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    short-to-ground reported by driver 0 1 2 4. Help Needed

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    • maxspongebobundefined
      maxspongebob
      last edited by

      I am new to the Duet board but have been building CNC machines for a while. This is a new install of a Duet 3 6HC on a newly created printer.

      Whenever I try any motion the short-to-ground error is given. I have tripple checked all the wiring, tested the motors and wires on other systems and also used a meter to check/verify the wiring and coils in the motors. There is no short in the wires or motors.

      I am at a loss. I have searched forum and found others with similar errors but they usually had wiring issues. I don't all the motors work, tested individually on the good driver channels.

      Here is my configuration file and a list of the errors.

      ; Configuration file for Duet 3 (firmware version 3)
      ; executed by the firmware on start-up
      ;

      ; --------------- Pin/connection Mapping Legend -------------------
      ; out0 - UNUSED
      ; out1 - Extruder 1 heater
      ; out2
      ; out3
      ; out4
      ; out5
      ; out6
      ; out7 - Solid State Relay 1 (Bed Heater)
      ; out8 - Solid State Relay 2 (unused)
      ; out9 - Run Signal to Limits/E-Stop board.
      ; out4.tach
      ; out5.tach
      ; out6.tach
      ; io0.in - X limit switch. Active High Signal.
      ; io1.in - Y limit switch. Active High Signal.
      ; io2.in - Z limit switch. Active High Signal.
      ; io3.in - Emergency stop from Limits/E-Stop board.
      ; io4.in - Unused Signal from Limits/E-Stop board.
      ; io5.in
      ; io6.in
      ; io7.in - BL-Touch
      ; io8.in
      ; io0.out
      ; io1.out
      ; io2.out
      ; io3.out
      ; io4.out
      ; io5.out
      ; io6.out
      ; io7.out - BL-Touch
      ; io8.out
      ; pson
      ; spi.cs0
      ; spi.cs1
      ; spi.cs2
      ; spi.cs3
      ; temp0 - Bed Thermistor
      ; temp1 - Hotend Thermistor
      ; temp2
      ; temp3
      ; mcu-temp - MCU sensor
      ; driver0 - XY Left NEMA 23 Stepper 4.0 Amps, 20 tooth GT2 belt.
      ; driver1 - XY Right NEMA 23 Stepper 4.0 Amps, 20 tooth GT2 belt.
      ; driver2 - Z Center/Rear NEMA 17 Stepper 1.5 Amps, Belt drive 3:1 reduction driving 1204 ballscrew.
      ; driver3 - Z Left/Front NEMA 17 Stepper 1.5 Amps, Belt drive 3:1 reduction driving 1204 ballscrew.
      ; driver4 - Z Right/Front NEMA 17 Stepper 1.5 Amps, Belt drive 3:1 reduction driving 1204 ballscrew.
      ; driver5 - Extruder, NEMA 17 Stepper 1.3 Amps, 14:1 planetary geared, driving Bondtech Drivegear 35mm/rotation
      ; -----------------------------------------------------------------

      ; generated by RepRapFirmware Configuration Tool v3.1.4 on Fri Aug 14 2020 15:56:18 GMT-0400 (Eastern Daylight Time)

      ; General preferences
      G04 P2000 ; Pause for 2 seconds.
      G90 ; send absolute coordinates...
      M83 ; ...but relative extruder moves
      M550 P"Duet 3" ; set printer name
      G21 ; Set units to Millimeters.
      M669 K1 ; select CoreXY mode

      ; Drives
      M569 P0.0 S1 ; physical drive 0.0 goes forwards
      M569 P0.1 S1 ; physical drive 0.1 goes forwards
      M569 P0.2 S1 ; physical drive 0.2 goes forwards
      M569 P0.3 S0 ; physical drive 0.3 goes forwards
      M569 P0.4 S1 ; physical drive 0.4 goes forwards
      M569 P0.5 S1 ; physical drive 0.5 goes forwards

      ; Next Line Modified.
      M584 X0.0 Y0.1 Z0.2:0.3:0.4 E0.5 ; set drive mapping. 3 Z motors
      M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation

