Error : Failed to get macro response from SBC (channel file)
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Installed RRF 3.2.0beta4 + DWC 3.2.0beta4 on an machine :
Duet 3 6HC + Duet3 EXP3HC (controlling 2 heads + Bed leveling) + SBC RaspberryPi4 + 7 inches screen, Pi4 powered by a 5A power supplySince I have installed RRF3.2.0beta4, I get error messages :
RRF 3.2.0beta4 Error : Failed to get macro response within 8000ms from SBC (channel file)
M122 Give that :
01/12/2020 à 09:18:29 M122 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.2-beta4 running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode) Board ID: 08DJM-956L2-G43S4-6JKDD-3SS6J-TB7AH Used output buffers: 1 of 40 (11 max) === RTOS === Static ram: 123212 Dynamic ram: 138860 of which 184 recycled Never used RAM 129936, free system stack 126 words Tasks: Linux(ready,77) HEAT(blocked,272) CanReceiv(blocked,819) CanSender(blocked,339) CanClock(blocked,352) TMC(blocked,18) MAIN(running,1179) IDLE(ready,19) Owned mutexes: HTTP(MAIN) === Platform === Last reset 17:23:20 ago, cause: software Last software reset details not available Error status: 0x00 MCU temperature: min 39.1, current 46.4, max 51.0 Supply voltage: min 23.7, current 24.3, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0 Driver 0: position 14364, standstill, reads 5618, writes 13 timeouts 0, SG min/max 0/1023 Driver 1: position 212977, standstill, reads 5619, writes 13 timeouts 0, SG min/max 0/1023 Driver 2: position 1536000, standstill, reads 5619, writes 13 timeouts 0, SG min/max 0/1023 Driver 3: position 0, standstill, reads 5619, writes 13 timeouts 0, SG min/max 0/1023 Driver 4: position 0, standstill, reads 5631, writes 0 timeouts 0, SG min/max not available Driver 5: position 0, standstill, reads 5631, writes 0 timeouts 0, SG min/max not available Date/time: 2020-12-01 08:18:28 Slowest loop: 4096.47ms; fastest: 0.13ms === Storage === Free file entries: 10 SD card 0 not detected, interface speed: 37.5MBytes/sec SD card longest read time 0.0ms, write time 0.0ms, max retries 0 === Move === Hiccups: 0(0), FreeDm: 375, MinFreeDm: 313, MaxWait: 18988068ms Bed compensation in use: mesh, comp offset 0.000 === MainDDARing === Scheduled moves 97, completed moves 97, StepErrors 0, LaErrors 0, Underruns [0, 0, 9], CDDA state -1 === AuxDDARing === Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1 Heater 0 is on, I-accum = 0.2 Heater 1 is on, I-accum = 0.0 === GCodes === Segments left: 0 Movement lock held by null HTTP* is doing "M122" in state(s) 0 Telnet is idle in state(s) 0 File* is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger* is idle in state(s) 0 Queue* is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 Code queue is empty. === CAN === Messages queued 478167, send timeouts 0, received 750297, lost 0, longest wait 1ms for reply type 6024, free buffers 47 === SBC interface === State: 0, failed transfers: 0 Last transfer: 18ms ago RX/TX seq numbers: 52732/54384 SPI underruns 0, overruns 0 Number of disconnects: 1, IAP RAM available 0x20a00 Buffer RX/TX: 0/0-0 === Duet Control Server === Duet Control Server v3.2.0-beta4 File: Buffered code: G1 Z10 F1000 ; Move the head ==> 36 bytes Executing macro bed.g, started by G32 ; bed leveling > Next stack level Suspended code: G92 E0 : ;Prime the extruders Suspended code: G1 E4 Suspended code: T1 Suspended code: G92 E0 Suspended code: G1 E4 Suspended code: T0 Suspended code: G1 Z15.0 F6000 ;Move the platform down 15mm Suspended code: G92 E0 Suspended code: M82 ;absolute extrusion mode Suspended code: T0 Suspended code: M83 ;relative extrusion mode Suspended code: M83 ;relative extrusion mode Suspended code: G1 Z15.0 F6000 ;Move the platform down 15mm Suspended code: G92 E0 Suspended code: G1 F200 E3 Suspended code: G92 E0 Suspended code: M83 ;relative extrusion mode Suspended code: G1 F2400 E-1 Suspended code: ;LAYER_COUNT:351 Suspended code: ;LAYER:0 Suspended code: M107 Suspended code: G0 F3600 X70.175 Y47.713 Z0.2 Suspended code: G1 F2400 E1.43038 Suspended code: