3.5b1 Reset reason: StuckInSpinLoop?
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@Diamondback no need to test 3.4.5.
The odd thing is that the M122 report indicates that the MAIN task is running, but the stack trace reports that the IDLE task is running. These two are not consistent.
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@dc42 So, when I increase the frequency of the endless loop iterations, the issue certainly happens quicker. It also only appears to happen when I use my 8x8 dotstar grid code, but not when I directly control the dotstars with just very simple code.
I'll try to minimize the needed code as much as possible, but my guess atm would be something to do with the arrays I use.
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@Diamondback a few more M122 reports after unexpected resets may be useful too.
You could also test whether reducing the DWC polling interval provokes the problem more quickly.
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@dc42 Alright, so far I have not been successful at replicating it at will, sometimes it happens five times in a row just seconds after starting the board, sometimes things work fine seemingly forever.
Will continue to test and get more M122. -
@Diamondback in that case it's probably an interaction between different tasks that's provoking the problem. Try reducing the DWC polling interval and/or having several instances of DWC attached.
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@dc42 some more M122, I think I figured out why it didn't want to crash anymore yesterday (removed too much code from daemon), trying to reduce the code less now.
=== Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.5beta1+ (2023-01-20 09:47:33) running on Duet 3 MB6HC v1.02 or later (standalone mode) Board ID: 08DJM-9P63L-DJ3T0-6J1F4-3S06S-9A1V9 Used output buffers: 3 of 40 (19 max) === RTOS === Static ram: 151340 Dynamic ram: 113468 of which 0 recycled Never used RAM 80952, free system stack 200 words Tasks: NETWORK(ready,29.8%,211) ETHERNET(notifyWait,0.2%,558) ACCEL(notifyWait,0.0%,348) HEAT(notifyWait,0.0%,328) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,798) CanSender(notifyWait,0.0%,335) CanClock(delaying,0.0%,352) TMC(notifyWait,7.3%,90) MAIN(running,61.6%,953) IDLE(ready,1.1%,30), total 100.0% Owned mutexes: === Platform === Last reset 00:00:11 ago, cause: software Last software reset at 2023-01-21 13:31, reason: StuckInSpinLoop, Gcodes spinning, available RAM 80196, slot 0 Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0040080f BFAR 0x00000000 SP 0x2042025c Task TMC Freestk 98 ok Stack: 004914df 0043059a 41000000 39690453 40c38800 7b79718d 3f8dae65 00000000 42e80000 33c36300 3f859c60 de14b3bb 3f1d3074 ff0c52d6 42880303 38800000 42c80000 43fa0000 44fa0000 20000010 0043057b 00000001 20414f29 2041fe08 004307b9 20420075 2041fd8c Error status: 0x00 Step timer max interval 133 MCU temperature: min 40.5, current 40.6, max 41.4 Supply voltage: min 23.8, current 23.8, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.3, current 12.4, max 12.4, under voltage events: 0 Heap OK, handles allocated/used 99/90, heap memory allocated/used/recyclable 4096/3584/180, gc cycles 4 Events: 4 queued, 4 completed Driver 0: standstill, SG min n/a, mspos 744, reads 61452, writes 14 timeouts 0 Driver 1: standstill, SG min n/a, mspos 360, reads 61452, writes 14 timeouts 0 Driver 2: standstill, SG min n/a, mspos 56, reads 61453, writes 14 timeouts 0 Driver 3: standstill, SG min n/a, mspos 248, reads 61453, writes 14 timeouts 0 Driver 4: standstill, SG min n/a, mspos 520, reads 61453, writes 14 timeouts 0 Driver 5: standstill, SG min n/a, mspos 952, reads 61453, writes 14 timeouts 0 Date/time: 2023-01-21 13:31:45 Slowest loop: 5.50ms; fastest: 0.06ms === Storage === Free file entries: 9 SD card 0 detected, interface speed: 25.0MBytes/sec SD card longest read time 2.4ms, write time 0.0ms, max retries 0 === Move === DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000 no step interrupt scheduled === DDARing 0 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is doing "G4 P500" in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0 Queue2 is idle in state(s) 0 Q0 segments left 0, axes/extruders owned 0x0000000 Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === Filament sensors === Extruder 0: no data received Extruder 1: no data received Extruder 2: no data received Extruder 3: no data received === CAN === Messages queued 133, received 282, lost 0, boc 0 Longest wait 1ms for reply type 6018, peak Tx sync delay 157, free buffers 50 (min 49), ts 56/55/0 Tx timeouts 0,0,0,0,0,0 === Network === Slowest loop: 9.31ms; fastest: 0.03ms Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0) HTTP sessions: 1 of 8 = Ethernet = State: active Error counts: 0 0 0 0 0 0 Socket states: 2 5 2 2 2 0 0 0 = WiFi = Network state is disabled WiFi module is disabled Failed messages: pending 0, notready 0, noresp 0 Socket states: 0 0 0 0 0 0 0 0 === Multicast handler === Responder is inactive, messages received 0, responses 0
