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    Manual bed probing / Mesh bed compensation Issue [DUET3]

    Scheduled Pinned Locked Moved Unsolved
    Tuning and tweaking
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    • Pierrelitoundefined
      Pierrelito
      last edited by

      Somehow I also get "Push(): Stack Overflow" when jogging the Z axis too fast and the machine goes back to Point 1

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      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        What firmware version specifically are you using? Please provide the results of M122.

        Z-Bot CoreXY Build | Thingiverse Profile

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        • Pierrelitoundefined
          Pierrelito
          last edited by Pierrelito

          I am using the 3.1.1 on the Mainboard 6HC and the 3.0 on the expansion 3HC, in SBC Mode. I thought the Expansion was on 3.1.0 but it seems that even though the 3.1.0 bin is here the machine never acknowledged it

          Here is the result of M122:

          M122
          === Diagnostics ===
          RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode)
          Board ID: 08DJM-956L2-G43S4-6J1DL-3SD6Q-1S5AF
          Used output buffers: 1 of 40 (13 max)
          === RTOS ===
          Static ram: 154604
          Dynamic ram: 163684 of which 52 recycled
          Exception stack ram used: 224
          Never used ram: 74652
          Tasks: NETWORK(ready,1972) HEAT(blocked,1212) CanReceiv(suspended,3520) CanSender(suspended,1488) CanClock(blocked,1452) TMC(blocked,204) MAIN(running,4928) IDLE(ready,76)
          Owned mutexes:
          === Platform ===
          Last reset 00:01:26 ago, cause: power up
          Last software reset at 2020-07-20 15:10, reason: User, spinning module LinuxInterface, available RAM 73960 bytes (slot 1)
          Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
          Error status: 0
          MCU temperature: min 22.9, current 33.0, max 33.1
          Supply voltage: min 24.0, current 24.0, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
          12V rail voltage: min 12.2, current 12.2, max 12.3, under voltage events: 0
          Driver 0: standstill, reads 30616, writes 14 timeouts 0, SG min/max 0/0
          Driver 1: standstill, reads 30616, writes 14 timeouts 0, SG min/max 0/0
          Driver 2: standstill, reads 30617, writes 14 timeouts 0, SG min/max 0/0
          Driver 3: standstill, reads 30617, writes 14 timeouts 0, SG min/max 0/0
          Driver 4: standstill, reads 30617, writes 14 timeouts 0, SG min/max 0/0
          Driver 5: standstill, reads 30621, writes 11 timeouts 0, SG min/max 0/0
          Date/time: 2020-07-21 08:10:04
          Slowest loop: 5.43ms; fastest: 0.14ms
          === Storage ===
          Free file entries: 10
          SD card 0 not detected, interface speed: 37.5MBytes/sec
          SD card longest read time 0.0ms, write time 0.0ms, max retries 0
          === Move ===
          Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
          Bed compensation in use: none, comp offset 0.000
          === MainDDARing ===
          Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
          === AuxDDARing ===
          Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
          === Heat ===
          Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = 6 -1 -1 -1
          === GCodes ===
          Segments left: 0
          Movement lock held by null
          HTTP* is ready with "M122" in state(s) 0
          Telnet is idle in state(s) 0
          File is idle in state(s) 0
          USB is idle in state(s) 0
          Aux is idle in state(s) 0
          Trigger* is idle in state(s) 0
          Queue is idle in state(s) 0
          LCD is idle in state(s) 0
          SBC is idle in state(s) 0
          Daemon* is idle in state(s) 0
          Aux2 is idle in state(s) 0
          Autopause is idle in state(s) 0
          Code queue is empty.
          === Network ===
          Slowest loop: 1.02ms; fastest: 0.01ms
          Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
          HTTP sessions: 0 of 8

          • Ethernet -
            State: disabled
            Error counts: 0 0 0 0 0
            Socket states: 0 0 0 0 0 0 0 0
            === CAN ===
            Messages sent 278, longest wait 2ms for type 6011
            === Linux interface ===
            State: 0, failed transfers: 0
            Last transfer: 17ms ago
            RX/TX seq numbers: 2064/2065
            SPI underruns 0, overruns 0
            Number of disconnects: 0
            Buffer RX/TX: 0/0-0
            === Duet Control Server ===
            Duet Control Server v1.3.2.0
            Code buffer space: 4096
            Configured SPI speed: 8000000 Hz
            Full transfers per second: 0.03

          ad for the Expansion Board 1
          M122 B1
          Diagnostics for board 1:
          Board EXP3HC firmware 3.0RC1 2019-12-16b1
          Never used RAM 162.8Kb, max stack 304b
          HEAT 1088 CanAsync 1452 CanRecv 1428 TMC 168 AIN 532 MAIN 2224
          Driver 0: standstill, reads 35834, writes 14 timeouts 0, SG min/max 0/0
          Driver 1: standstill, reads 35837, writes 14 timeouts 0, SG min/max 0/0
          Driver 2: standstill, reads 35842, writes 11 timeouts 0, SG min/max 0/0
          Moves scheduled 0, completed 0, hiccups 0
          VIN: 24.0V, V12: 12.1V
          MCU temperature: min 32.4C, current 32.7C, max 32.9C
          Ticks since heat task active 81, ADC conversions started 222824, completed 222824, timed out 0
          NVM user row de9a9239 aeecffb1 ffffffff ffffffff