      ; Next Line Modified. Uncomment and update when data is known.
      ; Set up three Z-axis location
      ;M671 X-52.5:377.5:377.5 Y162.5:282.5:42.5 S5 ; leadscrews at 1 - left, 2 - rear right and 3 - front right

      M92 X80.00 Y80.00 Z2400.00 E420.00 ; set steps per mm
      M566 X900.00 Y900.00 Z12.00 E120.00 ; set maximum instantaneous speed changes (mm/min)
      M203 X6000.00 Y6000.00 Z600.00 E1200.00 ; set maximum speeds (mm/min)
      M201 X500.00 Y500.00 Z20.00 E250.00 ; set accelerations (mm/s^2)
      M906 X3000 Y3000 Z1000 E800 I50 ; set motor currents (mA) and motor idle factor in per cent
      M84 S30 ; Set idle timeout

      ; Axis Limits
      M208 X0 Y0 Z0 S1 ; set axis minima
      M208 X230 Y210 Z200 S0 ; set axis maxima

      ; Endstops
      M574 X1 S1 P"io0.in" ; configure active-high endstop for low end on X via pin io0.in
      M574 Y1 S1 P"io1.in" ; configure active-high endstop for low end on Y via pin io1.in
      M574 Z1 S1 P"io2.in" ; configure active-high endstop for low end on Z via pin io2.in

      ; Z-Probe
      M950 S0 C"io7.out" ; create servo pin 0 for BLTouch
      M558 P9 C"^io7.in" H5 F120 T6000 ; set Z probe type to bltouch and the dive height + speeds
      G31 P500 X0 Y32 Z2.5 ; set Z probe trigger value, offset and trigger height
      M557 X15:215 Y15:195 S20 ; define mesh grid

      ; Heaters
      M308 S0 P"temp0" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin temp0
      ; Next Line Modified.
      M950 H0 C"out7" T0 ; create bed heater output on out7 and map it to sensor 0
      M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit
      M140 H0 ; map heated bed to heater 0
      M143 H0 S120 ; set temperature limit for heater 0 to 120C
      M308 S1 P"temp1" Y"thermistor" T100000 B4138 ; configure sensor 1 as thermistor on pin temp1
      M950 H1 C"out1" T1 ; create nozzle heater output on out1 and map it to sensor 1
      M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit

      ; Fans
      M950 F0 C"out4" Q500 ; create fan 0 on pin out4 and set its frequency
      M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned off
      M950 F1 C"out5" Q500 ; create fan 1 on pin out5 and set its frequency
      M106 P1 S1 H1 T45 ; set fan 1 value. Thermostatic control is turned on
      M950 F2 C"out6" Q500 ; create fan 2 on pin out6 and set its frequency
      M106 P2 S1 H1 T45 ; set fan 2 value. Thermostatic control is turned on

      ; Tools
      M563 P0 D0 H1 F0 ; define tool 0
      G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
      G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C

      ; Emergency Stop
      M574 S1 P"^!io3.in" ; Define Emergency endstop - emergency stop switch condition
      M581 P"io3.in" T0 ; Define action to be taken with activation of emergency stop switch

      ; Miscellaneous
      T0 ; select first tool
      M501 ; Store parameters

      8/15/2020, 8:57:43 AM Emergency stop, attemping to reconnect...
      8/15/2020, 8:57:42 AM Warning: Firmware halted
      8/15/2020, 8:57:38 AM Error: short-to-ground reported by driver(s) 0 1 2 4
      8/15/2020, 8:57:34 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:57:29 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:57:25 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:57:20 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:57:16 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:57:11 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:57:07 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:57:02 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:56:58 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:56:53 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:56:49 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:56:44 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:56:40 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:56:36 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:56:31 AM Error: short-to-ground reported by driver(s) 2 4
      8/15/2020, 8:56:17 AM Connected to 10.102.1.114

      droftartsundefined 1 Reply Last reply Reply Quote 0
      • droftartsundefined
        droftarts administrators @maxspongebob
        last edited by

        @maxspongebob sorry for the inconvenience, this is a known issue with a short run of boards. Please see this thread for info and what to do: https://forum.duet3d.com/topic/18011/duet-3-6hc-short-to-ground-issue?

        In short, contact Duet3D for a warranty replacement.

        Ian

        Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

        1 Reply Last reply Reply Quote 0
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