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    Duet 3 3.2 Beta2 + SBC jerking motion

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    Beta Firmware
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    • Garfieldundefined
      Garfield
      last edited by

      Appreciated Dave, I was about to report but have refrained since doing so would have been premature - and the kiss of death.

      So far running direct with no SBC and 3.2 b 2 I've had a print running 30 mins or so with zero issues so far.

      If you need me to do any testing let me know. I've created a completely new SD card to run local and can easily pop the Pi back on.

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      • Garfieldundefined
        Garfield
        last edited by

        Said it was the kiss of death ....

        So no jolts or odd behaviour - except now the print failed 1hr 14 into the print with Error 1 - Cannot read file.

        File reads fine via the Duet GUI, can be downloaded, edited, viewed to the end etc etc
        File reads fine with the SD card on the PC - scanned with notepad++ - no defects in file -

        I will try again and see if it chokes at the same point.

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        • Garfieldundefined
          Garfield
          last edited by

          Was just a glitch - file has printed fine now for hours ... all print defects are gone, the jolts are gone with the Pi removed from the equation.

          Phaedruxundefined 1 Reply Last reply Reply Quote 0
          • Phaedruxundefined
            Phaedrux Moderator @Garfield
            last edited by

            @Garfield said in Duet 3 3.2 Beta2 jerking motion:

            the jolts are gone with the Pi removed from the equation.

            Thanks for the confirmation.

            Z-Bot CoreXY Build | Thingiverse Profile

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            • tristanryerparkeundefined
              tristanryerparke
              last edited by tristanryerparke

              I had this issue with the Pi4 plus Duet3 on the 3.2 beta as well, went back to the stable to avoid it. Now after upgrading to 3.2rc1 I am still having this "jolting" issue.
              I need to run the sbc as ethernet connection is not an option in my workshop.

              Phaedruxundefined 1 Reply Last reply Reply Quote 0
              • Phaedruxundefined
                Phaedrux Moderator @tristanryerparke
                last edited by

                @tristanryerparke Can you give some more details about your setup? config.g, etc.

                Z-Bot CoreXY Build | Thingiverse Profile

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                • tristanryerparkeundefined
                  tristanryerparke
                  last edited by

                  Gantry style five axis machine. Nema23 on X,Y. Nema17 on Z,A,B. Duet 3 mainboard and one toolboard controlling the b axis and z probe.
                  Dual motors for Y axis, auto squaring with U axis.
                  Config;

                  ;CNC Mode
                  M453
                  ;Brake Pins
                  M950 P2 C"out8"
                  M950 P1 C"out7"
                  ;Drivers
                  M569 P0.0 S0  I1
                  M569 P0.1 S0  I1
                  M569 P0.2 S1  I1
                  M569 P0.3 S0  I1
                  M569 P0.4 S0  I1
                  M569 P121.0 S1 I1
                  ;Driver Mapping
                  M584 X0.3 Y0.1:0.2  Z0.0  A0.4  B121.0 P5
                  M584 U0.2 P5
                  ;Current
                  M906 X2000 Y3750    Z2000 U3750 A1750 B1500 I100
                  ;Microstepping
                  M350 X16   Y16      Z16   U16   A16 I1 
                  ;Steps Per MM
                  M92  X80   Y80      Z80   U80  A46.1062140618 B26.6666
                  ;Instantaneous Speed Change
                  M566 X500   Y500      Z500   U500   A500
                  ;Max Speeds
                  M203 X13000 Y13000    Z13000 U6000 A40000 B40000
                  ;Max Acceleration
                  M201 X750  Y750     Z500  U750 A2000 B2000
                  ;Disable Idle Current Reduction
                  M84 S0    
                  M917 Y100
                  ;Probe
                  M558 P9 C"!^121.io0.in" H200 F400 T2000 I1
                  ;Limits
                  M208 X0    Y-1360 Z-145 A-72000 B-101.4 S1
                  M208 X1242 Y0     Z0    A72000  B230 S0
                  ;Servos
                  M950 S3 C"io4.out"
                  M950 S4 C"io5.out"
                  ;Endstops
                  M574 U1 S1 P"!io6.in"
                  M574 Y1 S1 P"!io1.in"
                  M574 X1 S1 P"io8.in"
                  M574 Z1 S1 P"io7.in"
                  M574 A1 S1 P"io0.in"
                  ;Head Endstop
                  M574 B1 S1 P"121.io2.in"
                  ;Tool 0
                  M563 P0 S"Probe"
                  ;Tool 1
                  M563 P1 S"1/4 Flat Brush"
                  ;Tool 2
                  M563 P2 S"5/8 Flat Brush"
                  ;Allow Movement
                  M564 S0 H0
                  
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                  • Phaedruxundefined
                    Phaedrux Moderator
                    last edited by

                    RC2 is now out, can you test with that?

                    Z-Bot CoreXY Build | Thingiverse Profile

                    tristanryerparkeundefined 1 Reply Last reply Reply Quote 0
                    • tristanryerparkeundefined
                      tristanryerparke @Phaedrux
                      last edited by

                      @Phaedrux Just tried with RC2, no luck and jerks happen in the same places on same file.