M122 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.5beta1+ (2023-01-20 09:47:33) running on Duet 3 MB6HC v1.02 or later (standalone mode) Board ID: 08DJM-9P63L-DJ3T0-6J1F4-3S06S-9A1V9 Used output buffers: 3 of 40 (28 max) === RTOS === Static ram: 151340 Dynamic ram: 113468 of which 0 recycled Never used RAM 80952, free system stack 200 words Tasks: NETWORK(ready,28.3%,227) ETHERNET(notifyWait,0.2%,558) ACCEL(notifyWait,0.0%,348) HEAT(notifyWait,0.0%,322) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,773) CanSender(notifyWait,0.0%,335) CanClock(delaying,0.0%,352) TMC(notifyWait,7.2%,90) MAIN(running,62.9%,953) IDLE(ready,1.3%,30), total 100.0% Owned mutexes: === Platform === Last reset 00:00:09 ago, cause: software Last software reset at 2023-01-21 13:31, reason: StuckInSpinLoop, Gcodes spinning, available RAM 80952, slot 1 Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a80f BFAR 0x00000000 SP 0x20419664 Task IDLE Freestk 44 ok Stack: 004901dd 00490bb4 61000000 a5a5a5a5 004901dd a5a5a5a5 2041aea4 00007dfa 2041f370 20424e2c 2041967c 20424e24 00000004 20424ec8 20424ec8 2041967c 00000000 00000001 204196d8 4e49414d 00000000 00000000 00000001 00000001 00079777 00000000 00000000 Error status: 0x00 Step timer max interval 126 MCU temperature: min 40.5, current 40.6, max 41.5 Supply voltage: min 23.8, current 23.8, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.3, current 12.3, max 12.4, under voltage events: 0 Heap OK, handles allocated/used 99/90, heap memory allocated/used/recyclable 4096/3884/480, gc cycles 3 Events: 4 queued, 4 completed Driver 0: standstill, SG min n/a, mspos 744, reads 52669, writes 14 timeouts 0 Driver 1: standstill, SG min n/a, mspos 360, reads 52669, writes 14 timeouts 0 Driver 2: standstill, SG min n/a, mspos 56, reads 52669, writes 14 timeouts 0 Driver 3: standstill, SG min n/a, mspos 248, reads 52669, writes 14 timeouts 0 Driver 4: standstill, SG min n/a, mspos 520, reads 52670, writes 14 timeouts 0 Driver 5: standstill, SG min n/a, mspos 952, reads 52670, writes 14 timeouts 0 Date/time: 2023-01-21 13:32:16 Slowest loop: 5.50ms; fastest: 0.06ms === Storage === Free file entries: 9 SD card 0 detected, interface speed: 25.0MBytes/sec SD card longest read time 2.5ms, write time 0.0ms, max retries 0 === Move === DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000 no step interrupt scheduled === DDARing 0 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is doing "G4 P500" in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0 Queue2 is idle in state(s) 0 Q0 segments left 0, axes/extruders owned 0x0000000 Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === Filament sensors === Extruder 0: no data received Extruder 1: no data received Extruder 2: no data received Extruder 3: no data received === CAN === Messages queued 119, received 252, lost 0, boc 0 Longest wait 1ms for reply type 6018, peak Tx sync delay 174, free buffers 50 (min 49), ts 48/47/0 Tx timeouts 0,0,0,0,0,0 === Network === Slowest loop: 7.19ms; fastest: 0.03ms Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0) HTTP sessions: 1 of 8 = Ethernet = State: active Error counts: 0 0 0 0 0 0 Socket states: 5 2 2 2 2 0 0 0 = WiFi = Network state is disabled WiFi module is disabled Failed messages: pending 0, notready 0, noresp 0 Socket states: 0 0 0 0 0 0 0 0 === Multicast handler === Responder is inactive, messages received 0, responses 0
