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Connecting 3 wire fan Toolboard

Scheduled Pinned Locked Moved
Duet Hardware and wiring
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  • undefined
    dk
    last edited by 29 Jan 2021, 00:10

    Hello
    I try to connect 3 wire FAN BLOWER 35X10MM 12VDC WIRE (Delta Electronics BFB03512HHA-AF00) to Out 1 of Toolboard.
    Fan start spinning at the power up and continues to spin at a constant speed regardless of the settings and commands M106 and M107.
    Wires connected: Black to GND, Red to +12V, Blue to out1

    ; Fans
    M950 F0 C"20.out1" Q1000 ; create fan 0 part cooling on pin 20.out1 and set its frequency
    M106 P0 S0 ; set fan 0 value. Thermostatic control is turned off
    M950 F1 C"20.out2" Q500 ; create fan 1 heatsink on pin 20.out2 and set its frequency
    M106 P1 S0 H1 T45 ; set fan 1 value. Thermostatic control is turned on 45C

    I tried several Q parameters. H-1 at M106 also didn't help.

    any ideas that I messed up?

    undefined 1 Reply Last reply 29 Jan 2021, 09:46 Reply Quote 0
    • undefined
      Phaedrux Moderator
      last edited by 29 Jan 2021, 00:12

      Please share your full config.g and the output of M122 and M122 B1

      What commands did you send specifically?

      Z-Bot CoreXY Build | Thingiverse Profile

      1 Reply Last reply Reply Quote 0
      • undefined
        dk
        last edited by 29 Jan 2021, 00:17

        M106 with S250 S0 S10 S100 and M107 does not effect on blower

        ; Configuration file for Duet 3 (firmware version 3)
        ; executed by the firmware on start-up
        ;
        ; generated by RepRapFirmware Configuration Tool v3.1.4 on Tue Sep 01 2020 22:07:15 GMT-0400 (EDT)

        ; General preferences
        G90 ; send absolute coordinates...
        M83 ; ...but relative extruder moves
        M550 P"Duet 3" ; set printer name
        M665 L460.000:460.000:460.000 R244.194 H673.6 B190.0 X-0.140 Y-0.034 Z0.000 ; Set delta radius, diagonal rod length, printable radius and homed height
        M666 X0.22 Y0.12 Z-0.34 A0.00 B0.00 ; put your endstop adjustments here, or let auto calibration find them

        ; Drives
        M569 P0.0 S1 ; physical drive 0.0 upper 0 tower goes back
        M569 P0.1 S0 ; physical drive 0.1 upper 1 tower goes forwards
        M569 P0.2 S1 ; physical drive 0.2 upper 2 tower goes back
        M569 P0.3 S0 ; physical drive 0.3 lower 2 tower goes forwards
        M569 P0.4 S0 ; physical drive 0.4 lower 1 tower forwards
        M569 P0.5 S0 ; physical drive 0.5 lower 0 tower goes forwards
        M569 P20.0 S0 ; physical drive 20.0 - extruder on board 20 goes Back
        M584 X0.1:0.4 Y0.0:0.5 Z0.2:0.3 E20.0 ; set drive mapping
        M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
        M92 X160.00 Y160.00 Z160.00 E415.00 ; set steps per mm
        M566 X800.00 Y800.00 Z800.00 E600.00 ; set maximum instantaneous speed changes (mm/min)
        M203 X5000.00 Y5000.00 Z5000.00 E600.00 ; set maximum speeds (mm/min)
        M201 X2000.00 Y2000.00 Z2000.00 E1000.00 ; set accelerations (mm/s^2)
        M906 X1600 Y1600 Z1600 E900 I30 ; set motor currents (mA) and motor idle factor in per cent
        M84 S30 ; Set idle timeout