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          • Pierrelitoundefined
            Pierrelito
            last edited by Pierrelito

            the expansion Is now on 3.1.0
            M122B1
            Diagnostics for board 1:
            Board EXP3HC firmware 3.1.0 (2020-05-15b1)
            Never used RAM 163.6Kb, max stack 312b
            HEAT 1272 CanAsync 1452 CanRecv 1420 TMC 156 AIN 524 MAIN 2184
            Last reset 00:00:37 ago, cause: software
            Driver 0: standstill, reads 9689, writes 11 timeouts 0, SG min/max 0/0
            Driver 1: standstill, reads 9691, writes 11 timeouts 0, SG min/max 0/0
            Driver 2: standstill, reads 9694, writes 11 timeouts 0, SG min/max 0/0
            Moves scheduled 0, completed 0, hiccups 0
            VIN: 24.0V, V12: 12.1V
            MCU temperature: min 32.4C, current 32.7C, max 32.9C
            Ticks since heat task active 91, ADC conversions started 37834, completed 37834, timed out 0
            Last sensors broadcast 00000000 found 0 94 ticks ago
            Free CAN buffers: 36
            NVM user row de9a9239 aeecffb1 ffffffff ffffffff

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            • Phaedruxundefined
              Phaedrux Moderator @Pierrelito
              last edited by

              @Pierrelito said in Manual bed probing / Mesh bed compensation Issue [DUET3]:

              When moving the Z axis to make the nozzle touch the bed, the machine often randomly goes back to the starting height (dive height) of the point. But the worst happens at points different than the first one. The machine goes back to the first point calibration for no reason...

              Can you provide a video of this behaviour?

              Z-Bot CoreXY Build | Thingiverse Profile

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              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                This may be related to using SBC mode and the dialogue boxes required. @chrishamm may have an idea.

                Z-Bot CoreXY Build | Thingiverse Profile

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                • chrishammundefined
                  chrishamm administrators
                  last edited by

                  I am quite surprised you are seeing Push errors. Are you running G29 as part of any macro file or do you start that from the DWC dropdown menu?

                  It may help to see a console log from DCS with log level debug. Please refer to this section for further details.

                  Duet software engineer

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                  • Pierrelitoundefined
                    Pierrelito
                    last edited by

                    I am using the dropdown menu for True Bed leveling (same behavior with the mesh bed compensation).

                    You can see it the Z axis going up again in this video.(around 0.18) It happens the most when the Z jogging is quite fast but also randomly.

                    And in this video (interesting part at 1.15), you can see the machine going back the first probing point while I'm probing the third one.

                    As requested by @chrishamm I'll try to get the DCS Log level

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                    • Pierrelitoundefined
                      Pierrelito
                      last edited by

