Duet3D Logo Duet3D
    • Tags
    • Documentation
    • Order
    • Register
    • Login

    6HC+2x 3HC+SBC. 3.2 Crashes at high print speed.

    Scheduled Pinned Locked Moved
    Beta Firmware
    4
    39
    1.1k
    Loading More Posts
    • Oldest to Newest
    • Newest to Oldest
    • Most Votes
    Reply
    • Reply as topic
    Log in to reply
    This topic has been deleted. Only users with topic management privileges can see it.
    • jrocklandundefined
      jrockland @fcwilt
      last edited by

      @fcwilt they are running independent, one feeding the main 6hc and the second feeding both 3hc's (each power supply have 3 output)

      fcwiltundefined 1 Reply Last reply Reply Quote 1
      • fcwiltundefined
        fcwilt @jrockland
        last edited by

        @jrockland said in High performance issues.. Not bashing here, just a question.:

        @fcwilt they are running independent, one feeding the main 6hc and the second feeding both 3hc's (each power supply have 3 output)

        Good that should be safe - I think.

        Frederick

        Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

        1 Reply Last reply Reply Quote 0
        • jrocklandundefined
          jrockland @Phaedrux
          last edited by

          @Phaedrux
          ; General preferences
          G90 ; send absolute coordinates...
          M83 ; ...but relative extruder moves
          M550 P"MEGATOR" ; set printer name
          M669 K1 ; select DBL H-BOT mode

          ; Drives
          M569 P0.0 S0
          M569 P0.1 S0
          M569 P0.2 S0
          M569 P0.3 S0
          M569 P0.4 S0
          M569 P0.5 S1
          M569 P1.0 S0
          M569 P1.1 S1
          M569 P2.0 S0
          M569 P2.1 S1
          M584 X2.0:1.1 Y1.0:2.1 E0.4:0.5 Z0.0:0.3:0.2:0.1 U0.0 V0.3 W0.2 A0.1 P3
          M671 X-55:-55.0:365.0:365.0 Y-120.0:430.0:430.0:-120.0 S10.0 P1.0
          M350 X64 Y64 E1:1 Z1 I1
          M92 X320.00 Y320.00 E26.00:26.00 Z600.00 ; Steps per MM
          M566 X480.00 Y480.00 E18000.00:18000.00 Z20.00 ; set maximum instantaneous speed changes (mm/min)
          M203 X72000.00 Y72000.00 E72000.00:72000.00 Z200 ; set maximum speeds (mm/min)
          M201 X360 Y360 E4800.00:4800.00 Z80.00 ; set accelerations (mm/s^2)
          M906 X1200 Y1200 E800:800 Z1200 I30 ; set motor currents (mA) and motor idle factor in per cent
          M84 S10 ; Set idle timeout

          ; Axis Limits
          M208 X0 Y0 Z0 S1
          M208 X280 Y400 Z255 S0
          M557 X-51:222 Y2:398 S50

          ; Endstops
          M574 X1 S1 P"!2.io1.in"
          M574 Y1 S1 P"!1.io1.in"
          M574 U1 S1 P"!io0.in"
          M574 V1 S1 P"!io1.in"
          M574 W1 S1 P"!io2.in"

          ;Emergency Stop
          M581 T2 U1 S1 C0
          M581 T2 V1 S1 C0
          M581 T2 W1 S1 C0

          ; Z-Probe
          M558 P5 C"!io7.in" I1 S25.0
          G31 P100 X-53.0 Z1.05

          ; Heaters
          M308 S0 P"Temp0" Y"thermistor" A"Left" T100000 B4138
          M950 H0 C"out1" T0
          M307 H0 R2.724 C123.2 D5.23 S1.00 V24.1
          M308 S1 P"Temp1" Y"thermistor" A"Right" T100000 B4138
          M950 H1 C"out2" T1
          M307 H1 R3.292 C146.8 D3.42 S1.00 V24.1

          ; Fans
          M950 F0 C"out7"
          M106 P0 S0 H0 T100 L255
          M950 F1 C"out8"
          M106 P1 S0 H1 T100 L255
          M950 F2 C"out4"
          M106 P2

          ; Tools
          M563 P0 S"LEFT" D0 H0 F2
          M563 P1 S"RIGHT" D1 H1

          ; Miscellaneous
          ;M501 ; load saved parameters from non-volatile memory
          M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
          G10 P0 R200 S200
          G10 P1 Y-23.50 X0.0 R200 S200

