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    3.5b1 Reset reason: StuckInSpinLoop?

    Scheduled Pinned Locked Moved Solved
    Beta Firmware
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    • Diamondbackundefined
      Diamondback
      last edited by Diamondback

      @dc42 some more M122, I think I figured out why it didn't want to crash anymore yesterday (removed too much code from daemon), trying to reduce the code less now.

      === Diagnostics ===
      RepRapFirmware for Duet 3 MB6HC version 3.5beta1+ (2023-01-20 09:47:33) running on Duet 3 MB6HC v1.02 or later (standalone mode)
      Board ID: 08DJM-9P63L-DJ3T0-6J1F4-3S06S-9A1V9
      Used output buffers: 3 of 40 (19 max)
      === RTOS ===
      Static ram: 151340
      Dynamic ram: 113468 of which 0 recycled
      Never used RAM 80952, free system stack 200 words
      Tasks: NETWORK(ready,29.8%,211) ETHERNET(notifyWait,0.2%,558) ACCEL(notifyWait,0.0%,348) HEAT(notifyWait,0.0%,328) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,798) CanSender(notifyWait,0.0%,335) CanClock(delaying,0.0%,352) TMC(notifyWait,7.3%,90) MAIN(running,61.6%,953) IDLE(ready,1.1%,30), total 100.0%
      Owned mutexes:
      === Platform ===
      Last reset 00:00:11 ago, cause: software
      Last software reset at 2023-01-21 13:31, reason: StuckInSpinLoop, Gcodes spinning, available RAM 80196, slot 0
      Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0040080f BFAR 0x00000000 SP 0x2042025c Task TMC Freestk 98 ok
      Stack: 004914df 0043059a 41000000 39690453 40c38800 7b79718d 3f8dae65 00000000 42e80000 33c36300 3f859c60 de14b3bb 3f1d3074 ff0c52d6 42880303 38800000 42c80000 43fa0000 44fa0000 20000010 0043057b 00000001 20414f29 2041fe08 004307b9 20420075 2041fd8c
      Error status: 0x00
      Step timer max interval 133
      MCU temperature: min 40.5, current 40.6, max 41.4
      Supply voltage: min 23.8, current 23.8, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes
      12V rail voltage: min 12.3, current 12.4, max 12.4, under voltage events: 0
      Heap OK, handles allocated/used 99/90, heap memory allocated/used/recyclable 4096/3584/180, gc cycles 4
      Events: 4 queued, 4 completed
      Driver 0: standstill, SG min n/a, mspos 744, reads 61452, writes 14 timeouts 0
      Driver 1: standstill, SG min n/a, mspos 360, reads 61452, writes 14 timeouts 0
      Driver 2: standstill, SG min n/a, mspos 56, reads 61453, writes 14 timeouts 0
      Driver 3: standstill, SG min n/a, mspos 248, reads 61453, writes 14 timeouts 0
      Driver 4: standstill, SG min n/a, mspos 520, reads 61453, writes 14 timeouts 0
      Driver 5: standstill, SG min n/a, mspos 952, reads 61453, writes 14 timeouts 0
      Date/time: 2023-01-21 13:31:45
      Slowest loop: 5.50ms; fastest: 0.06ms
      === Storage ===
      Free file entries: 9
      SD card 0 detected, interface speed: 25.0MBytes/sec
      SD card longest read time 2.4ms, write time 0.0ms, max retries 0
      === Move ===
      DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
      no step interrupt scheduled
      === DDARing 0 ===
      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === DDARing 1 ===
      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === Heat ===
      Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
      === GCodes ===
      Movement locks held by null, null
      HTTP is idle in state(s) 0
      Telnet is idle in state(s) 0
      File is idle in state(s) 0
      USB is idle in state(s) 0
      Aux is idle in state(s) 0
      Trigger is idle in state(s) 0
      Queue is idle in state(s) 0
      LCD is idle in state(s) 0
      SBC is idle in state(s) 0
      Daemon is doing "G4 P500" in state(s) 0 0, running macro
      Aux2 is idle in state(s) 0
      Autopause is idle in state(s) 0
      File2 is idle in state(s) 0
      Queue2 is idle in state(s) 0
      Q0 segments left 0, axes/extruders owned 0x0000000
      Code queue 0 is empty
      Q1 segments left 0, axes/extruders owned 0x0000000
      Code queue 1 is empty
      === Filament sensors ===
      Extruder 0: no data received
      Extruder 1: no data received
      Extruder 2: no data received
      Extruder 3: no data received
      === CAN ===
      Messages queued 133, received 282, lost 0, boc 0
      Longest wait 1ms for reply type 6018, peak Tx sync delay 157, free buffers 50 (min 49), ts 56/55/0
      Tx timeouts 0,0,0,0,0,0
      === Network ===
      Slowest loop: 9.31ms; fastest: 0.03ms
      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
      HTTP sessions: 1 of 8
      = Ethernet =
      State: active
      Error counts: 0 0 0 0 0 0
      Socket states: 2 5 2 2 2 0 0 0
      = WiFi =
      Network state is disabled
      WiFi module is disabled
      Failed messages: pending 0, notready 0, noresp 0
      Socket states: 0 0 0 0 0 0 0 0
      === Multicast handler ===
      Responder is inactive, messages received 0, responses 0
      