                      Here is the result of the debug
                      [info] Settings loaded
                      [info] Environment initialized
                      [info] Connection to Duet established
                      [info] IPC socket created at /var/run/dsf/dcs.sock
                      [debug] Requesting update of key boards, seq 0 -> 1
                      [debug] Requesting update of key directories, seq 0 -> 0
                      [debug] Requesting update of key fans, seq 0 -> 2
                      [debug] Requesting update of key heat, seq 0 -> 24
                      [debug] Requesting update of key inputs, seq 0 -> 0
                      [debug] Requesting update of key job, seq 0 -> 0
                      [debug] Requesting update of key move, seq 0 -> 29
                      [debug] Requesting update of key network, seq 0 -> 2
                      [debug] Requesting update of key sensors, seq 0 -> 8
                      [debug] Requesting update of key spindles, seq 0 -> 0
                      [debug] Requesting update of key state, seq 0 -> 0
                      [debug] Requesting update of key tools, seq 0 -> 10
                      [debug] Requesting update of key volumes, seq 0 -> 0
                      [debug] Updated key boards
                      [debug] Updated key directories
                      [debug] Updated key fans
                      [debug] Updated key heat
                      [error] Failed to merge JSON: {"key":"inputs","flags":"d99vn","result":[{"axesRelative":false,"compatibility":"RepRapFirmware","distanceUnit":"mm","drivesRelative":true,"feedRate":50.0,"inMacro":false,"lineNumber":0,"name":"HTTP","stackDepth":0,"state":"idle","volumetric":false},{"axesRelative":false,"compatibility":"Marlin","distanceUnit":"mm","drivesRelative":true,"feedRate":50.0,"inMacro":false,"lineNumber":0,"name":"Telnet","stackDepth":0,"state":"idle","volumetric":false},{"axesRelative":false,"compatibility":"RepRapFirmware","distanceUnit":"mm","drivesRelative":true,"feedRate":50.0,"inMacro":false,"lineNumber":0,"name":"File","stackDepth":0,"state":"idle","volumetric":false},{"axesRelative":false,"compatibility":"Marlin","distanceUnit":"mm","drivesRelative":true,"feedRate":50.0,"inMacro":false,"lineNumber":0,"name":"USB","stackDepth":0,"state":"idle","volumetric":false},{"axesRelative":false,"compatibility":"RepRapFirmware","distanceUnit":"mm","drivesRelative":true,"feedRate":50.0,"inMacro":false,"lineNumber":0,"name":"Aux","stackDepth":0,"state":"idle","volumetric":false},{"axesRelative":false,"compatibility":"RepRapFirmware","distanceUnit":"mm","drivesRelative":true,"feedRate":50.0,"inMacro":false,"lineNumber":0,"name":"Trigger","stackDepth":0,"state":"idle","volumetric":false},{"axesRelative":false,"compatibility":"RepRapFirmware","distanceUnit":"mm","drivesRelative":true,"feedRate":50.0,"inMacro":false,"lineNumber":0,"name":"Queue","stackDepth":0,"state":"idle","volumetric":false},{"axesRelative":false,"compatibility":"RepRapFirmware","distanceUnit":"mm","drivesRelative":true,"feedRate":50.0,"inMacro":false,"lineNumber":0,"name":"LCD","stackDepth":0,"state":"idle","volumetric":false},{"axesRelative":false,"compatibility":"RepRapFirmware","distanceUnit":"mm","drivesRelative":true,"feedRate":50.0,"inMacro":false,"lineNumber":0,"name":"SBC","stackDepth":0,"state":"idle","volumetric":false},{"axesRelative":false,"compatibility":"RepRapFirmware","distanceUnit":"mm","drivesRelative":true,"feedRate":50.0,"inMacro":true,"lineNumber":0,"name":"Daemon","stackDepth":1,"state":"idle","volumetric":false},{"axesRelative":false,"compatibility":"RepRapFirmware","distanceUnit":"mm","drivesRelative":true,"feedRate":50.0,"inMacro":false,"lineNumber":0,"name":"Aux2","stackDepth":0,"state":"idle","volumetric":false},{"axesRelative":false,"compatibility":"RepRapFirmware","distanceUnit":"mm","drivesRelative":true,"feedRate":50.0,"inMacro":false,"lineNumber":0,"name":"Autopause","stackDepth":0,"state":"idle","volumetric":false}]}
                      System.Text.Json.JsonException: Failed to deserialize property [InputChannel].Name (type CodeChannel) from JSON "Aux2"
                      ---> System.Text.Json.JsonException: The JSON value could not be converted to DuetAPI.CodeChannel. Path: $ | LineNumber: 0 | BytePositionInLine: 6.
                      at System.Text.Json.ThrowHelper.ThrowJsonException()
                      at System.Text.Json.Serialization.Converters.JsonConverterEnum1.Read(Utf8JsonReader& reader, Type typeToConvert, JsonSerializerOptions options) at System.Text.Json.JsonPropertyInfoNotNullable4.OnRead(ReadStack& state, Utf8JsonReader& reader)
                      at System.Text.Json.JsonPropertyInfo.Read(JsonTokenType tokenType, ReadStack& state, Utf8JsonReader& reader)
                      at System.Text.Json.JsonSerializer.ReadCore(JsonSerializerOptions options, Utf8JsonReader& reader, ReadStack& readStack)
                      at System.Text.Json.JsonSerializer.ReadCore(Type returnType, JsonSerializerOptions options, Utf8JsonReader& reader)
                      at System.Text.Json.JsonSerializer.Deserialize(String json, Type returnType, JsonSerializerOptions options)
                      at DuetAPI.Machine.ModelObject.UpdateFromJson(JsonElement jsonElement, Boolean ignoreSbcProperties) in /home/christian/duet/DuetSoftwareFramework/src/DuetAPI/Machine/Base/ModelObject.cs:line 282
                      --- End of inner exception stack trace ---
                      at DuetAPI.Machine.ModelObject.UpdateFromJson(JsonElement jsonElement, Boolean ignoreSbcProperties) in /home/christian/duet/DuetSoftwareFramework/src/DuetAPI/Machine/Base/ModelObject.cs:line 287
                      at DuetAPI.Machine.ModelCollectionHelper.UpdateFromJson(IList list, Type itemType, JsonElement jsonElement, Boolean ignoreSbcProperties) in /home/christian/duet/DuetSoftwareFramework/src/DuetAPI/Machine/Base/ModelCollection.cs:line 214
                      at DuetAPI.Machine.MachineModel.UpdateFromFirmwareModel(String key, JsonElement jsonElement) in /home/christian/duet/DuetSoftwareFramework/src/DuetAPI/Machine/MachineModel.cs:line 162
                      at DuetControlServer.Model.Updater.Run() in /home/christian/duet/DuetSoftwareFramework/src/DuetControlServer/Model/Updater.cs:line 176
                      [debug] Updated key move
                      [debug] Updated key network
                      [debug] Updated key sensors
                      [debug] Updated key spindles
                      [debug] Updated key state
                      [debug] Updated key tools
                      [debug] Updated key volumes

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                      • Pierrelitoundefined
                        Pierrelito
                        last edited by

                        To make it was due to the SBC, I configured the duet in standalone mode and everything worked.
                        I might need the sbc in the future.

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