G1 F1500 X70.332 Y47.494 E0.00974 Suspended code: G1 X70.658 Y47.107 E0.01829 Suspended code: G1 X70.865 Y46.916 E0.01018 Suspended code: G1 X71.008 Y46.795 E0.00677 Suspended code: G1 X71.415 Y46.463 E0.01899 Code buffer space: 4096 Configured SPI speed: 8000000 Hz Full transfers per second: 36.48 File /opt/dsf/sd/gcodes/NEW-Ceinture-MASTER x2.gcode is selected, processing 01/12/2020 à 08:32:24 Error: Failed to get macro response within 8000ms from SBC (channel File) 01/12/2020 à 08:22:40 M32 "0:/gcodes/NEW-Ceinture-MASTER x2.gcode" File 0:/gcodes/NEW-Ceinture-MASTER x2.gcode selected for printing 01/12/2020 à 08:22:34 Envoi de NEW-Ceinture-MASTER x2.gcode réussi après 7s 01/12/2020 à 03:11:59 Finished printing file 0:/gcodes/maylis_dhaultfoeuille_piece1_ok.gcode, print time was 10h 3m 30/11/2020 à 20:23:37 Connected to 10.136.20.132
Any Idea ?
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If you are using start.g, please share it. The output of M122 may be helpful, too.
Also, please open a console on the Pi, send
journalctl -u duetcontrolserver -e
once the error occurred, and post the log here. -
M122 is on the post,
Sorry, the format is strange (my customer do it) :
=== Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.2-beta4 running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode) Board ID: 08DJM-956L2-G43S4-6JKDD-3SS6J-TB7AH Used output buffers: 1 of 40 (11 max) === RTOS === Static ram: 123212 Dynamic ram: 138860 of which 184 recycled Never used RAM 129936, free system stack 126 words Tasks: Linux(ready,77) HEAT(blocked,272) CanReceiv(blocked,819) CanSender(blocked,339) CanClock(blocked,352) TMC(blocked,18) MAIN(running,1179) IDLE(ready,19) Owned mutexes: HTTP(MAIN) === Platform === Last reset 17:23:20 ago, cause: software Last software reset details not available Error status: 0x00 MCU temperature: min 39.1, current 46.4, max 51.0 Supply voltage: min 23.7, current 24.3, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0 Driver 0: position 14364, standstill, reads 5618, writes 13 timeouts 0, SG min/max 0/1023 Driver 1: position 212977, standstill, reads 5619, writes 13 timeouts 0, SG min/max 0/1023 Driver 2: position 1536000, standstill, reads 5619, writes 13 timeouts 0, SG min/max 0/1023 Driver 3: position 0, standstill, reads 5619, writes 13 timeouts 0, SG min/max 0/1023 Driver 4: position 0, standstill, reads 5631, writes 0 timeouts 0, SG min/max not available Driver 5: position 0, standstill, reads 5631, writes 0 timeouts 0, SG min/max not available Date/time: 2020-12-01 08:18:28 Slowest loop: 4096.47ms; fastest: 0.13ms === Storage === Free file entries: 10 SD card 0 not detected, interface speed: 37.5MBytes/sec SD card longest read time 0.0ms, write time 0.0ms, max retries 0 === Move === Hiccups: 0(0), FreeDm: 375, MinFreeDm: 313, MaxWait: 18988068ms Bed compensation in use: mesh, comp offset 0.000 === MainDDARing === Scheduled moves 97, completed moves 97, StepErrors 0, LaErrors 0, Underruns [0, 0, 9], CDDA state -1 === AuxDDARing === Scheduled moves 0, completed moves 0, StepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1 Heater 0 is on, I-accum = 0.2 Heater 1 is on, I-accum = 0.0 === GCodes === Segments left: 0 Movement lock held by null HTTP* is doing "M122" in state(s) 0 Telnet is idle in state(s) 0 File* is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger* is idle in state(s) 0 Queue* is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 Code queue is empty. === CAN === Messages queued 478167, send timeouts 0, received 750297, lost 0, longest wait 1ms for reply type 6024, free buffers 47 === SBC interface === State: 0, failed transfers: 0 Last transfer: 18ms ago RX/TX seq numbers: 52732/54384 SPI underruns 0, overruns 0 Number of disconnects: 1, IAP RAM available 0x20a00 Buffer RX/TX: 0/0-0 === Duet Control Server === Duet Control Server v3.2.0-beta4 File: Buffered code: G1 Z10 F1000 ; Move the head ==> 36 bytes Executing macro bed.g, started by G32 ; bed leveling > Next stack level Suspended code: G92 E0 : ;Prime the extruders Suspended code: G1 E4 Suspended code: T1 Suspended code: G92 E0 Suspended code: G1 E4 Suspended code: T0 Suspended code: G1 Z15.0 F6000 ;Move the platform down 15mm Suspended code: G92 E0 Suspended code: M82 ;absolute extrusion mode Suspended code: T0 Suspended code: M83 ;relative extrusion mode Suspended code: M83 ;relative extrusion mode Suspended code: G1 Z15.0 F6000 ;Move the platform down 15mm Suspended code: G92 E0 Suspended code: G1 F200 E3 Suspended code: G92 E0 Suspended code: M83 ;relative extrusion mode Suspended code: G1 F2400 E-1 Suspended code: ;LAYER_COUNT:351 Suspended code: ;LAYER:0 Suspended code: M107 Suspended code: G0 F3600 X70.175 Y47.713 Z0.2 Suspended code: G1 F2400 E1.43038 Suspended code: G1 F1500 X70.332 Y47.494 E0.00974 Suspended code: G1 X70.658 Y47.107 E0.01829 Suspended code: G1 X70.865 Y46.916 E0.01018 Suspended code: G1 X71.008 Y46.795 E0.00677 Suspended code: G1 X71.415 Y46.463 E0.01899 Code buffer space: 4096 Configured SPI speed: 8000000 Hz Full transfers per second: 36.48 File /opt/dsf/sd/gcodes/NEW-Ceinture-MASTER x2.gcode is selected, processing -
I don't use start.g
The config.g
; Configuration file for Duet 3 (firmware version 3) ; executed by the firmware on start-up ; ; ;--------------------------------------------------- ; General preferences ;--------------------------------------------------- G90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"qu3-lt" ; set printer name ;--------------------------------------------------- ; Network ;--------------------------------------------------- M552 S1 P192.168.0.74/24 ; Activate Network with IP 192.168.0.74 netmask 255.255.255.0 (/24) Only for Duet3 connected by RJ45 M554 P192.168.0.1 ; Set Gateway 192.168.0.1 M586 P0 S1 ; Activate HTTP protocol M586 P2 S1 R23 ; Configure Telnet on port 23 ;M555 P5 ; Set compatibility Repetier (currently 2020-02-29 Not activated in the Firmware, will be updated in future version) ;--------------------------------------------------- ; Drives ;--------------------------------------------------- M569 P0.0 S1 ; X physical drive 0.0 goes forwards M569 P0.1 S1 ; Y physical drive 0.1 goes forwards M569 P0.2 S1 ; Z0 physical drive 0.2 goes forwards M569 P0.3 S1 ; Z1 physical drive 0.3 goes forwards M569 P1.0 S0 ; physical drive 1.0 goes forwards M569 P1.1 S0 ; physical drive 1.1 goes forwards M584 X0.0 Y0.1 Z0.2:0.3 E1.0:1.1 ; set drive mapping M350 X256 Y256 Z128 E128:128 I0 ; configure microstepping without interpolation M92 X711.11 Y711.11 Z5120 E4656.00:4656.00 ; set steps per mm M566 X400.00 Y400.00 Z100.00 E120.00:120.00 ; set maximum instantaneous speed changes (mm/min) M203 X10000.00 Y10000.00 Z500.00 E400.00:400.00 ; set maximum speeds (mm/min) M201 X300.00 Y300.00 Z40.00 E5000.00:5000.00 ; set accelerations (mm/s^2) (was M201 X800.00 Y800.00 Z40.00 E250.00:250.00 ) M906 X1500 Y1500 Z2800 E800:800 I70 ; set motor currents (mA) and motor idle factor in per cent M84 S30 XY ; Set idle timeout ;--------------------------------------------------- ; Axis Limits ;--------------------------------------------------- M208 X0 Y0 Z0 S1 ; set axis minima M208 X350 Y350 Z300 S0 ; set axis maxima ;--------------------------------------------------- ; Endstops ;--------------------------------------------------- M574 X1 S1 P"!0.io1.in" ; configure active-high endstop for low end on X via pin io1.in M574 Y1 S1 P"!0.io2.in" ; configure active-high endstop for low end on Y via pin io2.in M574 Z1 S1 P"!0.io3.in" ; configure active-high endstop for low end on Z via pin io3.in ;--------------------------------------------------- ; Z-Probe ;--------------------------------------------------- M558 P8 C"1.io0.in" H10 F500 T15000 ; set Z probe type to switch and the dive height + speeds G31 X0 Y0 Z4.07 ; set Z probe trigger value, offset and trigger height M557 X35:345 Y20:310 P5 ; define mesh grid ;--------------------------------------------------- ; Heaters ;--------------------------------------------------- M308 S0 