        ; Axis Limits
        M208 Z0 S1 ; set minimum Z

        ; Endstops
        M574 X2 S1 P"io1.in" ; configure active-high endstop for HIGH end on X via pin io0.in
        M574 Y2 S1 P"io0.in" ; configure active-high endstop for HIGH end on Y via pin io1.in
        M574 Z2 S1 P"io2.in" ; configure active-high endstop for HIGH end on Z via pin io2.in

        ; Z-Probe
        M558 P8 C"20.io0.in" ; set Z probe type to 8 and
        G31 P50 X-21 Y-8 Z1 ; set Z probe trigger value, offset and trigger height
        M557 R150 S50 ; define mesh grid

        ; Heaters
        M308 S0 P"temp0" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin temp3
        M950 H0 C"out0" T0 ; create bed heater output on out1 and map it to sensor 0
        M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit
        M140 H0 ; map heated bed to heater 0
        M143 H0 S120 ; set temperature limit for heater 0 to 120C
        M308 S1 P"20.temp0" Y"thermistor" T500000 B4723 C1.19622e-7 ; configure sensor 1 as thermistor on pin 20.temp0
        M950 H1 C"20.out0" T1 ; create nozzle heater output on 20.out0 and map it to sensor 1
        M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit

        ; Fans
        M950 F0 C"20.out1" Q1000 ; create fan 0 part cooling on pin 20.out1 and set its frequency
        M106 P0 S0 ; set fan 0 value. Thermostatic control is turned off
        M950 F1 C"20.out2" Q500 ; create fan 1 heatsink on pin 20.out2 and set its frequency
        M106 P1 S0 H1 T45 ; set fan 1 value. Thermostatic control is turned on 45C

        ; Tools
        M563 P0 D0 H1 F0 ; define tool 0
        G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
        G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C

        ; Custom settings are not defined
        M501

        M122
        === Diagnostics ===
        RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode)
        Board ID: 08DJM-956L2-G43S4-6JTDJ-3SJ6S-986GH
        Used output buffers: 1 of 40 (10 max)
        === RTOS ===
        Static ram: 154604
        Dynamic ram: 161704 of which 160 recycled
        Exception stack ram used: 416
        Never used ram: 76332
        Tasks: NETWORK(ready,1972) HEAT(blocked,1188) CanReceiv(suspended,3460) CanSender(suspended,1460) CanClock(blocked,1436) TMC(blocked,68) MAIN(running,4960) IDLE(ready,76)
        Owned mutexes:
        === Platform ===
        Last reset 00:49:42 ago, cause: software
        Last software reset at 2021-01-28 23:24, reason: User, spinning module LinuxInterface, available RAM 75988 bytes (slot 2)
        Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
        Error status: 0
        MCU temperature: min 46.5, current 47.0, max 47.3
        Supply voltage: min 25.9, current 26.0, max 26.0, under voltage events: 0, over voltage events: 0, power good: yes
        12V rail voltage: min 12.2, current 12.3, max 12.3, under voltage events: 0
        Driver 0: standstill, reads 48539, writes 19 timeouts 0, SG min/max 0/199
        Driver 1: standstill, reads 48539, writes 19 timeouts 0, SG min/max 0/210
        Driver 2: standstill, reads 48540, writes 19 timeouts 0, SG min/max 0/220
        Driver 3: standstill, reads 48540, writes 19 timeouts 0, SG min/max 0/255
        Driver 4: standstill, reads 48541, writes 19 timeouts 0, SG min/max 0/207
        Driver 5: standstill, reads 48541, writes 19 timeouts 0, SG min/max 0/233
        Date/time: 2021-01-29 00:13:55
        Slowest loop: 4.77ms; fastest: 0.14ms
        === Storage ===
        Free file entries: 10
        SD card 0 not detected, interface speed: 37.5MBytes/sec
        SD card longest read time 0.0ms, write time 0.0ms, max retries 0
        === Move ===
        Hiccups: 0(0), FreeDm: 375, MinFreeDm: 369, MaxWait: 10723ms
        Bed compensation in use: none, comp offset 0.000
        === MainDDARing ===
        Scheduled moves: 5, completed moves: 5, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
        === AuxDDARing ===
        Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
        === Heat ===
        Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
        === GCodes ===
        Segments left: 0
        Movement lock held by null
        HTTP* is ready with "M122" in state(s) 0
        Telnet is idle in state(s) 0
        File is idle in state(s) 0
        USB is idle in state(s) 0
        Aux is idle in state(s) 0
        Trigger* is idle in state(s) 0
        Queue is idle in state(s) 0
        LCD is idle in state(s) 0
        SBC is idle in state(s) 0
        Daemon* is idle in state(s) 0 0, running macro
        Aux2 is idle in state(s) 0
        Autopause is idle in state(s) 0
        Code queue is empty.
        === Network ===
        Slowest loop: 0.82ms; fastest: 0.01ms
        Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
        HTTP sessions: 0 of 8