      M122
      === Diagnostics ===
      RepRapFirmware for Duet 3 MB6HC version 3.5beta1+ (2023-01-20 09:47:33) running on Duet 3 MB6HC v1.02 or later (standalone mode)
      Board ID: 08DJM-9P63L-DJ3T0-6J1F4-3S06S-9A1V9
      Used output buffers: 3 of 40 (28 max)
      === RTOS ===
      Static ram: 151340
      Dynamic ram: 113468 of which 0 recycled
      Never used RAM 80952, free system stack 200 words
      Tasks: NETWORK(ready,28.3%,227) ETHERNET(notifyWait,0.2%,558) ACCEL(notifyWait,0.0%,348) HEAT(notifyWait,0.0%,322) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,773) CanSender(notifyWait,0.0%,335) CanClock(delaying,0.0%,352) TMC(notifyWait,7.2%,90) MAIN(running,62.9%,953) IDLE(ready,1.3%,30), total 100.0%
      Owned mutexes:
      === Platform ===
      Last reset 00:00:09 ago, cause: software
      Last software reset at 2023-01-21 13:31, reason: StuckInSpinLoop, Gcodes spinning, available RAM 80952, slot 1
      Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a80f BFAR 0x00000000 SP 0x20419664 Task IDLE Freestk 44 ok
      Stack: 004901dd 00490bb4 61000000 a5a5a5a5 004901dd a5a5a5a5 2041aea4 00007dfa 2041f370 20424e2c 2041967c 20424e24 00000004 20424ec8 20424ec8 2041967c 00000000 00000001 204196d8 4e49414d 00000000 00000000 00000001 00000001 00079777 00000000 00000000
      Error status: 0x00
      Step timer max interval 126
      MCU temperature: min 40.5, current 40.6, max 41.5
      Supply voltage: min 23.8, current 23.8, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes
      12V rail voltage: min 12.3, current 12.3, max 12.4, under voltage events: 0
      Heap OK, handles allocated/used 99/90, heap memory allocated/used/recyclable 4096/3884/480, gc cycles 3
      Events: 4 queued, 4 completed
      Driver 0: standstill, SG min n/a, mspos 744, reads 52669, writes 14 timeouts 0
      Driver 1: standstill, SG min n/a, mspos 360, reads 52669, writes 14 timeouts 0
      Driver 2: standstill, SG min n/a, mspos 56, reads 52669, writes 14 timeouts 0
      Driver 3: standstill, SG min n/a, mspos 248, reads 52669, writes 14 timeouts 0
      Driver 4: standstill, SG min n/a, mspos 520, reads 52670, writes 14 timeouts 0
      Driver 5: standstill, SG min n/a, mspos 952, reads 52670, writes 14 timeouts 0
      Date/time: 2023-01-21 13:32:16
      Slowest loop: 5.50ms; fastest: 0.06ms
      === Storage ===
      Free file entries: 9
      SD card 0 detected, interface speed: 25.0MBytes/sec
      SD card longest read time 2.5ms, write time 0.0ms, max retries 0
      === Move ===
      DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
      no step interrupt scheduled
      === DDARing 0 ===
      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === DDARing 1 ===
      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === Heat ===
      Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
      === GCodes ===
      Movement locks held by null, null
      HTTP is idle in state(s) 0
      Telnet is idle in state(s) 0
      File is idle in state(s) 0
      USB is idle in state(s) 0
      Aux is idle in state(s) 0
      Trigger is idle in state(s) 0
      Queue is idle in state(s) 0
      LCD is idle in state(s) 0
      SBC is idle in state(s) 0
      Daemon is doing "G4 P500" in state(s) 0 0, running macro
      Aux2 is idle in state(s) 0
      Autopause is idle in state(s) 0
      File2 is idle in state(s) 0
      Queue2 is idle in state(s) 0
      Q0 segments left 0, axes/extruders owned 0x0000000
      Code queue 0 is empty
      Q1 segments left 0, axes/extruders owned 0x0000000
      Code queue 1 is empty
      === Filament sensors ===
      Extruder 0: no data received
      Extruder 1: no data received
      Extruder 2: no data received
      Extruder 3: no data received
      === CAN ===
      Messages queued 119, received 252, lost 0, boc 0
      Longest wait 1ms for reply type 6018, peak Tx sync delay 174, free buffers 50 (min 49), ts 48/47/0
      Tx timeouts 0,0,0,0,0,0
      === Network ===
      Slowest loop: 7.19ms; fastest: 0.03ms
      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
      HTTP sessions: 1 of 8
      = Ethernet =
      State: active
      Error counts: 0 0 0 0 0 0
      Socket states: 5 2 2 2 2 0 0 0
      = WiFi =
      Network state is disabled
      WiFi module is disabled
      Failed messages: pending 0, notready 0, noresp 0
      Socket states: 0 0 0 0 0 0 0 0
      === Multicast handler ===
      Responder is inactive, messages received 0, responses 0
      
      M122
      === Diagnostics ===
      RepRapFirmware for Duet 3 MB6HC version 3.5beta1+ (2023-01-20 09:47:33) running on Duet 3 MB6HC v1.02 or later (standalone mode)
      Board ID: 08DJM-9P63L-DJ3T0-6J1F4-3S06S-9A1V9
      Used output buffers: 3 of 40 (28 max)
      === RTOS ===
      Static ram: 151340
      Dynamic ram: 113468 of which 0 recycled
      Never used RAM 80952, free system stack 200 words
      Tasks: NETWORK(ready,31.5%,244) ETHERNET(notifyWait,0.3%,558) ACCEL(notifyWait,0.0%,348) HEAT(notifyWait,0.0%,328) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,798) CanSender(notifyWait,0.0%,335) CanClock(delaying,0.0%,340) TMC(notifyWait,7.3%,90) MAIN(running,59.9%,953) IDLE(ready,0.9%,30), total 100.0%
      Owned mutexes:
      === Platform ===
      Last reset 00:00:13 ago, cause: software
      Last software reset at 2023-01-21 13:32, reason: StuckInSpinLoop, Gcodes spinning, available RAM 80024, slot 0
      Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a80f BFAR 0x00000000 SP 0x20419664 Task IDLE Freestk 44 ok
      Stack: 004901dd 00490bb8 61000000 a5a5a5a5 004901dd a5a5a5a5 2041aea4 00006c61 2041f370 20424e2c 2041967c 20424e24 00000004 20424ec8 20424ec8 2041967c 00000000 00000001 204196d8 4e49414d 00000000 00000000 00000001 00000001 003a0da3 00000000 00000000
      Error status: 0x00
      Step timer max interval 127
      MCU temperature: min 40.5, current 40.8, max 41.7
      Supply voltage: min 23.8, current 23.8, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes
      12V rail voltage: min 12.3, current 12.4, max 12.4, under voltage events: 0
      Heap OK, handles allocated/used 99/90, heap memory allocated/used/recyclable 4096/3932/528, gc cycles 4
      Events: 3 queued, 3 completed
      Driver 0: standstill, SG min n/a, mspos 744, reads 10492, writes 14 timeouts 0
      Driver 1: standstill, SG min n/a, mspos 360, reads 10492, writes 14 timeouts 0
      Driver 2: standstill, SG min n/a, mspos 56, reads 10493, writes 14 timeouts 0
      Driver 3: standstill, SG min n/a, mspos 248, reads 10493, writes 14 timeouts 0
      Driver 4: standstill, SG min n/a, mspos 520, reads 10493, writes 14 timeouts 0
      Driver 5: standstill, SG min n/a, mspos 952, reads 10493, writes 14 timeouts 0
      Date/time: 2023-01-21 13:33:21
      Slowest loop: 5.49ms; fastest: 0.06ms
      === Storage ===
      Free file entries: 9
      SD card 0 detected, interface speed: 25.0MBytes/sec
      SD card longest read time 2.4ms, write time 0.0ms, max retries 0
      === Move ===
      DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
      no step interrupt scheduled
      === DDARing 0 ===
      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === DDARing 1 ===
      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === Heat ===
      Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
      === GCodes ===
      Movement locks held by null, null
      HTTP is idle in state(s) 0
      Telnet is idle in state(s) 0
      File is idle in state(s) 0
      USB is idle in state(s) 0
      Aux is idle in state(s) 0
      Trigger is idle in state(s) 0
      Queue is idle in state(s) 0
      LCD is idle in state(s) 0
      SBC is idle in state(s) 0
      Daemon is doing "G4 P500" in state(s) 0 0, running macro
      Aux2 is idle in state(s) 0
      Autopause is idle in state(s) 0
      File2 is idle in state(s) 0
      Queue2 is idle in state(s) 0
      Q0 segments left 0, axes/extruders owned 0x0000000
      Code queue 0 is empty
      Q1 segments left 0, axes/extruders owned 0x0000000
      Code queue 1 is empty
      === Filament sensors ===
      Extruder 0: no data received
      Extruder 1: no data received
      Extruder 2: no data received
      Extruder 3: no data received
      === CAN ===
      Messages queued 156, received 335, lost 0, boc 0
      Longest wait 2ms for reply type 6048, peak Tx sync delay 401, free buffers 50 (min 49), ts 69/68/0
      Tx timeouts 0,0,0,0,0,0
      === Network ===
      Slowest loop: 7.44ms; fastest: 0.03ms
      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
      HTTP sessions: 1 of 8
      = Ethernet =
      State: active
      Error counts: 0 0 0 0 0 0
      Socket states: 5 2 2 2 2 0 0 0
      = WiFi =
      Network state is disabled
      WiFi module is disabled
      Failed messages: pending 0, notready 0, noresp 0
      Socket states: 0 0 0 0 0 0 0 0
      === Multicast handler ===
      Responder is inactive, messages received 0, responses 0
      