          1 Reply Last reply Reply Quote 0
          • jrocklandundefined
            jrockland @Phaedrux
            last edited by

            @Phaedrux
            21/01/2021, 21:01:28 m98 P"config.g"
            Error: M550: Machine name must consist of the same letters and digits as configured by the Linux hostname
            Fan 2, speed: 0%, min: 10%, max: 100%, blip: 0.10

            Phaedruxundefined 1 Reply Last reply Reply Quote 0
            • jrocklandundefined
              jrockland @Phaedrux
              last edited by

              @Phaedrux
              21/01/2021, 21:00:17 m122
              === Diagnostics ===
              RepRapFirmware for Duet 3 MB6HC version 3.2 running on Duet 3 MB6HC v1.01 or later (SBC mode)
              Board ID: 08DJM-956L2-G43S4-6J1F8-3SD6T-9V56D
              Used output buffers: 1 of 40 (16 max)
              === RTOS ===
              Static ram: 149788
              Dynamic ram: 63136 of which 56 recycled
              Never used RAM 145852, free system stack 200 words
              Tasks: Linux(ready,105) HEAT(blocked,296) CanReceiv(blocked,848) CanSender(blocked,371) CanClock(blocked,356) TMC(blocked,53) MAIN(running,1157) IDLE(ready,19)
              Owned mutexes: HTTP(MAIN)
              === Platform ===
              Last reset 00:02:27 ago, cause: power up
              Last software reset at 2021-01-21 19:47, reason: MemoryProtectionFault mmarValid daccViol, GCodes spinning, available RAM 145604, slot 2
              Software reset code 0x4163 HFSR 0x00000000 CFSR 0x00000082 ICSR 0x00400804 BFAR 0x0048ba20 SP 0x2041fb80 Task MAIN Freestk 1646 ok
              Stack: 2041e168 2041e168 00000002 732f2e2d 000000c7 0046b2c3 0046ab04 210f0000 0046b2c0 610f0000 00000000 00000000 00000000 00000000 204180d8 00000000 2041e168 2042ae18 00000000 00000001 00000000 0046ad93 2042ae18 00000000 2042ae18 0046b0ff 2042a908
              Error status: 0x00
              Aux0 errors 0,0,0
              Aux1 errors 0,0,0
              MCU temperature: min 18.9, current 32.6, max 32.7
              Supply voltage: min 24.2, current 24.2, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes
              12V rail voltage: min 12.0, current 12.1, max 12.1, under voltage events: 0
              Driver 0: position 0, standstill, reads 41583, writes 14 timeouts 0, SG min/max 0/0
              Driver 1: position 0, standstill, reads 41583, writes 14 timeouts 0, SG min/max 0/0
              Driver 2: position 0, standstill, reads 41583, writes 14 timeouts 0, SG min/max 0/0
              Driver 3: position 0, standstill, reads 41583, writes 14 timeouts 0, SG min/max 0/0
              Driver 4: position 0, standstill, reads 41583, writes 14 timeouts 0, SG min/max 0/0
              Driver 5: position 0, standstill, reads 41584, writes 14 timeouts 0, SG min/max 0/0
              Date/time: 2021-01-21 21:00:16
              Slowest loop: 0.47ms; fastest: 0.07ms
              === Storage ===
              Free file entries: 10
              SD card 0 not detected, interface speed: 37.5MBytes/sec
              SD card longest read time 0.0ms, write time 0.0ms, max retries 0
              === Move ===
              DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000
              === MainDDARing ===
              Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
              === AuxDDARing ===
              Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
              === Heat ===
              Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
              === GCodes ===
              Segments left: 0
              Movement lock held by null
              HTTP* is doing "M122" in state(s) 0
              Telnet is idle in state(s) 0
              File is idle in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger* is idle in state(s) 0
              Queue is idle in state(s) 0
              LCD is idle in state(s) 0
              SBC is idle in state(s) 0
              Daemon is idle in state(s) 0
              Aux2 is idle in state(s) 0
              Autopause is idle in state(s) 0
              Code queue is empty.
              === CAN ===
              Messages queued 486, send timeouts 0, received 18, lost 0, longest wait 1ms for reply type 6018, free buffers 48
              === SBC interface ===
              State: 4, failed transfers: 0
              Last transfer: 1ms ago
              RX/TX seq numbers: 4154/4154
              SPI underruns 0, overruns 0
              Number of disconnects: 0, IAP RAM available 0x2c8a8
              Buffer RX/TX: 0/0-0
              === Duet Control Server ===
              Duet Control Server v3.2.0
              Code buffer space: 4096
              Configured SPI speed: 8000000 Hz
              Full transfers per second: 0.95
              Maximum length of RX/TX data transfers: 4102/924