P"temp0" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin temp0 M950 H0 C"out0" T0 ; create bed heater output on out0 and map it to sensor 0 M143 H0 S120 ; set temperature limit for heater 0 to 120C M307 H0 A160.3 C979.4 D1.9 V24.2 S0.9 B0 ; AutoTuning parameters disable bang-bang mode for the bed heater and set PWM limit M140 H0 ; map heated bed to heater 0 M308 S1 P"1.temp0" Y"thermistor" T100000 B4138 ; configure sensor 1 as thermistor on pin 1.temp0 M950 H1 C"1.out0" T1 ; create nozzle heater output on 1.out0 and map it to sensor 1 M143 H1 S280 ; set temperature limit for heater 1 to 280C M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit M308 S2 P"1.temp1" Y"thermistor" T100000 B4138 ; configure sensor 2 as thermistor on pin 1.temp1 M950 H2 C"1.out1" T2 ; create nozzle heater output on 1.out1 and map it to sensor 2 M143 H2 S280 ; set temperature limit for heater 2 to 280C M307 H2 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit ;--------------------------------------------------- ; Cooling Part Fans ;--------------------------------------------------- M950 F0 C"1.out3" Q4 ; create fan 0 on pin 1.out3 and set its frequency to 4hz to have variable speed M106 P0 X255 S0 H-1 ; set fan 0 value. Thermostatic control is turned off M950 F1 C"1.out4" Q4 ; create fan 1 on pin 1.out4 and set its frequency to 4hz to have variable speed M106 P1 X255 S0 H-1 ; set fan 1 value. Thermostatic control is turned off ;--------------------------------------------------- ; Cooling Head Fans ;--------------------------------------------------- M950 F0 C"!1.out3+^out3.tach" Q25000 ; create fan 0 on pin 1.out3 and set PWM frequency 1.out3 on Qu3 Head Sunon PF36281BX-S99 M106 P0 S0 ; set fan 0 value. Thermostatic control is turned off M950 F1 C"!1.out4+^out4.tach" Q25000 ; create fan 1 on pin 1.out4 and set PWM frequency 1.out4 on Qu3 Head Sunon PF36281BX-S99 M106 P1 S0 ; set fan 1 value. Thermostatic control is turned off ;--------------------------------------------------- ; LED Light ;--------------------------------------------------- M950 F4 C"0.out3" Q500 ; create fan 4 "Eclairage Interne" on pin 0.out3 and set its frequency M106 P4 S1 H-1 ;--------------------------------------------------- ; Enclosure HEPA FAN ;--------------------------------------------------- M950 F5 C"0.out1" Q500 ; create fan 5 "Filtre HEPA" on pin 0.out5 and set its frequency M106 P5 S1 H-1 ;--------------------------------------------------- ; Tools ;--------------------------------------------------- M563 P0 S"TETE 0" D0 H1 F0 ; define tool 0 G10 P0 X-20.2 Y0.5 Z0 ; set tool 0 axis offsets G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C M563 P1 S"TETE 1" D1 H2 F1 ; define tool 1 G10 P1 X21.1 Y10.6 Z0.30 ; set tool 1 axis offsets G10 P1 R0 S0 ; set initial tool 1 active and standby temperatures to 0C ;--------------------------------------------------- ;Servo ;--------------------------------------------------- M950 S0 C"1.io1.out" ; Create Servo 0 Port with 1.io4.out M280 P0 S1700 I1 ; Switch to Head 1 G4 S3 ; Wait 3 sec the time the servo finish move M280 P0 S1010 I1 ; Switch to Head 0 G4 S3 ; Wait 3 sec the time the servo finish move --------------------------------------------------- ;End Of Filament Detection ;--------------------------------------------------- M950 J7 C"!0.io7.in" ; create pin 7 for end of filament detection M581 P7 T2 ; filament monitor T0 connected to 0.io7.in and execute trigger2.g file M950 J8 C"!0.io8.in" ; create pin 8 for end of filament detection M581 P8 T3 ; filament monitor T1 connected to 0.io8.in and execute trigger3.g file ;--------------------------------------------------- ;Homing at start ;--------------------------------------------------- ;G28 ; Custom settings are not defined ; Miscellaneous ;M501 ; load saved parameters from non-volatile memory M911 S20 R23 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss T0 ; select first tool
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I call my customer, take the control of the pi and send you the log soon...
