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    Duet Maestro Short to Ground

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    • Nemesisundefined
      Nemesis @infamous_panda
      last edited by

      @infamous_panda Not sure on the Duet Maestro. However I have two DuetWifi's and I love them! Have little to no issue with them and the documentation and support is awesome!

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      • dc42undefined
        dc42 administrators
        last edited by

        The issue of spurious short-to-ground reports from the drivers when using them in stealthChop mode was resolved many weeks ago, in the 2.01 firmware release AFAIR. The reports are a known feature of the Trinamic drivers at high speeds, and the fix is to have them switch to spreadCycle mode above a certain speed. We've made the speed at which it does this configurable.

        Duet WiFi hardware designer and firmware engineer
        Please do not ask me for Duet support via PM or email, use the forum
        http://www.escher3d.com, https://miscsolutions.wordpress.com

        infamous_pandaundefined 1 Reply Last reply Reply Quote 2
        • infamous_pandaundefined
          infamous_panda @dc42
          last edited by

          @dc42 That's good news. By "configurable" do you mean that this is something you expect will have different speeds for different setups? How would one go about determining this value?

          aidarundefined dc42undefined 2 Replies Last reply Reply Quote 0
          • aidarundefined
            aidar @infamous_panda
            last edited by

            @infamous_panda said in Duet Maestro Short to Ground:

            @dc42 That's good news. By "configurable" do you mean that this is something you expect will have different speeds for different setups? How would one go about determining this value?

            Hi. There - https://duet3d.dozuki.com/Wiki/Gcode#Section_M569_Set_motor_driver_direction_enable_polarity_and_step_pulse_timing

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            • dc42undefined
              dc42 administrators @infamous_panda
              last edited by dc42

              @infamous_panda said in Duet Maestro Short to Ground:

              @dc42 That's good news. By "configurable" do you mean that this is something you expect will have different speeds for different setups? How would one go about determining this value?

              The firmware default is to switch at a very low speed, so that the drivers are in stealthChop at idle but switch to spreadCycle even at quite slow speeds. If this is too noisy, you can increase the threshold so that it changes over above your usual print speed but probably below your maximum travel speed. There is a slight jerk at changeover (this is a feature of the driver chip), so it's probably best to avoid the changeover happening during printing moves.

              Duet WiFi hardware designer and firmware engineer
              Please do not ask me for Duet support via PM or email, use the forum
              http://www.escher3d.com, https://miscsolutions.wordpress.com

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              • infamous_pandaundefined
                infamous_panda
                last edited by

                Almost ready to dive back in. Question:

                So previously when the short to ground error occurred. The board/software would turn off that motor/axis, but the others would continue to run indefinately. As you can imagine this can be catastrophic especially on a delta printer. Is it now possible to have a setting to stop or pause the print should this error occur?

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                • dc42undefined
                  dc42 administrators
                  last edited by

                  That's a good point, However, short-to-ground reports are rare, now that we've sorted out the issue with TMC2224 drivers giving false short-to-ground reports.

                  Duet WiFi hardware designer and firmware engineer
                  Please do not ask me for Duet support via PM or email, use the forum
                  http://www.escher3d.com, https://miscsolutions.wordpress.com

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                  • infamous_pandaundefined
                    infamous_panda
                    last edited by

                    Is this functionality something that would be non trivial to implement?

                    The biggest pain point when I was trying to diagnose this issue, was that I would have to watch and wait so I could shut down the printer as soon as it occurred or risk damage. This could be anywhere from 1 minute or well over an hour into a job.

                    So the the issue is mostly mitigated but as you say there is an element of experimentation in balancing speed and noise to for each printer setup. Without some range of values on when stealth-chop is known to fail I don't think I could leave the ever leave the printer alone.

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                    • dc42undefined
                      dc42 administrators
                      last edited by

                      It's not exactly trivial, but I will add it to the firmware work list. Pausing the print would not make sense in this situation, it would be necessary to stop the print and leave the print head exactly where it is.

                      Duet WiFi hardware designer and firmware engineer
                      Please do not ask me for Duet support via PM or email, use the forum
                      http://www.escher3d.com, https://miscsolutions.wordpress.com

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                      • infamous_pandaundefined
                        infamous_panda
                        last edited by

                        Bit the bullet a week back and have gotten through maybe 10 hours of successful printing without the short to ground issue.

                        Not going to mess around with Stealthchop/Spreadcycle for now since the machine runs quiet enough.

                        Having some other trouble which I'll start a new thread over.

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