      M122
      === Diagnostics ===
      RepRapFirmware for Duet 3 MB6HC version 3.5beta1+ (2023-01-20 09:47:33) running on Duet 3 MB6HC v1.02 or later (standalone mode)
      Board ID: 08DJM-9P63L-DJ3T0-6J1F4-3S06S-9A1V9
      Used output buffers: 3 of 40 (21 max)
      === RTOS ===
      Static ram: 151340
      Dynamic ram: 113596 of which 0 recycled
      Never used RAM 80024, free system stack 202 words
      Tasks: NETWORK(ready,24.8%,244) ETHERNET(notifyWait,0.3%,558) ACCEL(notifyWait,0.0%,348) HEAT(notifyWait,0.0%,328) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,798) CanSender(notifyWait,0.0%,335) CanClock(delaying,0.0%,352) TMC(notifyWait,7.2%,90) MAIN(running,65.9%,953) IDLE(ready,1.8%,30), total 100.0%
      Owned mutexes:
      === Platform ===
      Last reset 00:00:06 ago, cause: software
      Last software reset at 2023-01-21 13:34, reason: StuckInSpinLoop, Gcodes spinning, available RAM 80952, slot 2
      Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a80f BFAR 0x00000000 SP 0x20419664 Task IDLE Freestk 44 ok
      Stack: 004901dd 00490bb8 61000000 a5a5a5a5 004901dd a5a5a5a5 2041aea4 00007dc0 2041f370 20424e2c 2041967c 20424e24 00000004 20424ec8 20424ec8 2041967c 00000000 00000001 204196d8 4e49414d 00000000 00000000 00000001 00000001 005554bf 00000000 00000000
      Error status: 0x00
      Step timer max interval 132
      MCU temperature: min 40.8, current 40.8, max 41.6
      Supply voltage: min 23.8, current 23.9, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes
      12V rail voltage: min 12.3, current 12.3, max 12.4, under voltage events: 0
      Heap OK, handles allocated/used 198/90, heap memory allocated/used/recyclable 4096/4016/612, gc cycles 2
      Events: 4 queued, 4 completed
      Driver 0: standstill, SG min n/a, mspos 744, reads 38237, writes 14 timeouts 0
      Driver 1: standstill, SG min n/a, mspos 360, reads 38237, writes 14 timeouts 0
      Driver 2: standstill, SG min n/a, mspos 56, reads 38237, writes 14 timeouts 0
      Driver 3: standstill, SG min n/a, mspos 248, reads 38237, writes 14 timeouts 0
      Driver 4: standstill, SG min n/a, mspos 520, reads 38238, writes 14 timeouts 0
      Driver 5: standstill, SG min n/a, mspos 952, reads 38238, writes 14 timeouts 0
      Date/time: 2023-01-21 13:34:27
      Slowest loop: 5.62ms; fastest: 0.06ms
      === Storage ===
      Free file entries: 9
      SD card 0 detected, interface speed: 25.0MBytes/sec
      SD card longest read time 2.4ms, write time 0.0ms, max retries 0
      === Move ===
      DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
      no step interrupt scheduled
      === DDARing 0 ===
      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === DDARing 1 ===
      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
      === Heat ===
      Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
      === GCodes ===
      Movement locks held by null, null
      HTTP is idle in state(s) 0
      Telnet is idle in state(s) 0
      File is idle in state(s) 0
      USB is idle in state(s) 0
      Aux is idle in state(s) 0
      Trigger is idle in state(s) 0
      Queue is idle in state(s) 0
      LCD is idle in state(s) 0
      SBC is idle in state(s) 0
      Daemon is doing "G4 P500" in state(s) 0 0, running macro
      Aux2 is idle in state(s) 0
      Autopause is idle in state(s) 0
      File2 is idle in state(s) 0
      Queue2 is idle in state(s) 0
      Q0 segments left 0, axes/extruders owned 0x0000000
      Code queue 0 is empty
      Q1 segments left 0, axes/extruders owned 0x0000000
      Code queue 1 is empty
      === Filament sensors ===
      Extruder 0: no data received
      Extruder 1: no data received
      Extruder 2: no data received
      Extruder 3: no data received
      === CAN ===
      Messages queued 95, received 195, lost 0, boc 0
      Longest wait 1ms for reply type 6018, peak Tx sync delay 62, free buffers 50 (min 49), ts 35/34/0
      Tx timeouts 0,0,0,0,0,0
      === Network ===
      Slowest loop: 9.56ms; fastest: 0.03ms
      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
      HTTP sessions: 1 of 8
      = Ethernet =
      State: active
      Error counts: 0 0 0 0 0 0
      Socket states: 5 2 2 2 2 0 0 0
      = WiFi =
      Network state is disabled
      WiFi module is disabled
      Failed messages: pending 0, notready 0, noresp 0
      Socket states: 0 0 0 0 0 0 0 0
      === Multicast handler ===
      Responder is inactive, messages received 0, responses 0
      
      1 Reply Last reply Reply Quote 0
      • Diamondbackundefined
        Diamondback
        last edited by Diamondback

        @dc42
        Ok, so here's the most minimalistic version I can create:

        daemon.g

        while global.daemonActive == true
        	set global.deactivateToolAfterFilamentChange = false
        
        	while iterations < #global.displayChar0
        		var lineIndex = iterations ;cache iterations value here since we have a 2D array and need this line counter later again
        		while iterations < #(global.displayChar0[var.lineIndex])
        			M150 R{global.RGBWhite[0]} U{global.RGBWhite[1]} B{global.RGBWhite[2]} P{global.displayChar0[var.lineIndex][iterations] > 0 ? global.displayDefaultBrightness : 0} S1 F1
        		
        	M150 R0 U0 B0 P0 S1 F0 ;announce last LED with a dummy
        	
        	G4 P500
        

        Most notably, if I remove the set global.deactivateToolAfterFilamentChange = false line, things work fine... However, that piece of code has been running for months just fine, this issue only started appearing with my use of LEDs and/or custom arrays.

        And the globals (these are created inside a macro that is called from config.g)

        if !exists(global.displayChar0)
        	global displayChar0 = {{0,1,1,1,1,1,1,0},{1,1,1,1,1,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,0}}
        	global displayChar1 = {{0,0,1,1,1,0,0,0},{0,0,1,1,1,1,0,0},{0,0,1,1,1,1,1,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0}}	
        	global displayChar2 = {{0,1,1,1,1,1,1,0},{1,1,1,1,1,1,1,1},{1,1,1,0,0,1,1,1},{0,1,1,1,0,0,0,0},{0,0,0,1,1,1,0,0},{0,0,0,0,0,1,1,1},{1,1,1,1,1,1,1,1},{1,1,1,1,1,1,1,1}}
        	global displayChar3 = {{0,1,1,1,1,1,1,1},{1,1,1,1,1,1,1,1},{1,1,1,0,0,0,0,0},{0,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,1},{1,1,1,0,0,0,0,0},{1,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,1}}
        	
        	global RGBRed = {255,0,0}
        	global RGBGreen = {0,255,0}
        	global RGBBlue = {0,0,255}
        	global RGBWhite = {255,255,255}
        

        All of the above code has been copied together from various macros, it's usually a lot more generic and this is just the smallest version of the overall stuff that I can produce.