        • Ethernet -
          State: disabled
          Error counts: 0 0 0 0 0
          Socket states: 0 0 0 0 0 0 0 0
          === CAN ===
          Messages sent 11917, longest wait 3ms for type 6011
          === Linux interface ===
          State: 0, failed transfers: 0
          Last transfer: 22ms ago
          RX/TX seq numbers: 30007/30009
          SPI underruns 0, overruns 0
          Number of disconnects: 0
          Buffer RX/TX: 0/0-0
          === Duet Control Server ===
          Duet Control Server v3.1.1
          Code buffer space: 4096
          Configured SPI speed: 8000000 Hz
          Full transfers per second: 32.10

        M122 B20
        Diagnostics for board 20:
        Board TOOL1LC firmware 3.1.0 (2020-05-15b1)
        Never used RAM 8.5Kb, max stack 368b
        HEAT 1064 CanAsync 1428 CanRecv 1384 TMC 196 AIN 524 MAIN 2284
        Last reset 01:01:12 ago, cause: power up
        Driver 0: standstill, SG min/max 0/0, read errors 0, write errors 0, ifcount 13, reads 1283, writes 13, timeouts 1, DMA errors 0, failedOp 0x80
        Moves scheduled 0, completed 0, hiccups 0
        VIN: 26.1V
        MCU temperature: min 33.7C, current 36.8C, max 37.2C
        Ticks since heat task active 152, ADC conversions started 3658040, completed 3658038, timed out 0
        Last sensors broadcast 00000002 found 1 155 ticks ago
        Free CAN buffers: 36
        NVM user row b1d088a9 fffff8bb d33ea5c7 72796b23
        TSENS 000e6e GAIN 014eb1 OFFS 002812 CAL 1f2c

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        • undefined
          Phaedrux Moderator
          last edited by 29 Jan 2021, 04:53

          Can you do a sudo apt update followed by sudo apt upgrade to update your firmware? Check the versions again after updating. Both the main board and tool board should be 3.2.

          Z-Bot CoreXY Build | Thingiverse Profile

          1 Reply Last reply Reply Quote 0
          • undefined
            dc42 administrators @dk
            last edited by dc42 29 Jan 2021, 09:46

            @dk said in Connecting 3 wire fan Toolboard:

            Wires connected: Black to GND, Red to +12V, Blue to out1

            That's the wrong connection for a 3-wire fan. It should be: Red to +12V, black to OUT1_NEG, blue to OUT1_TACHO.

            The tacho reading will only be correct when the fan is running at full PWM, or off.

            Duet WiFi hardware designer and firmware engineer
            Please do not ask me for Duet support via PM or email, use the forum
            http://www.escher3d.com, https://miscsolutions.wordpress.com

            undefined 1 Reply Last reply 30 Jan 2021, 18:50 Reply Quote 0
            • undefined
              dk @dc42
              last edited by 30 Jan 2021, 18:50

              @dc42 Thank you David!

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