              1 Reply Last reply Reply Quote 0
              • Phaedruxundefined
                Phaedrux Moderator @jrockland
                last edited by

                @jrockland said in High performance issues.. Not bashing here, just a question.:

                Error: M550: Machine name must consist of the same letters and digits as configured by the Linux hostname
                Fan 2, speed: 0%, min: 10%, max: 100%, blip: 0.10

                The first one is pretty obvious what it means. The fan 2 is because you have M106 P2 with nothing else so it's just reporting the settings of fan2.

                I should have also asked if you could send M122 B1 and M122 B2 to check the expansion boards as well.

                @jrockland said in High performance issues.. Not bashing here, just a question.:

                Last software reset at 2021-01-21 19:47, reason: MemoryProtectionFault mmarValid daccViol, GCodes spinning, available RAM 145604, slot 2

                Was that M122 captured after it crashed?

                Z-Bot CoreXY Build | Thingiverse Profile

                jrocklandundefined 1 Reply Last reply Reply Quote 0
                • jrocklandundefined
                  jrockland @Phaedrux
                  last edited by

                  @Phaedrux
                  m550 I have that on all my machines, never took the time to look into it..

                  I will launch another "test run" tomorrow then take the m122 from all the boards when it crash

                  1 Reply Last reply Reply Quote 0
                  • Phaedruxundefined
                    Phaedrux Moderator
                    last edited by

                    Use M122 B1 and M122 B2 before your test to make sure the expansions are running 3.2 as well. If not, send M997 B1 and M997 B2 to flash them as well.

                    Z-Bot CoreXY Build | Thingiverse Profile

                    jrocklandundefined 2 Replies Last reply Reply Quote 0
                    • jrocklandundefined
                      jrockland @Phaedrux
                      last edited by

                      @Phaedrux
                      So I did flash them to the last update (they where at 2020-12-20, they are now at 2021-01-05)
                      and here my m122 and m122 b1/b2

                      22/01/2021, 11:47:39 m122
                      === Diagnostics ===
                      RepRapFirmware for Duet 3 MB6HC version 3.2 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                      Board ID: 08DJM-956L2-G43S4-6J1F8-3SD6T-9V56D
                      Used output buffers: 1 of 40 (16 max)
                      === RTOS ===
                      Static ram: 149788
                      Dynamic ram: 63132 of which 56 recycled
                      Never used RAM 145856, free system stack 200 words
                      Tasks: Linux(ready,111) HEAT(blocked,302) CanReceiv(blocked,848) CanSender(blocked,371) CanClock(blocked,352) TMC(blocked,53) MAIN(running,1202) IDLE(ready,19)
                      Owned mutexes: HTTP(MAIN)
                      === Platform ===
                      Last reset 00:01:19 ago, cause: power up
                      Last software reset at 2021-01-22 11:41, reason: User, none spinning, available RAM 145356, slot 1
                      Software reset code 0x0012 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0x00000000 Task Linu Freestk 0 n/a
                      Error status: 0x00
                      Aux0 errors 0,0,0
                      Aux1 errors 0,0,0
                      MCU temperature: min 38.9, current 39.5, max 39.7
                      Supply voltage: min 24.1, current 24.2, max 24.2, under voltage events: 0, over voltage events: 0, power good: yes
                      12V rail voltage: min 12.1, current 12.1, max 12.1, under voltage events: 0
                      Driver 0: position 0, standstill, reads 54751, writes 14 timeouts 0, SG min/max 0/0
                      Driver 1: position 0, standstill, reads 54751, writes 14 timeouts 0, SG min/max 0/0
                      Driver 2: position 0, standstill, reads 54752, writes 14 timeouts 0, SG min/max 0/0
                      Driver 3: position 0, standstill, reads 54752, writes 14 timeouts 0, SG min/max 0/0
                      Driver 4: position 0, standstill, reads 54752, writes 14 timeouts 0, SG min/max 0/0
                      Driver 5: position 0, standstill, reads 54752, writes 14 timeouts 0, SG min/max 0/0
                      Date/time: 2021-01-22 11:47:38
                      Slowest loop: 0.41ms; fastest: 0.05ms
                      === Storage ===
                      Free file entries: 10
                      SD card 0 not detected, interface speed: 37.5MBytes/sec
                      SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                      === Move ===
                      DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                      === MainDDARing ===
                      Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                      === AuxDDARing ===
                      Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                      === Heat ===
                      Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                      === GCodes ===
                      Segments left: 0
                      Movement lock held by null
                      HTTP* is doing "M122" in state(s) 0
                      Telnet is idle in state(s) 0
                      File is idle in state(s) 0
                      USB is idle in state(s) 0
                      Aux is idle in state(s) 0
                      Trigger* is idle in state(s) 0
                      Queue is idle in state(s) 0
                      LCD is idle in state(s) 0
                      SBC is idle in state(s) 0
                      Daemon is idle in state(s) 0
                      Aux2 is idle in state(s) 0
                      Autopause is idle in state(s) 0
                      Code queue is empty.
                      === CAN ===
                      Messages queued 212, send timeouts 0, received 18, lost 0, longest wait 1ms for reply type 6042, free buffers 48
                      === SBC interface ===
                      State: 4, failed transfers: 0
                      Last transfer: 1ms ago
                      RX/TX seq numbers: 1725/1725
                      SPI underruns 0, overruns 0
                      Number of disconnects: 0, IAP RAM available 0x2c8a8
                      Buffer RX/TX: 0/0-0
                      === Duet Control Server ===
                      Duet Control Server v3.2.0
                      Code buffer space: 4096
                      Configured SPI speed: 8000000 Hz
                      Full transfers per second: 4.15
                      Maximum length of RX/TX data transfers: 4102/812