        Here's another M122 from that minimal code:

        M122
        === Diagnostics ===
        RepRapFirmware for Duet 3 MB6HC version 3.5beta1+ (2023-01-20 09:47:33) running on Duet 3 MB6HC v1.02 or later (standalone mode)
        Board ID: 08DJM-9P63L-DJ3T0-6J1F4-3S06S-9A1V9
        Used output buffers: 3 of 40 (19 max)
        === RTOS ===
        Static ram: 151340
        Dynamic ram: 113436 of which 0 recycled
        Never used RAM 80984, free system stack 200 words
        Tasks: NETWORK(ready,27.2%,241) ETHERNET(notifyWait,0.2%,434) ACCEL(notifyWait,0.0%,348) HEAT(notifyWait,0.0%,342) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,798) CanSender(notifyWait,0.0%,335) CanClock(delaying,0.0%,352) TMC(notifyWait,7.1%,90) MAIN(running,64.5%,953) IDLE(ready,1.0%,30), total 100.0%
        Owned mutexes:
        === Platform ===
        Last reset 00:00:12 ago, cause: software
        Last software reset at 2023-01-21 14:42, reason: StuckInSpinLoop, Gcodes spinning, available RAM 80984, slot 2
        Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a80f BFAR 0x00000000 SP 0x20419664 Task IDLE Freestk 44 ok
        Stack: 004901dd 00490bb2 61000000 a5a5a5a5 004901dd a5a5a5a5 2041aea4 0003f273 20424e2c 2041f370 2041967c 20424e24 00000004 20424ec8 20424ec8 2041967c 00000000 00000001 204196d8 4e49414d 00000000 00000000 00000001 00000001 014858ad 00000000 00000000
        Error status: 0x00
        Step timer max interval 126
        MCU temperature: min 41.4, current 41.5, max 42.4
        Supply voltage: min 23.8, current 23.8, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes
        12V rail voltage: min 12.3, current 12.4, max 12.4, under voltage events: 0
        Heap OK, handles allocated/used 99/89, heap memory allocated/used/recyclable 4096/3548/156, gc cycles 1
        Events: 3 queued, 3 completed
        Driver 0: standstill, SG min n/a, mspos 744, reads 3000, writes 14 timeouts 0
        Driver 1: standstill, SG min n/a, mspos 360, reads 3000, writes 14 timeouts 0
        Driver 2: standstill, SG min n/a, mspos 56, reads 3000, writes 14 timeouts 0
        Driver 3: standstill, SG min n/a, mspos 248, reads 3000, writes 14 timeouts 0
        Driver 4: standstill, SG min n/a, mspos 520, reads 3001, writes 14 timeouts 0
        Driver 5: standstill, SG min n/a, mspos 952, reads 3001, writes 14 timeouts 0
        Date/time: 2023-01-21 14:43:16
        Slowest loop: 5.40ms; fastest: 0.06ms
        === Storage ===
        Free file entries: 10
        SD card 0 detected, interface speed: 25.0MBytes/sec
        SD card longest read time 2.4ms, write time 0.0ms, max retries 0
        === Move ===
        DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
        no step interrupt scheduled
        === DDARing 0 ===
        Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
        === DDARing 1 ===
        Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
        === Heat ===
        Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
        === GCodes ===
        Movement locks held by null, null
        HTTP is idle in state(s) 0
        Telnet is idle in state(s) 0
        File is idle in state(s) 0
        USB is idle in state(s) 0
        Aux is idle in state(s) 0
        Trigger is idle in state(s) 0
        Queue is idle in state(s) 0
        LCD is idle in state(s) 0
        SBC is idle in state(s) 0
        Daemon is idle in state(s) 0
        Aux2 is idle in state(s) 0
        Autopause is idle in state(s) 0
        File2 is idle in state(s) 0
        Queue2 is idle in state(s) 0
        Q0 segments left 0, axes/extruders owned 0x0000000
        Code queue 0 is empty
        Q1 segments left 0, axes/extruders owned 0x0000000
        Code queue 1 is empty
        === Filament sensors ===
        Extruder 0: no data received
        Extruder 1: no data received
        Extruder 2: no data received
        Extruder 3: no data received
        === CAN ===
        Messages queued 144, received 308, lost 0, boc 0
        Longest wait 1ms for reply type 6018, peak Tx sync delay 157, free buffers 50 (min 49), ts 62/61/0
        Tx timeouts 0,0,0,0,0,0
        === Network ===
        Slowest loop: 9.07ms; fastest: 0.03ms
        Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
        HTTP sessions: 1 of 8
        = Ethernet =
        State: active
        Error counts: 0 0 0 0 0 0
        Socket states: 5 2 2 2 2 0 0 0
        = WiFi =
        Network state is disabled
        WiFi module is disabled
        Failed messages: pending 0, notready 0, noresp 0
        Socket states: 0 0 0 0 0 0 0 0
        === Multicast handler ===
        Responder is inactive, messages received 0, responses 0
        
        1 Reply Last reply Reply Quote 0
        • Diamondbackundefined
          Diamondback
          last edited by Diamondback

          @dc42
          Hm, i think I might have created a macro that causes this all on its own without daemon.g ( I just call this macro as is without any params for this test)

          var brightness = global.displayDefaultBrightness
          if exists(param.B)
          	set var.brightness = param.B
          
          var activeLEDs = 0
          if exists(param.S)
          	set var.activeLEDs = floor(param.S * global.displayLEDCount)
          	
          var displayContent = "progress" ^ var.activeLEDs
          if global.lastDisplayContent != var.displayContent
          	set global.lastDisplayContent = var.displayContent
          	while iterations < global.displayLEDCount
          		;M150 R{param.C[0]} U{param.C[1]} B{param.C[2]} P{iterations < var.activeLEDs ? var.brightness : 0} S1 F1 ;3.5+
          		var isFrame = iterations < 8 || iterations > 55
          		var isProgress = false ;todo
          		var isActive = var.isFrame || var.isProgress
          		M150 R255 U0 B0 P{var.isActive ? var.brightness : 0} S1 F1
          
          	M150 R0 U0 B0 P0 S1 F0 ;announce last LED with a dummy
          

          This immediately makes the board crash every time, here's an M122 for this:

