715520, send timeouts 0, received 1546216, lost 0, errs 1, boc 0, free buffers 18, min 17, error reg 20000
      dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 352, adv 35330/100443
      Accelerometer: LIS3DH, status: 00
      I2C bus errors 0, naks 3, contentions 0, other errors 0
      === Filament sensors ===
      Interrupt 4 to 85us, poll 6 to 1313us
      Driver 0: pos 13983.05, errs: frame 21 parity 0 ovrun 0 pol 0 ovdue 0
      

      She/Her
      I work at a local 3D printing shop.
      Printers: Micron+ w/Duet 3 Mini, in-progress adaptation of the Jubilee REL onto an E3D MS, Prusa i3 MK3S.

      dc42undefined 1 Reply Last reply Reply Quote 0
      • dc42undefined
        dc42 administrators @curieos
        last edited by

        @curieos please try the latest 3.5 firmware build from https://www.dropbox.com/scl/fo/yzchzlyxmxlzywjawqflu/h?rlkey=tl7dfs75yozhfgpze0jnkn32n&dl=0.

        Duet WiFi hardware designer and firmware engineer
        Please do not ask me for Duet support via PM or email, use the forum
        http://www.escher3d.com, https://miscsolutions.wordpress.com

        curieosundefined 2 Replies Last reply Reply Quote 0
        • curieosundefined
          curieos @dc42
          last edited by

          @dc42 This is in SBC mode, can I just upload these to the FW directory and send the update commands?

          She/Her
          I work at a local 3D printing shop.
          Printers: Micron+ w/Duet 3 Mini, in-progress adaptation of the Jubilee REL onto an E3D MS, Prusa i3 MK3S.

          dc42undefined 1 Reply Last reply Reply Quote 0
          • curieosundefined
            curieos @dc42
            last edited by curieos

            @dc42 Is there a DSF or DWC release to go with those? I just encountered some very strange behavior retrying that print with those binaries.

            I first homed the machine before the print. Then I started the print, and it homed again (as expected), and then immediately it rehomed. It then moved to the "starting position" near the nozzle wiper, skipped over waiting for the tool to heat and wiping in the tool change macros, moved to the print start location, waited for T0 to heat up, and started printing. It then got halfway done with the skirt, retracted, and moved back to the wiping location, then moved back to where it stopped with the skirt, did the extruder priming sequence, and resumed the skirt. I then paused it, and it moved to the park position. I tried resuming, and it then properly ran the toolchange sequence, but then it went to the start of the brim and seemingly randomly extruded a few lines in varying directions, unrelated the print geometry.

            The start gcode for this file is:

            ; Run nozzle diameter and filament check
            M98 P"0:/sys/System Macros/Config Checks/nozzle_check.g" L0.6 S0.6
            M98 P"0:/sys/System Macros/Config Checks/filament_check.g" L"NYLON" S"PVA"
            
            ; set extruder temp
            M568 P0 S275 R170 A1
            M568 P1 S210 R120 A1
            
            ; Set and wait for bed temp
            M190 S80
            
            ; Home all axes
            G28
            
            ; Enable mesh compensation
            M98 P"0:/sys/System Macros/Config Checks/load_heightmap.g"
            
            ; Move to starting position
            G0 H2 X{move.axes[0].min} Y50 F6000
            
            ; Select first tool
            T0
            
            ; Move near start
            G1 X251.37 Y156.171 Z2.3 F12000
            G21 ; set units to millimeters
            G90 ; use absolute coordinates
            M83 ; use relative distances for extrusion
            T0
            M116 P0 S5
            ; Filament gcode
            
            
            
            M572 D0 S0.006
            M107
            ;LAYER_CHANGE
            ;Z:0.3
            ;HEIGHT:0.3
            

            The macros called can be found here:
            https://github.com/HartSmart-Products/HSP1-I-SD-Image/tree/main

            edit: Attached is the version report for all duet components
            10a6f68d-0018-4a62-89ab-c983e006c5cf-image.png

            She/Her
            I work at a local 3D printing shop.
            Printers: Micron+ w/Duet 3 Mini, in-progress adaptation of the Jubilee REL onto an E3D MS, Prusa i3 MK3S.

            1 Reply Last reply Reply Quote 0
            • dc42undefined
              dc42 administrators @curieos
              last edited by dc42

              @curieos said in M116 Hanging after M568 Error:

              @dc42 This is in SBC mode, can I just upload these to the FW directory and send the update commands?

              As you have already installed 3.5.0-rc3 from the package server, yes you can. However, to get the full fix you will need a DSF update too. We expect to release rc4 very soon.

              Duet WiFi hardware designer and firmware engineer
              Please do not ask me for Duet support via PM or email, use the forum
              http://www.escher3d.com, https://miscsolutions.wordpress.com

              1 Reply Last reply Reply Quote 0
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