                      22/01/2021, 11:48:26 m122 b2
                      Diagnostics for board 2:
                      Duet EXP3HC firmware version 3.2 (2021-01-05)
                      Bootloader ID: not available
                      Never used RAM 154848, free system stack 200 words
                      HEAT 77 CanAsync 94 CanRecv 87 TMC 64 MAIN 313 AIN 257
                      Last reset 00:02:07 ago, cause: reset button
                      Last software reset data not available
                      Driver 0: position 0, 320.0 steps/mm, standstill, reads 14960, writes 16 timeouts 0, SG min/max 0/0
                      Driver 1: position 0, 320.0 steps/mm, standstill, reads 14962, writes 16 timeouts 0, SG min/max 0/0
                      Driver 2: position 0, 80.0 steps/mm, standstill, reads 14970, writes 11 timeouts 0, SG min/max 0/0
                      Moves scheduled 0, completed 0, in progress 0, hiccups 0
                      No step interrupt scheduled
                      VIN: 24.2V, V12: 12.1V
                      MCU temperature: min 37.3C, current 37.5C, max 37.5C
                      Ticks since heat task active 248, ADC conversions started 127240, completed 127238, timed out 0
                      Last sensors broadcast 0x00000000 found 0 1 ticks ago, loop time 0
                      CAN messages queued 28, send timeouts 0, received 1035, lost 0, free buffers 36
                      22/01/2021, 11:48:09 m122 b1
                      Diagnostics for board 1:
                      Duet EXP3HC firmware version 3.2 (2021-01-05)
                      Bootloader ID: not available
                      Never used RAM 154848, free system stack 200 words
                      HEAT 102 CanAsync 94 CanRecv 87 TMC 64 MAIN 319 AIN 257
                      Last reset 00:01:50 ago, cause: reset button
                      Last software reset data not available
                      Driver 0: position 0, 320.0 steps/mm, standstill, reads 53562, writes 16 timeouts 0, SG min/max 0/0
                      Driver 1: position 0, 320.0 steps/mm, standstill, reads 53565, writes 16 timeouts 0, SG min/max 0/0
                      Driver 2: position 0, 80.0 steps/mm, standstill, reads 53573, writes 11 timeouts 0, SG min/max 0/0
                      Moves scheduled 0, completed 0, in progress 0, hiccups 0
                      No step interrupt scheduled
                      VIN: 24.2V, V12: 12.3V
                      MCU temperature: min 36.6C, current 36.6C, max 36.6C
                      Ticks since heat task active 50, ADC conversions started 110042, completed 110041, timed out 0
                      Last sensors broadcast 0x00000000 found 0 53 ticks ago, loop time 0
                      CAN messages queued 28, send timeouts 0, received 880, lost 0, free buffers 36

                      1 Reply Last reply Reply Quote 0
                      • jrocklandundefined
                        jrockland @Phaedrux
                        last edited by

                        @Phaedrux I realized something else: the pi actually do a reboot when the board shut down, it doesn't just loose power.