          M122
          === Diagnostics ===
          RepRapFirmware for Duet 3 MB6HC version 3.5beta1+ (2023-01-20 09:47:33) running on Duet 3 MB6HC v1.02 or later (standalone mode)
          Board ID: 08DJM-9P63L-DJ3T0-6J1F4-3S06S-9A1V9
          Used output buffers: 3 of 40 (22 max)
          === RTOS ===
          Static ram: 151340
          Dynamic ram: 113436 of which 0 recycled
          Never used RAM 80984, free system stack 200 words
          Tasks: NETWORK(ready,32.2%,221) ETHERNET(notifyWait,0.3%,432) ACCEL(notifyWait,0.0%,348) HEAT(notifyWait,0.0%,328) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,796) CanSender(notifyWait,0.0%,335) CanClock(delaying,0.0%,340) TMC(notifyWait,7.2%,90) MAIN(running,60.2%,953) IDLE(ready,0.2%,30), total 100.0%
          Owned mutexes:
          === Platform ===
          Last reset 00:01:09 ago, cause: software
          Last software reset at 2023-01-21 14:56, reason: StuckInSpinLoop, Gcodes spinning, available RAM 80920, slot 2
          Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a80f BFAR 0x00000000 SP 0x20419664 Task IDLE Freestk 44 ok
          Stack: 004901dd 00490bba 61000000 a5a5a5a5 004901dd a5a5a5a5 2041aea4 00021363 20424e2c 2041f370 2041967c 20424e24 00000004 20419100 20419100 2041967c 00000000 00000001 204196d8 4e49414d 00000000 00000000 00000001 00000001 02b69a1b 00000000 00000000
          Error status: 0x00
          Step timer max interval 139
          MCU temperature: min 41.1, current 41.3, max 42.3
          Supply voltage: min 23.8, current 23.9, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes
          12V rail voltage: min 12.3, current 12.4, max 12.4, under voltage events: 0
          Heap OK, handles allocated/used 99/89, heap memory allocated/used/recyclable 4096/3776/384, gc cycles 1
          Events: 4 queued, 4 completed
          Driver 0: standstill, SG min n/a, mspos 744, reads 61186, writes 14 timeouts 0
          Driver 1: standstill, SG min n/a, mspos 360, reads 61186, writes 14 timeouts 0
          Driver 2: standstill, SG min n/a, mspos 56, reads 61186, writes 14 timeouts 0
          Driver 3: standstill, SG min n/a, mspos 248, reads 61186, writes 14 timeouts 0
          Driver 4: standstill, SG min n/a, mspos 520, reads 61186, writes 14 timeouts 0
          Driver 5: standstill, SG min n/a, mspos 952, reads 61186, writes 14 timeouts 0
          Date/time: 2023-01-21 14:57:41
          Slowest loop: 5.51ms; fastest: 0.06ms
          === Storage ===
          Free file entries: 10
          SD card 0 detected, interface speed: 25.0MBytes/sec
          SD card longest read time 2.4ms, write time 0.0ms, max retries 0
          === Move ===
          DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
          no step interrupt scheduled
          === DDARing 0 ===
          Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
          === DDARing 1 ===
          Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
          === Heat ===
          Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
          === GCodes ===
          Movement locks held by null, null
          HTTP is idle in state(s) 0
          Telnet is idle in state(s) 0
          File is idle in state(s) 0
          USB is idle in state(s) 0
          Aux is idle in state(s) 0
          Trigger is idle in state(s) 0
          Queue is idle in state(s) 0
          LCD is idle in state(s) 0
          SBC is idle in state(s) 0
          Daemon is idle in state(s) 0
          Aux2 is idle in state(s) 0
          Autopause is idle in state(s) 0
          File2 is idle in state(s) 0
          Queue2 is idle in state(s) 0
          Q0 segments left 0, axes/extruders owned 0x0000000
          Code queue 0 is empty
          Q1 segments left 0, axes/extruders owned 0x0000000
          Code queue 1 is empty
          === Filament sensors ===
          Extruder 0: no data received
          Extruder 1: no data received
          Extruder 2: no data received
          Extruder 3: no data received
          === CAN ===
          Messages queued 657, received 1476, lost 0, boc 0
          Longest wait 1ms for reply type 6042, peak Tx sync delay 276, free buffers 50 (min 49), ts 347/346/0
          Tx timeouts 0,0,0,0,0,0
          === Network ===
          Slowest loop: 9.82ms; fastest: 0.03ms
          Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
          HTTP sessions: 1 of 8
          = Ethernet =
          State: active
          Error counts: 0 0 0 1 0 0
          Socket states: 5 2 2 2 2 0 0 0
          = WiFi =
          Network state is disabled
          WiFi module is disabled
          Failed messages: pending 0, notready 0, noresp 0
          Socket states: 0 0 0 0 0 0 0 0
          === Multicast handler ===
          Responder is inactive, messages received 0, responses 0
          
          dc42undefined 1 Reply Last reply Reply Quote 0
          • Diamondbackundefined
            Diamondback
            last edited by Diamondback

            @dc42
            It looks like this line is the culprit: var isActive = var.isFrame || var.isProgress, when I remove it (and directly use that expression below), it works fine...

            Disregard, now that line works fine, so probably some random component to it again...

            Diamondbackundefined 1 Reply Last reply Reply Quote 0
            • Diamondbackundefined
              Diamondback @Diamondback
              last edited by

              @dc42 Now I prevented it from crashing by moving a global set to a later place...

              if global.lastDisplayContent != var.displayContent
              	set global.lastDisplayContent = var.displayContent
              	while iterations < global.displayLEDCount
              		;M150 R{param.C[0]} U{param.C[1]} B{param.C[2]} P{iterations < var.activeLEDs ? var.brightness : 0} S1 F1 ;3.5+
              		var isFrame = iterations < 8 || iterations > 55
              		var isProgress = false ;todo
              		var isActive = var.isFrame || var.isProgress
              		M150 R255 U0 B0 P{var.isActive ? var.brightness : 0} S1 F1
               
              	M150 R0 U0 B0 P0 S1 F0 ;announce last LED with a dummy
              

              becomes:

              if global.lastDisplayContent != var.displayContent
              	while iterations < global.displayLEDCount
              		;M150 R{param.C[0]} U{param.C[1]} B{param.C[2]} P{iterations < var.activeLEDs ? var.brightness : 0} S1 F1 ;3.5+
              		var isFrame = iterations < 8 || iterations > 55
              		var isProgress = false ;todo
              		var isActive = var.isFrame || var.isProgress
              		M150 R255 U0 B0 P{var.isActive ? var.brightness : 0} S1 F1
               
              	M150 R0 U0 B0 P0 S1 F0 ;announce last LED with a dummy
                      set global.lastDisplayContent = var.displayContent
              

              Note how line #2 moved. This somewhat aligns with the crash in daemon.g where a global set also had critical impact on it...

              1 Reply Last reply Reply Quote 0
              • dc42undefined
                dc42 administrators @Diamondback
                last edited by

                @Diamondback what values do you set for the global variables before running this macro? I tried the following values, but it doesn't crash.

                global displayLEDCount=20
                global lastDisplayContent="none"
                global displayDefaultBrightness=10

                Duet WiFi hardware designer and firmware engineer
                Please do not ask me for Duet support via PM or email, use the forum
                http://www.escher3d.com, https://miscsolutions.wordpress.com

                Diamondbackundefined 1 Reply Last reply Reply Quote 0
                • Diamondbackundefined
                  Diamondback @dc42
                  last edited by

                  @dc42

                  global displayLEDCount = 64
                  global displayDefaultBrightness = 10
                  global lastDisplayContent = ""
                  

                  The more I play around with it, the more I think it's a timing issue... Sometimes I can do things fine by updating the 64 dotstar pixels with 500ms delay between them but not with 100ms etc.

                  dc42undefined 1 Reply Last reply Reply Quote 0
                  • dc42undefined
                    dc42 administrators @Diamondback
                    last edited by

                    @Diamondback said in 3.5b1 Reset reason: StuckInSpinLoop?:

                    global displayLEDCount = 64
                    global displayDefaultBrightness = 10
                    global lastDisplayContent = ""

                    It still doesn't crash for me. Perhaps it depends on what global variables you have created already? Can you share your whole config.g file and any macros that it calls?

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                    Diamondbackundefined 1 Reply Last reply Reply Quote 0
                    • Diamondbackundefined
                      Diamondback @dc42
                      last edited by

                      @dc42
                      config.g

                      ;M929 S3                                        ;enable debug logging
                      ;M575 P1 S1 B57600                              ;Enable PanelDue Port
                      G90                                             ; send absolute coordinates...
                      M83                                             ; ...but relative extruder moves
                      M550 P"V-Core Toolchanger"                      ; set printer name
                      
                      ; Enable network
                      M552 P0.0.0.0 S1
                      
                      M669 K1                                         ; select CoreXY mode
                      
                      G4 S2 ; wait for expansion boards to start
                      
                      ; Drives
                      ;XY1: back left
                      ;XY2: back right
                      M569 P0.2 S0                                      ; stepper XY1
                      M569 P0.3 S0                                      ; stepper XY2
                      M569 P0.4 S1                                      ; stepper Coupler
                      M569 P100.0 S0                                    ; stepper E0
                      M569 P100.1 S0                                    ; stepper E1
                      M569 P100.2 S0                                    ; stepper E2
                      M569 P100.3 S0                                    ; stepper E3
                      M569 P0.0 S0                                      ; stepper Z1
                      M569 P0.1 S0                                      ; stepper Z2
                      M569 P0.5 S0                                      ; stepper Z3
                      