                      Phaedruxundefined 1 Reply Last reply Reply Quote 1
                      • Phaedruxundefined
                        Phaedrux Moderator @tristanryerparke
                        last edited by

                        @tristanryerparke I'm just noticing in your config some rather large spacing between some values. Is that intentional? Can you send M98 P"config.g" to check for errors? Can you send some of those commands like M208 or M201 etc by themselves to see if all of the values for all axis are being set as expected?

                        Z-Bot CoreXY Build | Thingiverse Profile

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                        • tristanryerparkeundefined
                          tristanryerparke @Phaedrux
                          last edited by

                          @Phaedrux yes the spacing was large just for readability/comparing values for axes.
                          I have removed the spacing so config.g now looks like this:

                          ;CNC Mode
                          M453
                          ;Name
                          M550 P"tristan-painting-machine"
                          ;Brake Pins
                          M950 P2 C"out8"
                          M950 P1 C"out7"
                          ;Drivers
                          M569 P0.0 S0  I1
                          M569 P0.1 S0  I1
                          M569 P0.2 S1  I1
                          M569 P0.3 S0  I1
                          M569 P0.4 S0  I1
                          M569 P121.0 S1 I1
                          ;Driver Mapping
                          M584 X0.3 Y0.1:0.2  Z0.0  A0.4  B121.0 P5
                          M584 U0.2 P5
                          ;Current
                          M906 X2000 Y3750 Z2000 U3750 A1750 B1500 I100
                          ;Microstepping
                          M350 X16 Y16 Z16 U16 A16 I1 
                          ;Steps Per MM
                          M92 X80 Y80 Z80 U80 A46.1062140618 B26.6666
                          ;Instantaneous Speed Change
                          M566 X500 Y500 Z500 U500 A500
                          ;Max Speeds
                          M203 X13000 Y13000 Z13000 U6000 A40000 B40000
                          ;Max Acceleration
                          M201 X750 Y750 Z500 U750 A2000 B2000
                          ;Disable Idle Current Reduction
                          M84 S0    
                          M917 Y100
                          ;Probe
                          M558 P9 C"!^121.io0.in" H200 F400 T2000 I1
                          ;Limits
                          M208 X0 Y-1360 Z-145 A-72000 B-101.4 S1
                          M208 X1242 Y0 Z0 A72000 B230 S0
                          ;Servos
                          M950 S3 C"io4.out"
                          M950 S4 C"io5.out"
                          ;Endstops
                          M574 U1 S1 P"!io6.in"
                          M574 Y1 S1 P"!io1.in"
                          M574 X1 S1 P"!io8.in"
                          M574 Z1 S1 P"io7.in"
                          M574 A1 S1 P"io0.in"
                          ;Head Endstop
                          M574 B1 S1 P"121.io2.in"
                          ;Tool 0
                          M563 P0 S"Probe"
                          ;Tool 1
                          M563 P1 S"1/4 Flat Brush"
                          ;Tool 2
                          M563 P2 S"5/8 Flat Brush"
                          ;Allow Movement
                          M564 S0 H0
                          

                          Running 3.2 stable now and the issue is still happening. M98 P"config.g" runs fine with no errors.
                          Here is video of one of the clunks:
                          https://youtu.be/egwhWUq8yAg
                          As you can see the system is not losing steps, it just stops for a fraction of a second without accelerating/decelerating.
                          Maybe I should make a new thread for this issue?
                          Let me know.
                          Cheers,
                          T

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                          • Phaedruxundefined
                            Phaedrux Moderator @tristanryerparke
                            last edited by

                            @tristanryerparke said in Duet 3 3.2 Beta2 + SBC jerking motion:

                            Maybe I should make a new thread for this issue?

                            Is this different than the initial issue?

                            Z-Bot CoreXY Build | Thingiverse Profile

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                            • Phaedruxundefined
                              Phaedrux Moderator @tristanryerparke
                              last edited by

                              @tristanryerparke said in Duet 3 3.2 Beta2 + SBC jerking motion:

                              A0.4 B121.0

                              Are those rotational axis? Did you notice the note in the release notes for 3.2?

                              Z-Bot CoreXY Build | Thingiverse Profile

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                              • tristanryerparkeundefined
                                tristanryerparke @Phaedrux
                                last edited by

                                @Phaedrux I believe this is the same issue as the what the OP had.
                                I did read the notes for 3.2, A and B axes are rotational and should be defaulting to that within the first M584 command, correct?
                                I will try now explicitly defining them as rotational.
                                Also something interesting:
                                I just started messing around with the M595 command to see if I could fix the clunks.
                                So far I have tried S=5, S=10, S=50, S=100 and S=1000.
                                All of these made the clunking way worse!
                                Very strange.
                                T

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                                • Phaedruxundefined
                                  Phaedrux Moderator @tristanryerparke
                                  last edited by

                                  @tristanryerparke said in Duet 3 3.2 Beta2 + SBC jerking motion:

                                  I believe this is the same issue as the what the OP had.

                                  Ah, sorry, I didn't notice that you weren't the OP.

                                  Yes please create a new thread.

                                  Z-Bot CoreXY Build | Thingiverse Profile

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