Can't run homex.g with M98
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I am trying to run homex.g via M98 and it seems to produce the following error:
12:00:39 AM
M98 P"homex.g"
Error: G0/G1: insufficient axes homedThe contents of the file are
; X axis homing file for dc42 Duet firmware
G91
G1 Z4 F200 S2
G1 X-280 F3000 S1
G1 X4 F600
G1 X-10 S1
G1 Z-4 F200
G90I can run the contents myself with no issues at all. It is only when I try to invoke with M98 does this issue arise.
Here is my config.g:
; Configuration file for My Printer
; Communication and general
M111 S0 ; Debug off
M550 PRailCore ; Machine name and Netbios name (can be anything you like)
;M551 Pmyrap ; Machine password (used for FTP)
;*** If you have more than one Duet on your network, they must all have different MAC addresses, so change the last digits
M540 P0xBE:0xEF:0xDE:0xAD:0xFE:0xEE ; MAC Address
;*** Wifi Networking
M552 S1 ; Enable WiFi
M555 P2 ; Set output to look like Marlin
M575 P1 B57600 S1 ; Comms parameters for PanelDueG21 ; Work in millimetres
G90 ; Send absolute coordinates...
M83 ; ...but relative extruder moves; Axis and motor configuration
M669 K1 ; CoreXY modeM584 X0 Y1 Z5:6:7 E3:4:8:9 ; Map Z to drivers 5, 6, 7. Define unused drivers 3,4,8 and 9 as extruders
M569 P0 S1 ; Drive 0 goes forwards (change to S0 to reverse it) X stepper (Rear)
M569 P1 S0 ; Drive 1 goes backwards Y Stepper (Front)
M569 P2 S1 ; Drive 2 goes forwards Unused
M569 P3 S1 ; Drive 3 goes forwards Extruder
M569 P4 S1 ; Drive 4 goes forwards Extruder (unused)
M569 P5 S0 ; Drive 5 goes backwards Front Left Z
M569 P6 S0 ; Drive 6 goes backwards Rear Left Z
M569 P7 S1 ; Drive 7 goes backwards Right Z;Leadscrew locations
M671 X-10:-10:344 Y21:275:146 S7.5 ;Front left, Rear Left, Right S7.5 is the max correction - measure your own offsets, to the bolt for the yoke of each leadscrewM350 X16 Y16 Z16 E16 I1 ; set 16x microstepping for axes& extruder, with interpolation
M574 X1 Y1 Z0 S1 ; set homing switch configuration (x,y at min, z at max) IF YOU NEED TO REVERSE YOUR HOMING SWITCHES CHANGE S1 to S0
M906 X1400 Y1400 Z1000 E1250 I60 ; Set motor currents (mA)
M201 X2500 Y2500 Z80 E1500 ; Accelerations (mm/s^2)
M203 X24000 Y24000 Z900 E3600 ; Maximum speeds (mm/min)
M566 X1000 Y1000 Z80 E1500 ; Maximum jerk speeds mm/minute
M208 X295 Y300 Z330 ; set axis maxima and high homing switch positions (adjust to suit your machine)
M208 X0 Y0 Z-0.5 S1 ; set axis minima and low homing switch positions (adjust to make X=0 and Y=0 the edges of the bed)
M92 X200 Y200 Z1600 E837 ; steps/mm; Thermistors
M305 P0 T100000 B4240 R4700 H0 L0 ; Put your own H and/or L values here to set the bed thermistor ADC correction
M305 P1 T100000 B4725 R4700 H0 L0 C7.06e-8 ; Put your own H and/or L values here to set the first nozzle thermistor ADC correction
M305 P105 S"Keenovo" X5 T100000 B3950 R4700M307 H0 A276.1 C816.1 D11.9 S1.00 V24.3 B0 ; Bed Heaters
M307 H1 A430.0 C241.4 D3.7 S1.00 V24.3 B0 ;Heater 1 model
M570 S360 ; Hot end may be a little slow to heat up so allow it 180 seconds
M143 S285; Fans
M106 P0 H-1 ; disable thermostatic mode for fan 0
M106 P1 T45 H1 ; enable thermostatic mode for fan 1
M106 P2 H-1
M106 P0 S0 ; turn off fans
M106 P2 S0; Tool definitions
M563 P0 D0 H1 ; Define tool 0
G10 P0 S0 R0 ; Set tool 0 operating and standby temperatures;BLTouch - comment out the following 3 lines if using a IR Probe
M307 H3 A-1 C-1 D-1
M558 P9 X0 Y0 Z1 H5 F50 T6000 A5 S0.02
G31 X2.3 Y41.6 Z2.73 P25 ; Customize your offsets appropriately - do a paper test, and put the probed value in the Z value hereM208 S1 Z-0.2 ; set minimum Z
T0 ; select first hot end
M581 T1 E2 S0 C0 ;filament sentinel
M557 X45:280 Y45:255 S210 ;configure mesh pointsI am running 2.02(RTOS) (2018-12-24b1)
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Does
G28 X
work? -
I think I may have solved it. Missing S2 on the second last line. That'll teach me to work on this stuff so late at night and tired.