                      M584 X0.3 Y0.2 C0.4                               ; set drive mapping (motion system X Y C)
                      M584 E100.0:100.1:100.2:100.3                     ; set drive mapping (extruders)
                      M584 Z0.0:0.1:0.5                                 ; set drive mapping (motion system Z)
                      ;Leadscrew order (starting back center, then clockwise):
                      ;1: back center
                      ;2: front right
                      ;3: front left
                      M671 X-12:216:-203 Y222:-179:-179 S30             ; set Z leadscrew positions
                      
                      
                      ; Axis Limits
                      if !exists(global.hasRunInit)
                      	global minY = -266
                      	global maxY = 115
                      
                      M208 X-148:160 Y{global.minY,global.maxY}       ; set axis minima & maxima
                      M208 C0:250 Z-2:270                             ; set axis minima & maxima
                      
                      M92 X80.00 Y80.00                               ; X/Y: 1.8°/step
                      ;M92 X160.00 Y160.00                            ; X/Y: 0.9°/step
                      M92 C200.00                                     ; C: E3D coupler
                      M92 Z800.00                                     ; Z: TR8x4 leadscrews
                      M350 X16 Y16 I1                                 ; configure microstepping with interpolation
                      M350 C16 Z16 I1                                 ; configure microstepping with interpolation
                      M566 X600 Y600 C2 Z50                           ; set maximum instantaneous speed changes (mm/min)
                      M203 X30000 Y30000 C10000 Z2000                 ; set maximum speeds (mm/min)
                      M201 X5000 Y5000 C500 Z350                      ; set accelerations (mm/s^2)
                      M204 P500 T5000
                      ;M204 P5000 T5000
                      
                      M906 X2000 Y2000                            ; set motor currents (mA) and motor idle factor in per cent
                      M906 C700                                    ; set motor currents (mA) and motor idle factor in per cent
                      M906 Z1500                                   ; set motor currents (mA) and motor idle factor in per cent
                      M906 E500:500:500:500                       ; set motor currents (mA) and motor idle factor in per cent (4x LGX)
                      M906 I50                                   ;only a single idle factor allowed for ALL steppers
                      M84 S30                                         ; Set idle timeout    
                      
                      ;=================== Extruder ======================
                      M92 E408:408:408:408                            ; set steps per mm 
                      M350 E16:16:16:16 I1                            ; configure microstepping 
                      M566 E500:500:500:500                           ; set maximum instantaneous speed changes (mm/min) ; used to be at 1200
                      M203 E15000:15000:15000:15000                   ; set maximum speeds (mm/min) 
                      M201 E3000:3000:3000:3000                       ; set accelerations (mm/s^2)
                      ;====================================================
                      
                      ; Endstops
                      M574 X2 S1 P"0.io0.in"                          ; configure active-high endstop for high end on X via pin xstop
                      M574 Y1 S1 P"0.io1.in"                          ; configure active-high endstop for high end on Y via pin ystop
                      M574 Z0                                         ; No Z-Endstop (use as probe instead)
                      
                      ; Z-Probe
                      if !exists(global.hasRunInit)
                      	global zProbeSpeedFeed = 300
                      	global zProbeSpeedFeedLevel = 1500
                      	global zProbeSpeedTravel = 20000
                      	global zProbeDiveHeightLevel = 30
                      	global zProbeDiveHeightMesh = 3
                      	global zProbePin = "0.io2.in"
                      	global zProbeType = 8
                      	global zProbeTriggerValue = 200
                      	global minXMesh = -146 
                      	global maxXMesh = 150
                      	global minYMesh = -150
                      	global maxYMesh = 150
                      	global meshPointSpacing = 30
                      
                      M558 K0 P{global.zProbeType} C{global.zProbePin} H{global.zProbeDiveHeightMesh} F{global.zProbeSpeedFeed} T{global.zProbeSpeedTravel}  ; Z Endstop/probe
                      M558 K2 P8 C"0.io4.in" H10 F100 T20000  ; tool length switch
                      
                      G31 K0 X0 Y0 Z0 P200 
                      ;G31 K1 X0 Y0 Z0 P200
                      G31 K2 X0 Y0 Z0 P200 
                      
                      ;G31 K0 X0 Y0 Z0 P{global.zProbeTriggerValue}                               ; set Z probe trigger value, offset and trigger height, offsets here are hardcoded in leveling macro as well
                      
                      M557 X{global.minXMesh, global.maxXMesh} Y{global.minYMesh, global.maxYMesh} S{global.meshPointSpacing}   ; define mesh grid
                      M376 H30                                        ; Set bed correction taper
                      
                      ; Heaters
                      M308 S0 P"100.temp0" Y"thermistor" T100000 B3950           ; configure sensor 0 as thermistor 
                      M950 H0 C"100.out0" T0 Q10                                 ; create bed heater output and map it to sensor 0
                      M143 H0 S121                                               ; set temperature limit for heater 0 to 121C
                      M307 H0 B0 R0.676 C345.1 D2.68 S1.00 V24.3                 ; Bed PID Tuning
                      M140 H0                                                    ; map heated bed to heater 0
                      
                      M308 S1 P"0.temp1" Y"thermistor" T100000 B4725 C7.06e-8    ; configure sensor 1 as thermistor
                      M950 H1 C"0.out1" T1                                       ; create nozzle heater output and map it to sensor 1
                      M143 H1 S301                                               ; set temperature limit for heater 1 to 301C
                      
                      M308 S2 P"0.temp2" Y"thermistor" T100000 B4725 C7.06e-8    ; configure sensor 2 as thermistor
                      M950 H2 C"0.out2" T2                                       ; create nozzle heater output and map it to sensor 2
                      M143 H2 S301                                               ; set temperature limit for heater 2 to 301C
                      
                      M308 S3 P"100.temp1" Y"thermistor" T100000 B4725 C7.06e-8  ; configure sensor 3 as thermistor
                      M950 H3 C"100.out1" T3                                     ; create nozzle heater output and map it to sensor 3
                      M143 H3 S301                                               ; set temperature limit for heater 3 to 301C
                      
                      M308 S4 P"100.temp2" Y"thermistor" T100000 B4725 C7.06e-8  ; configure sensor 2 as thermistor
                      M950 H4 C"100.out2" T4                                     ; create nozzle heater output and map it to sensor 2
                      M143 H4 S301                                               ; set temperature limit for heater 2 to 301C
                      
                      M302 S190 R190                                             ;Cold extrusion settings
                      
                      M307 H1 R4.637 K0.673:0.218 D2.31 E1.35 S1.00 B0 V24.2     ; PID Tuning T0
                      M307 H2 R4.174 K0.555:0.276 D1.96 E1.35 S1.00 B0 V24.2     ; PID Tuning T1
                      M307 H3 R4.301 K0.536:0.105 D1.89 E1.35 S1.00 B0 V24.2     ; PID Tuning T2
                      M307 H4 R3.780 K0.576:0.060 D1.57 E1.35 S1.00 B0 V24.2     ; PID Tuning T3
                      
                      ; Fans
                      M950 F0 C"0.out7"                                 ; Hotend Fan Tool 0
                      M106 P0 S255 L255 H1 T50 C"T0 Hotend"             ; Hotend Fan Tool 0
                      M950 F1 C"0.out4" Q50                             ; Layer Fan Tool 0
                      M106 P1 S0 H-1 C"T0"                              ; Layer Fan Tool 0
                      
