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    Y Axis behaving strangely

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    Duet Hardware and wiring
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    • dataknifeundefined
      dataknife
      last edited by

      I have a problem with my new Duet Wifi- I can home the Y Axis, but if I try any manual movement, the axis doesn't move (or barely moves.)

      Here's a YouTube video of what's happening.

      I tried M906 and M913 to make sure that the motor was receiving enough current, and it is matching the configured values.

      I thought that the motor is somehow toast, but that doesn't seem consistent with the Homing behavior.

      Any ideas?

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      • dc42undefined
        dc42 administrators
        last edited by

        Please post your config.g, homey.g and homeall.g files.

        Duet WiFi hardware designer and firmware engineer
        Please do not ask me for Duet support via PM or email, use the forum
        http://www.escher3d.com, https://miscsolutions.wordpress.com

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        • dataknifeundefined
          dataknife
          last edited by

          Here you go-

          homey.g

          homeall.g

          config.g

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          • Phaedruxundefined
            Phaedrux Moderator
            last edited by

            Are you sure that you have your 0,0 origin set to the front left corner?

            You may need to verify the direction of your motors.

            https://duet3d.dozuki.com/Wiki/ConfiguringRepRapFirmwareCartesianPrinter#Section_Movement_section

            Also, you should remove the G92 Z0 command form your home all if you are using a Z probe and G30 to home Z.

            Are you temporarily using an endstop switch for Z?

            What firmware version are you using? I see you have a BLTouch, but you are using P5 as the probe type. Newer firmware versions have a dedicated probe type for the BLTouch. P9.

            https://duet3d.dozuki.com/Wiki/Connecting_a_Z_probe#Section_BLTouch
            https://duet3d.dozuki.com/Wiki/BLTouch_Troubleshooting

            Z-Bot CoreXY Build | Thingiverse Profile

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            • dc42undefined
              dc42 administrators
              last edited by

              I didn't spot anything wrong with your config. From the noise that the stepper motor is making, I think you have the acceleration or movement speed set too high and the motor can't keep up because of the mass of the bed. Try reducing the Y acceleration in the M201 command in config.g, or the Y maximum speed in the M203 command in config.g.

              Duet WiFi hardware designer and firmware engineer
              Please do not ask me for Duet support via PM or email, use the forum
              http://www.escher3d.com, https://miscsolutions.wordpress.com

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