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    print to travel moves, no jerk

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    travel move print move jerk firmware 2.01 pause
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    • dc42undefined
      dc42 administrators
      last edited by

      Are you using pressure advance? If not then i suggest you enable it.

      Duet WiFi hardware designer and firmware engineer
      Please do not ask me for Duet support via PM or email, use the forum
      http://www.escher3d.com, https://miscsolutions.wordpress.com

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      • imqqmiundefined
        imqqmi
        last edited by

        Thanks, I wasn't aware of that option. I'll try this in config.g:
        M572 D0 S0.2

        The bowden tube is about 600mm.

        dc42undefined 1 Reply Last reply Reply Quote 0
        • dc42undefined
          dc42 administrators @imqqmi
          last edited by

          @imqqmi said in print to travel moves, no jerk:

          Thanks, I wasn't aware of that option. I'll try this in config.g:
          M572 D0 S0.2

          The bowden tube is about 600mm.

          You may need to use a higher value then, possibly 0.3 or 0.4. There is a thread on pressure advance calibration. You may need to reduce the retraction distance, to avoid over-retracting at the ends of fast printing moves.

          Duet WiFi hardware designer and firmware engineer
          Please do not ask me for Duet support via PM or email, use the forum
          http://www.escher3d.com, https://miscsolutions.wordpress.com

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          • imqqmiundefined
            imqqmi
            last edited by imqqmi

            Thanks! Before your last comment I printed four test prints as shown below. Clearly the top and bottom is a big difference but at 1.6 the printer is slowing down as if a low acceleration is set. The extrusion stepper motor is doing some wacky back and forth motion on the infill too, though I must say the infill looked fine.
            I'll try reducing retraction distance tomorrow. (please ignore the bent prints, I've pried them off while the bed was still fully heated, it didn't warp during print.)

            0_1542739240717_PressureAdvance.jpg

            Marlin 1.1.9 seems better controlled, yet doesn't use pressure advance:
            0_1542739594662_marlin.jpg

            T3P3Tonyundefined 1 Reply Last reply Reply Quote 0
            • T3P3Tonyundefined
              T3P3Tony administrators @imqqmi
              last edited by

              @imqqmi are you using the same gcode for marlin? Also its worth looking at tuning pressure advance:
              https://forum.duet3d.com/topic/6698/pressure-advance-calibration

              www.duet3d.com

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              • imqqmiundefined
                imqqmi
                last edited by

                Thanks for the link, I'll check it out. It's not the exact same gcode but the same settings as with the test print. I didn't do any test prints on marlin 1.1.9, only actual prints of things I needed like an extruder holder for the e3d v6 (which is what the last image is of).

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                • imqqmiundefined
                  imqqmi
                  last edited by

                  Here's the pressure advance calibration test with the settings K=0.4 to 2.0. 2.0 isn't high enough, so next test print will be 2.0 to 6.0. Is my bowden setup that bad? Maybe the teflon tube is a bit too wide?
                  0_1542798668383_IMG_20181121_120000063a.jpg

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                  • dc42undefined
                    dc42 administrators
                    last edited by

                    2.0 would be a very high value for pressure advance. Using a Bowden tube that has too large an ID for the filament might account for it. Does the filament seem a loose fit in it?

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

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                    • imqqmiundefined
                      imqqmi
                      last edited by

                      Here's the same test with setting k= 2 to 6. The third layer looked good to me, which corresponds to k=2.24. I have this set in the config.g file now.

                      0_1542800757209_IMG_20181121_124324078a.jpg

                      I've reprinted the 20x20x2 slab. To the left is the 2.24 newly printed, and compared with the 0.2 one printed earlier. A clear improvement and the blob on the top is almost gone. Instead there's now a hole, probably due to the pressure not being able to come back up quickly enough. The infill cornering is improved as well, I can now set the infill/perimeter overlap higher to fix this. There's a print speed penalty though as the acceleration is now adjusted to the speed/acceleration the extruder can handle. I will tune that further first and see how it will perform. I did notice that the infill looked different, in the center it seems wider and flatter and near the perimeter it's narrower and rounder. Coming into the corner looks different than coming out of the corner. The left one looks more consistent apart from the blobs at the end of each infill cornering.
                      0_1542802284584_PressureAdvance2.24vs0.2.jpg

                      I've looked in my failed prints bin and found a couple of marlin 1.1.9 prints, but I'm not sure what settings and what stage of calibration it was. I had to calibrate motor current at some point, not sure if it was before or after motor calibration. My guess is the left one is pre motor calibration and the right one post motor calibration looking at the extrusion line spacing, left is irregular and right is more regular. I don't know if jerk was changed either. At least I've gotten rid of the corner blob that is still present in the print below.
                      0_1542802671815_Marlin1.1.9.jpg

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                      • dc42undefined
                        dc42 administrators
                        last edited by

                        You can avoid the speed penalty if you can increase the extruder jerk limit in the M566 command without the extruder skipping steps. However, I've never heard of anyone needing pressure advance greater than 1 before, so I think there is far too much elasticity in your Bowden extrusion system. What is the inside diameter of the Bowden tube? If you are using push-fit connectors on the ends of it, does the Bowden tube move at all relative to the connectors when the extruder reverses direction?