                        1 Reply Last reply Reply Quote 0
                        • Phaedruxundefined
                          Phaedrux Moderator
                          last edited by

                          Now that they are all on 3.2 hopefully that will show an improvement.

                          If it does crash again get an M122 afterwards and setup this monitoring on the pi.

                          https://duet3d.dozuki.com/Wiki/Getting_Started_With_Duet_3#Section_Monitoring_optional

                          Z-Bot CoreXY Build | Thingiverse Profile

                          jrocklandundefined 1 Reply Last reply Reply Quote 0
                          • jrocklandundefined
                            jrockland @Phaedrux
                            last edited by

                            @Phaedrux
                            I did but they didn't gave me any info, so I did it again and recorded the whole thing.
                            video here (1.30 min)
                            the video is not publish publicly, you can only see it from the link. I didn't want people to have the wrong idea.

                            you can see at 1:20 everything just *freeze as the whole system just quit.
                            when I reboot I have no error message or anything, it just boot as usual.

                            1 Reply Last reply Reply Quote 0
                            • Phaedruxundefined
                              Phaedrux Moderator
                              last edited by

                              And when it boots up again, gather a M122 so we can see what the last reset reason was.

                              Z-Bot CoreXY Build | Thingiverse Profile

                              jrocklandundefined 2 Replies Last reply Reply Quote 0
                              • jrocklandundefined
                                jrockland @Phaedrux
                                last edited by

                                @Phaedrux
                                m122
                                === Diagnostics ===
                                RepRapFirmware for Duet 3 MB6HC version 3.2 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                Board ID: 08DJM-956L2-G43S4-6J1F8-3SD6T-9V56D
                                Used output buffers: 1 of 40 (16 max)
                                === RTOS ===
                                Static ram: 149788
                                Dynamic ram: 63132 of which 56 recycled
                                Never used RAM 145856, free system stack 200 words
                                Tasks: Linux(ready,107) HEAT(blocked,302) CanReceiv(blocked,848) CanSender(blocked,371) CanClock(blocked,352) TMC(blocked,53) MAIN(running,1189) IDLE(ready,19)
                                Owned mutexes: HTTP(MAIN)
                                === Platform ===
                                Last reset 00:04:03 ago, cause: power up
                                Last software reset at 2021-01-22 13:19, reason: HardFault undefInstr, Platform spinning, available RAM 145856, slot 2
                                Software reset code 0x4060 HFSR 0x40000000 CFSR 0x00010000 ICSR 0x0440f803 BFAR 0x00000000 SP 0x2041fca8 Task MAIN Freestk 1720 ok
                                Stack: 0008eddf 00000000 204180d8 20420d58 000000af 00462ac7 00462ac6 610f0000 a5a5a5a5 a5a5a5a5 00000000 0046bd7f 00000001 fffc0000 204193df 00000000 2041dbcc a5a5a5a5 1a28e11f a5a5a5a5 a5a5a5a5 a5a5a5a5 a5a5a5a5 004170a1 204276c0 00462ac3 00000000
                                Error status: 0x00
                                Aux0 errors 0,0,0
                                Aux1 errors 0,0,0
                                MCU temperature: min 18.5, current 34.4, max 34.5
                                Supply voltage: min 24.2, current 24.2, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes
                                12V rail voltage: min 12.0, current 12.1, max 12.1, under voltage events: 0
                                Driver 0: position 0, standstill, reads 51221, writes 14 timeouts 0, SG min/max 0/0
                                Driver 1: position 0, standstill, reads 51221, writes 14 timeouts 0, SG min/max 0/0
                                Driver 2: position 0, standstill, reads 51221, writes 14 timeouts 0, SG min/max 0/0
                                Driver 3: position 0, standstill, reads 51222, writes 14 timeouts 0, SG min/max 0/0
                                Driver 4: position 0, standstill, reads 51222, writes 14 timeouts 0, SG min/max 0/0
                                Driver 5: position 0, standstill, reads 51222, writes 14 timeouts 0, SG min/max 0/0
                                Date/time: 2021-01-22 14:04:38
                                Slowest loop: 0.47ms; fastest: 0.06ms
                                === Storage ===
                                Free file entries: 10
                                SD card 0 not detected, interface speed: 37.5MBytes/sec
                                SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                                === Move ===
                                DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                                === MainDDARing ===
                                Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                === AuxDDARing ===
                                Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                === Heat ===
                                Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                === GCodes ===
                                Segments left: 0
                                Movement lock held by null
                                HTTP* is doing "M122" in state(s) 0
                                Telnet is idle in state(s) 0
                                File is idle in state(s) 0
                                USB is idle in state(s) 0
                                Aux is idle in state(s) 0
                                Trigger* is idle in state(s) 0
                                Queue is idle in state(s) 0
                                LCD is idle in state(s) 0
                                SBC is idle in state(s) 0
                                Daemon is idle in state(s) 0
                                Aux2 is idle in state(s) 0
                                Autopause is idle in state(s) 0
                                Code queue is empty.
                                === CAN ===
                                Messages queued 860, send timeouts 0, received 18, lost 0, longest wait 1ms for reply type 6018, free buffers 48
                                === SBC interface ===
                                State: 4, failed transfers: 0
                                Last transfer: 1ms ago
                                RX/TX seq numbers: 7514/7514
                                SPI underruns 0, overruns 0
                                Number of disconnects: 0, IAP RAM available 0x2c8a8
                                Buffer RX/TX: 0/0-0
                                === Duet Control Server ===
                                Duet Control Server v3.2.0
                                Code buffer space: 4096
                                Configured SPI speed: 8000000 Hz
                                Full transfers per second: 2.71
                                Maximum length of RX/TX data transfers: 4102/904