Note : it seems to appear only with the 3.2.0beta4
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The log of Pi :
pi@qu3-lt:~ $ journalctl -u duetcontrolserver -e Dec 01 07:32:25 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:25 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:25 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:25 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:25 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [error] Failed to get macro respo Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [info] Starting macro file retrac Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 ( Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [info] Finished macro file retrac Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] File: Pending out-of-order Dec 01 08:01:41 qu3-lt DuetControlServer[388]: [info] Starting macro file homeal Dec 01 08:02:52 qu3-lt DuetControlServer[388]: [info] Finished macro file homeal lines 119-141/141 (END) Dec 01 07:32:25 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:25 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:25 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:25 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:25 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [error] Failed to get macro response within 8000ms from SBC (channel File) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [info] Starting macro file retractprobe.g on channel File Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] Resending packet type #0 (request LockMovementAndWaitForStandstill) Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [info] Finished macro file retractprobe.g Dec 01 07:32:26 qu3-lt DuetControlServer[388]: [warn] File: Pending out-of-order reply: '' Dec 01 08:01:41 qu3-lt DuetControlServer[388]: [info] Starting macro file homeall.g on channel HTTP Dec 01 08:02:52 qu3-lt DuetControlServer[388]: [info] Finished macro file homeall.g
The header of GCode
;FLAVOR:RepRap ;TIME:36333 ;Filament used: 52.3015m, 0m ;Layer height: 0.25 ;MINX:43.084 ;MINY:35.498 ;MINZ:0.2 ;MAXX:284.579 ;MAXY:264.698 ;MAXZ:87.7 ;Generated with Cura_SteamEngine 4.8.0-beta T0 M190 S60 M104 S190 M109 S190 M82 ;absolute extrusion mode G28 ;Home M929 P"eventlog.txt" S1 T0 ; Select T0 before doing a bed leveling G1 X175 Y150 Z15 G32 ; bed leveling G92 E0 : ;Prime the extruders G1 E4 T1 G92 E0 G1 E4 T0 G1 Z15.0 F6000 ;Move the platform down 15mm ;Prime the extruder G92 E0 M82 ;absolute extrusion mode T0 M83 ;relative extrusion mode M83 ;relative extrusion mode G1 Z15.0 F6000 ;Move the platform down 15mm ;Prime the extruder G92 E0 G1 F200 E3 G92 E0 M83 ;relative extrusion mode G1 F2400 E-1 ;LAYER_COUNT:351 ;LAYER:0 M107 G0 F3600 X70.175 Y47.713 Z0.2 ;TYPE:SKIRT G1 F2400 E1.43038 G1 F1500 X70.332 Y47.494 E0.00974 G1 X70.658 Y47.107 E0.01829 G1 X70.865 Y46.916 E0.01018 G1 X71.008 Y46.795 E0.00677...
Note : I have checked the header of GCode is the same than the GCode printed last night i doesn't give macro SBC error...
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I am sorry but I have not managed to reproduce this problem on my setup with your G-code. Can you please share the following macro files as well:
- homeall.g
- bed.g
- retractprobe.g
- deployprobe.g
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retractprobe.g homeall.g deployprobe.g config.g bed.g
Thank you