                      M950 F2 C"0.out8"                                 ; Hotend Fan Tool 1
                      M106 P2 S255 L255 H2 T50 C"T1 Hotend"             ; Hotend Fan Tool 1
                      M950 F3 C"0.out5" Q50                             ; Layer Fan Tool 1
                      M106 P3 S0 H-1 C"T1"                              ; Layer Fan Tool 1
                      
                      M950 F4 C"100.out5"                               ; Hotend Fan Tool 2
                      M106 P4 S255 L255 H3 T50 C"T2 Hotend"             ; Hotend Fan Tool 2
                      M950 F5 C"100.out3" Q50                           ; Layer Fan Tool 2
                      M106 P5 S0 H-1 C"T2"                              ; Layer Fan Tool 2
                      
                      M950 F6 C"100.out6"                               ; Hotend Fan Tool 3
                      M106 P6 S255 L255 H4 T50 C"T3 Hotend"             ; Hotend Fan Tool 3
                      M950 F7 C"100.out4" Q50                           ; Layer Fan Tool 3
                      M106 P7 S0 H-1 C"T3"                              ; Layer Fan Tool 3
                      
                      ;Static layer fan
                      M950 F8 C"0.out0" Q65535                          ; static layer fan
                      M106 P8 S0 H-1 I1 L0.2 C"RSCS"
                      
                      ; Tools
                      M563 P0 D0 H1 F1                                 ; define tool 0
                      G10 P0 R0 S0                                     ; set initial tool 0 active and standby temperatures to 0C
                      
                      M563 P1 D1 H2 F3                                 ; define tool 1
                      G10 P1 R0 S0                                     ; set initial tool 1 active and standby temperatures to 0C
                      
                      M563 P2 D2 H3 F5                                 ; define tool 2
                      G10 P2 R0 S0                                     ; set initial tool 2 active and standby temperatures to 0C
                      
                      M563 P3 D3 H4 F7                                 ; define tool 3
                      G10 P3 R0 S0                                     ; set initial tool 3 active and standby temperatures to 0C
                      
                      M563 P4 S"Pen"                                   ; define tool 4 (Pen)
                      
                      ;Dock present switches
                      M950 J0 C"0.io7.in"                              ; Tool 0 Dock switch
                      M950 J1 C"0.io8.in"                              ; Tool 1 Dock switch
                      M950 J2 C"100.io5.in"                            ; Tool 2 Dock switch
                      M950 J3 C"100.io6.in"                            ; Tool 3 Dock switch
                      
                      ;additional tool related switches
                      M950 J4 C"0.io3.in"                             ;potential toolhead tool present switch, not installed atm, but already wired up inside the box
                      
                      ;Filament sensors, not installed atm, but already wired up inside the box
                      M591 D0 P4 C"100.io0.in" S1 L23.2 R70:150 E5
                      M591 D1 P4 C"100.io1.in" S1 L23.2 R70:150 E5
                      M591 D2 P4 C"100.io2.in" S1 L23.2 R70:150 E5
                      M591 D3 P4 C"100.io3.in" S1 L23.2 R70:150 E5
                      
                      M950 S0 C"0.out9" Q333                          ;PebbleWiper Servo
                      M280 P0 S70                                     ;Servo in idle position
                      M950 P1 C"0.io5.out"                            ;Light switch PWM
                      
                      ;Toolhead Dotstar
                      M150 X0
                      
                      ;Accelerometer
                      M955 P0 C"spi.cs2+spi.cs3"
                      
                      ;Inputshaping
                      ;M593 P"zvddd" F70 S0.2 
                      
                      ; Miscellaneous
                      M98 P"/macros/Misc/ToolheadDisplay/InitToolheadDisplay"
                      M98 P"/macros/Misc/Lights/On"
                      M98 P"/sys/config-tools.g"
                      
                      if !exists(global.hasRunInit)
                      	global pebbleFeedSpeedDefault = 300
                      	global pebbleFeedSpeed = global.pebbleFeedSpeedDefault	
                      	global deactivateToolAfterFilamentChange = false
                      	global displayActiveToolOnHead = true
                      	global hasRunInit = true
                      	global daemonActive = false
                      

                      InitToolheadDisplay

                      if !exists(global.displayLEDCount)
                      	global displayLEDCount = 64
                      	global displayDefaultBrightness = 10
                      	global lastDisplayContent = ""
                      	;global displayDigit = {null, null, null, null, null, null, null, null, null, null} ;enable once we can set individual elements of arrays
                      	;set global.displayDigit[0] = {{0,1,1,1,1,1,1,0},{1,1,1,1,1,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,0}}
                      	;set global.displayDigit[1] = {{0,0,1,1,1,0,0,0},{0,0,1,1,1,1,0,0},{0,0,1,1,1,1,1,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0}}
                      	;set global.displayDigit[2] = {{0,1,1,1,1,1,1,0},{1,1,1,1,1,1,1,1},{1,1,1,0,0,1,1,1},{0,1,1,1,0,0,0,0},{0,0,0,1,1,1,0,0},{0,0,0,0,0,1,1,1},{1,1,1,1,1,1,1,1},{1,1,1,1,1,1,1,1}}
                      	;set global.displayDigit[3] = {{0,1,1,1,1,1,1,1},{1,1,1,1,1,1,1,1},{1,1,1,0,0,0,0,0},{0,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,1},{1,1,1,0,0,0,0,0},{1,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,1}}
                      	
                      if !exists(global.displayChar0) && boards[0].firmwareVersion != "3.4.5"
                      	global displayChar0 = {{0,1,1,1,1,1,1,0},{1,1,1,1,1,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,0}}
                      	global displayChar1 = {{0,0,1,1,1,0,0,0},{0,0,1,1,1,1,0,0},{0,0,1,1,1,1,1,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0}}	
                      	global displayChar2 = {{0,1,1,1,1,1,1,0},{1,1,1,1,1,1,1,1},{1,1,1,0,0,1,1,1},{0,1,1,1,0,0,0,0},{0,0,0,1,1,1,0,0},{0,0,0,0,0,1,1,1},{1,1,1,1,1,1,1,1},{1,1,1,1,1,1,1,1}}
                      	global displayChar3 = {{0,1,1,1,1,1,1,1},{1,1,1,1,1,1,1,1},{1,1,1,0,0,0,0,0},{0,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,1},{1,1,1,0,0,0,0,0},{1,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,1}}
                      	
                      	global RGBOff = {0,0,0,0}
                      	global RGBRed = {255,0,0,25}
                      	global RGBGreen = {0,255,0,10}
                      	global RGBBlue = {0,0,255,45}
                      	global RGBWhite = {255,255,255,10}
                      

                      Lights/On

                      M42 P1 S230
                      

                      config-tools.g

                      if !exists(global.hasRunInit)
                      	;global toolNozzleSizes = {0,0,0,0}
                      	;global toolNozzleMaterials = {"brass","brass","brass","brass"}
                      	
                      	global tool0NozzleSize = "0.0"
                      	global tool1NozzleSize = "0.0"
                      	global tool2NozzleSize = "0.0"
                      	global tool3NozzleSize = "0.0"
                      	
                      	global tool0NozzleMaterial = ""
                      	global tool1NozzleMaterial = ""
                      	global tool2NozzleMaterial = ""
                      	global tool3NozzleMaterial = ""
                      
                      M98 P"/sys/config-tools-size.g"
                      M98 P"/sys/config-tools-material.g"
                      