                                1 Reply Last reply Reply Quote 0
                                • jrocklandundefined
                                  jrockland @Phaedrux
                                  last edited by

                                  @Phaedrux
                                  I think we have our issue here: Last software reset at 2021-01-22 13:19, reason: HardFault undefInstr, Platform spinning, available RAM 145856, slot 2.
                                  Slot 2 mean the second 3HC in line right ?
                                  Im having some issue with him, loosing connection (red led start flashing fast). I didnt bother as it does the exact same job as the first 3HC the print was going anyway.

                                  1 Reply Last reply Reply Quote 0
                                  • Phaedruxundefined
                                    Phaedrux Moderator
                                    last edited by

                                    I've flagged this for review. Will just need to wait for time zones before anyone can take a look.

                                    Z-Bot CoreXY Build | Thingiverse Profile

                                    jrocklandundefined 1 Reply Last reply Reply Quote 0
                                    • jrocklandundefined
                                      jrockland @Phaedrux
                                      last edited by

                                      @Phaedrux
                                      Im having that fault every 10 min now while trying normal print speed..:
                                      HardFault undefInstr, Platform spinning, available RAM 145856, slot 2
                                      since I updated the boards.. Ill just shut it down for now.

                                      no worry I know we are not in the same time zones. thank for the help

                                      1 Reply Last reply Reply Quote 0
                                      • Phaedruxundefined
                                        Phaedrux Moderator
                                        last edited by

                                        If you disconnect that tool board entirely does the problem go with it?

                                        Z-Bot CoreXY Build | Thingiverse Profile

                                        jrocklandundefined 1 Reply Last reply Reply Quote 0
                                        • jrocklandundefined
                                          jrockland @Phaedrux
                                          last edited by

                                          @Phaedrux
                                          seem like it.
                                          as per my config.g file do you think I can move X-Y to the main board and the 4 Z to the extension boards ? (older version wouldn't accept my Z sensor on extension boards, and also the sensor will not be on the same board as all the Z (only 3 ports, 4 motors)..

                                          But that would solve the communication issue as Z barely receive anything compare to x and y..

                                          dc42undefined 1 Reply Last reply Reply Quote 0
                                          • dc42undefined
                                            dc42 administrators @jrockland
                                            last edited by

                                            @jrockland, there have been fixes to CAN communication at high movement rates in 3.3beta. But I don't think any of them accounts for the reset you are seeing. I will analyse the reset data.

                                            Duet WiFi hardware designer and firmware engineer
                                            Please do not ask me for Duet support via PM or email, use the forum
                                            http://www.escher3d.com, https://miscsolutions.wordpress.com

                                            1 Reply Last reply Reply Quote 0
                                            • First post
                                              Last post
                                            Unless otherwise noted, all forum content is licensed under CC-BY-SA