                        Duet WiFi hardware designer and firmware engineer
                        Please do not ask me for Duet support via PM or email, use the forum
                        http://www.escher3d.com, https://miscsolutions.wordpress.com

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                        • imqqmiundefined
                          imqqmi
                          last edited by

                          I've increased acceleration, velocity and jerk (slightly) but it doesn't seem to improve much. The left most seems to be the best. At the top you can see the outer perimeter near the hole isn't as thin as the other two. I'll try bumping up jerk as you suggest, its at 600mm/min, I'll try 2400mm/min.
                          0_1542809238852_DuetAP2.24_Acc2000-4000_Vel2700-4800.jpg

                          The bowden tube diameter is about 3.1 to 3.2mm when I scan a cross section and measure it in photoshop. With the calipers it's between 3 and 3.1mm. The ABS filament is about 2.85 to 2.90mm (brand: RRW Dutch ABS).

                          The push fit connectors don't show any motion. I use 3d printed clips to secure it in place. There's a bit of wiggle room between the extruder gears though. I've attempted to tighten them but ended up with skipping steps. That was before the duet upgrade so I could try it again. The drivers provide much more power to the stepper motors.

                          Bowden connector on the x carriage:
                          0_1542810317190_IMG_20181121_151954525_HDRa.jpg

                          Bowden connector on the extruder side, there's no play in the tube nor any movement when printing/retracting un retracting:
                          0_1542810322126_IMG_20181121_151945789a.jpg

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                          • imqqmiundefined
                            imqqmi
                            last edited by imqqmi

                            I've adjusted jerk to 1000mm/s from 600mm/s and started skipping steps. I upped the motor current to 1800mA (was 800mA) and stopped skipping steps. It makes a heck of a racket when doing infill. And the gap is still there unfortunately. But the speed is about the same now as without pressure advance.

                            I'll try doing the pressure advance calibration again since the backlash may have changed since tightening the gears, there's no play in them now.

                            0_1542812476783_E0Jerk1000_MotI1800mA.jpg

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                            • imqqmiundefined
                              imqqmi
                              last edited by

                              No change or improvement in the pressure advance department unfortunately. The same k value is indicated.

                              I've tried a bigger print. The infill makes the extruder go back and forth with quite a bit of noise, clacking back and forth.

                              I'm not sure this is the way to go for me at least. Does the noise improve at lower k values? It wears the filament down too, with the PA calibration the extruder lost grip on the filament. Luckily it was near the end of the print but it wouldn't be good for other long prints to fail half way.

                              I may try an older firmware to see if the travel/extrusion move jerk is back on how it performs.

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                              • dc42undefined
                                dc42 administrators
                                last edited by dc42

                                I've never used 2.85mm filament, so I don't have a feel for the amount of pressure advance that a 2.85mm Bowden extruder needs. From a physics point of view, 2.85mm will be affected by a factor of 2.65 times more than 1.75mm filament. Although the filament itself will be less compressible because it is thicker, in practice most of the compressibility comes from the slop of the filament in the Bowden tube. When compressed, the filament adopts a helical path in the Bowden tube, and the more force is applies, the shorter the pitch of the helix.

                                I suspect that you have 1/8" ID PTFE tubing. If that is the case, then 3mm ID tubing would be better if you can find it, because it would have around half the amount of slop.

                                Notwithstanding the above, I can see that there may be some point in allowing large amounts of extruder jerk at the start and end of very short travel moves, as Marlin appears to do. I suspect that like some other firmwares, Marlin was ignoring extruder jerk completely until very recently, when implementing pressure advance forced them to consider it.

                                Duet WiFi hardware designer and firmware engineer
                                Please do not ask me for Duet support via PM or email, use the forum
                                http://www.escher3d.com, https://miscsolutions.wordpress.com

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                                • imqqmiundefined
                                  imqqmi
                                  last edited by

                                  Thank you David, hopefully allowing high jerk for travel moves will resolve the issue.

                                  I'll try and source a 3mm bowden tube. In the mean time I'll turn off the pressure advance feature for now. I just printed a floppy cleaning kit someone asked for but the filament lost traction for about 10 layers before picking it up again due to the extreme back and forth motion of the extruder motor, especially with narrow infills like 2-5mm wide.

                                  Especially the turn tool got out with under extruded layers, it was easy to snap them in two parts. I've reprinted it without PA and came out fine.
                                  0_1543075306472__MG_9561.jpg

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