                      
                      ;Z-Offset: 	If nozzle is too close to bed _reduce_ offset (negative number becomes more negative)
                      ;			If nozzle is too far away, _increase_ offset (negative number becomes less negative)
                      ;Tool offsets
                      G10 P0 X-8.340 Y39.270 Z-4.190
                      G10 P1 X-8.480 Y39.310 Z-4.020
                      G10 P2 X-8.180 Y38.930 Z-4.200
                      G10 P3 X-8.360 Y39.060 Z-4.506
                      
                      G10 P4 X0 Y46.5 Z-20.000                        ; set tool 4 axis offsets
                      
                      
                      
                      ;    Filament     Nozzle   PA    R-Distance   R-Speed  
                      ; -------------- -------- ----- ------------ --------- 
                      ;  Generic PETG     0.25   0.175        0.6      2100  
                      ;  ---               0.3   0.13         0.6      2100  
                      ;  ---               0.4   0.1          0.6      2100  
                      ;  ---               0.6   0.05         0.6      2100 
                      ;  ---               0.8   0.03         0.6      2100  
                      ;  Generic PLA      0.25   0.0          0.6      2100  
                      ;  ---               0.3   0.0          0.6      2100  
                      ;  ---               0.4   0.08         0.6      2100  
                      ;  ---               0.6   0.0          0.6      2100 
                      ;  ---               0.8   0.0          0.6      2100  
                      ;  BioFusion         0.25  0.0          0.6      2100  
                      ;  ---               0.3   0.09         0.6      2100  
                      ;  ---               0.4   0.07         0.6      2100  
                      ;  ---               0.6   0.0          0.6      2100 
                      ;  ---               0.8   0.035        0.6      2100  
                      ;  PA-CF             0.3   0.0          0.6      2100  
                      ;  ---               0.4   0.0          0.6      2100  
                      ;  PC-CF             0.3   0.0          0.6      2100  
                      ;  ---               0.4   0.0          0.6      2100  
                      ;  PA12              0.25  0.0          0.6      2100  
                      ;  ---               0.3   0.0          0.6      2100  
                      ;  ---               0.4   0.13         0.6      2100  
                      ;  ---               0.6   0.0          0.6      2100 
                      ;  ---               0.8   0.0          0.6      2100  
                      ;  Wood              0.8   0.04         0.6      2100
                      ;  TPU               0.4   0.0          1.0      2100
                      
                      
                      ;https://ozh.github.io/ascii-tables/
                      

                      config-tools-size.g

                      set global.tool0NozzleSize = "0.4"
                      set global.tool1NozzleSize = "0.4"
                      set global.tool2NozzleSize = "0.4"
                      set global.tool3NozzleSize = "0.6"
                      

                      config-tools-material.g

                      set global.tool0NozzleMaterial = "brass"
                      set global.tool1NozzleMaterial = "brass"
                      set global.tool2NozzleMaterial = "brass"
                      set global.tool3NozzleMaterial = "nozzlex"
                      ;set global.toolNozzleMaterials = {"brass","brass","brass","nozzlex"}
                      
                      dc42undefined 1 Reply Last reply Reply Quote 0
                      • dc42undefined
                        dc42 administrators @Diamondback
                        last edited by

                        @Diamondback thanks.

                        I still couldn't make it crash with your files, but I eventually got a crash with a similar M122 report to yours after running this macro several times:

                        var activeLEDs=10
                        while iterations < 1000
                        	var displayContent = "progress" ^ var.activeLEDs
                        	set global.lastDisplayContent = var.displayContent
                        echo "Done"
                        

                        Duet WiFi hardware designer and firmware engineer
                        Please do not ask me for Duet support via PM or email, use the forum
                        http://www.escher3d.com, https://miscsolutions.wordpress.com

                        Diamondbackundefined 1 Reply Last reply Reply Quote 1
                        • Diamondbackundefined
                          Diamondback @dc42
                          last edited by

                          @dc42 Yea it seems quite random what exactly triggers it, the only things in common for me seem to be some of interaction with custom variables/arrays and possibly the dotstar LEDs, ofc, either one could be a coincidence...

                          dc42undefined 1 Reply Last reply Reply Quote 0
                          • dc42undefined
                            dc42 administrators @Diamondback
                            last edited by

                            @Diamondback I suspect it's an interaction between DWC polling the object model (which involves reading some values from the heap) and garbage collection of the heap taking place because string or array variables are being reassigned.

                            Duet WiFi hardware designer and firmware engineer
                            Please do not ask me for Duet support via PM or email, use the forum
                            http://www.escher3d.com, https://miscsolutions.wordpress.com

                            Diamondbackundefined 1 Reply Last reply Reply Quote 0
                            • Diamondbackundefined
                              Diamondback @dc42
                              last edited by

                              @dc42 I played around with the DWC polling time this morning but didn't get any immediate results, I'll play around with it some more and see if I can maybe make it go away by setting it much higher?

                              dc42undefined 1 Reply Last reply Reply Quote 0
                              • dc42undefined
                                dc42 administrators @Diamondback
                                last edited by

                                @Diamondback my next step will be to disconnect DWC completely and then see if I can provoke the reset by sending the command to run the macro over USB.

                                Duet WiFi hardware designer and firmware engineer
                                Please do not ask me for Duet support via PM or email, use the forum
                                http://www.escher3d.com, https://miscsolutions.wordpress.com

                                Diamondbackundefined dc42undefined 2 Replies Last reply Reply Quote 0
                                • Diamondbackundefined
                                  Diamondback @dc42
                                  last edited by

                                  @dc42 Hm, I guess I can try the same by having the issue triggered by daemon.g and not having any browser connected to it? Or does DWC still do stuff in the background then somehow?

                                  dc42undefined 1 Reply Last reply Reply Quote 0
                                  • dc42undefined
                                    dc42 administrators @dc42
                                    last edited by

                                    Confirmed, if I send the command over USB with DWC not connected, it doesn't reset. If I connect DWC and send the command over USB, it resets.

                                    Duet WiFi hardware designer and firmware engineer
                                    Please do not ask me for Duet support via PM or email, use the forum
                                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                                    1 Reply Last reply Reply Quote 1
                                    • dc42undefined
                                      dc42 administrators @Diamondback
                                      last edited by

                                      @Diamondback please try the firmware at https://www.dropbox.com/sh/z9f9v517t9txqh9/AACG2Dycr_EghlN4p1HsYVUNa?dl=0. It fixes the case that I was able to reproduce. The change is quite extensive, so please use it with caution.

                                      Duet WiFi hardware designer and firmware engineer
                                      Please do not ask me for Duet support via PM or email, use the forum
                                      http://www.escher3d.com, https://miscsolutions.wordpress.com

                                      Diamondbackundefined 1 Reply Last reply Reply Quote 1
                                      • Diamondbackundefined
                                        Diamondback @dc42
                                        last edited by

                                        @dc42 Will do! 🙂 This includes the previous array memory leak fix?

                                        dc42undefined 1 Reply Last reply Reply Quote 0
                                        • dc42undefined
                                          dc42 administrators @Diamondback
                                          last edited by

                                          @Diamondback yes it does. If you get any resets, please post a subsequent M122 report.

                                          Duet WiFi hardware designer and firmware engineer
                                          Please do not ask me for Duet support via PM or email, use the forum
                                          http://www.escher3d.com, https://miscsolutions.wordpress.com

                                          Diamondbackundefined 3 Replies Last reply Reply Quote 1
                                          • Diamondbackundefined
                                            Diamondback @dc42
                                            last edited by

                                            @dc42 Looking promising so far, no more resets atm. 🙂
                                            I also yesterday played around more with the DWC polling frequency between 50ms and 60s and as you assumed, with lower values it was happening much quicker.

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