M122 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.5beta1+ (2023-01-20 09:47:33) running on Duet 3 MB6HC v1.02 or later (standalone mode) Board ID: 08DJM-9P63L-DJ3T0-6J1F4-3S06S-9A1V9 Used output buffers: 3 of 40 (28 max) === RTOS === Static ram: 151340 Dynamic ram: 113468 of which 0 recycled Never used RAM 80952, free system stack 200 words Tasks: NETWORK(ready,31.5%,244) ETHERNET(notifyWait,0.3%,558) ACCEL(notifyWait,0.0%,348) HEAT(notifyWait,0.0%,328) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,798) CanSender(notifyWait,0.0%,335) CanClock(delaying,0.0%,340) TMC(notifyWait,7.3%,90) MAIN(running,59.9%,953) IDLE(ready,0.9%,30), total 100.0% Owned mutexes: === Platform === Last reset 00:00:13 ago, cause: software Last software reset at 2023-01-21 13:32, reason: StuckInSpinLoop, Gcodes spinning, available RAM 80024, slot 0 Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a80f BFAR 0x00000000 SP 0x20419664 Task IDLE Freestk 44 ok Stack: 004901dd 00490bb8 61000000 a5a5a5a5 004901dd a5a5a5a5 2041aea4 00006c61 2041f370 20424e2c 2041967c 20424e24 00000004 20424ec8 20424ec8 2041967c 00000000 00000001 204196d8 4e49414d 00000000 00000000 00000001 00000001 003a0da3 00000000 00000000 Error status: 0x00 Step timer max interval 127 MCU temperature: min 40.5, current 40.8, max 41.7 Supply voltage: min 23.8, current 23.8, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.3, current 12.4, max 12.4, under voltage events: 0 Heap OK, handles allocated/used 99/90, heap memory allocated/used/recyclable 4096/3932/528, gc cycles 4 Events: 3 queued, 3 completed Driver 0: standstill, SG min n/a, mspos 744, reads 10492, writes 14 timeouts 0 Driver 1: standstill, SG min n/a, mspos 360, reads 10492, writes 14 timeouts 0 Driver 2: standstill, SG min n/a, mspos 56, reads 10493, writes 14 timeouts 0 Driver 3: standstill, SG min n/a, mspos 248, reads 10493, writes 14 timeouts 0 Driver 4: standstill, SG min n/a, mspos 520, reads 10493, writes 14 timeouts 0 Driver 5: standstill, SG min n/a, mspos 952, reads 10493, writes 14 timeouts 0 Date/time: 2023-01-21 13:33:21 Slowest loop: 5.49ms; fastest: 0.06ms === Storage === Free file entries: 9 SD card 0 detected, interface speed: 25.0MBytes/sec SD card longest read time 2.4ms, write time 0.0ms, max retries 0 === Move === DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000 no step interrupt scheduled === DDARing 0 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is doing "G4 P500" in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0 Queue2 is idle in state(s) 0 Q0 segments left 0, axes/extruders owned 0x0000000 Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === Filament sensors === Extruder 0: no data received Extruder 1: no data received Extruder 2: no data received Extruder 3: no data received === CAN === Messages queued 156, received 335, lost 0, boc 0 Longest wait 2ms for reply type 6048, peak Tx sync delay 401, free buffers 50 (min 49), ts 69/68/0 Tx timeouts 0,0,0,0,0,0 === Network === Slowest loop: 7.44ms; fastest: 0.03ms Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0) HTTP sessions: 1 of 8 = Ethernet = State: active Error counts: 0 0 0 0 0 0 Socket states: 5 2 2 2 2 0 0 0 = WiFi = Network state is disabled WiFi module is disabled Failed messages: pending 0, notready 0, noresp 0 Socket states: 0 0 0 0 0 0 0 0 === Multicast handler === Responder is inactive, messages received 0, responses 0
M122 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.5beta1+ (2023-01-20 09:47:33) running on Duet 3 MB6HC v1.02 or later (standalone mode) Board ID: 08DJM-9P63L-DJ3T0-6J1F4-3S06S-9A1V9 Used output buffers: 3 of 40 (21 max) === RTOS === Static ram: 151340 Dynamic ram: 113596 of which 0 recycled Never used RAM 80024, free system stack 202 words Tasks: NETWORK(ready,24.8%,244) ETHERNET(notifyWait,0.3%,558) ACCEL(notifyWait,0.0%,348) HEAT(notifyWait,0.0%,328) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,798) CanSender(notifyWait,0.0%,335) CanClock(delaying,0.0%,352) TMC(notifyWait,7.2%,90) MAIN(running,65.9%,953) IDLE(ready,1.8%,30), total 100.0% Owned mutexes: === Platform === Last reset 00:00:06 ago, cause: software Last software reset at 2023-01-21 13:34, reason: StuckInSpinLoop, Gcodes spinning, available RAM 80952, slot 2 Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a80f BFAR 0x00000000 SP 0x20419664 Task IDLE Freestk 44 ok Stack: 004901dd 00490bb8 61000000 a5a5a5a5 004901dd a5a5a5a5 2041aea4 00007dc0 2041f370 20424e2c 2041967c 20424e24 00000004 20424ec8 20424ec8 2041967c 00000000 00000001 204196d8 4e49414d 00000000 00000000 00000001 00000001 005554bf 00000000 00000000 Error status: 0x00 Step timer max interval 132 MCU temperature: min 40.8, current 40.8, max 41.6 Supply voltage: min 23.8, current 23.9, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.3, current 12.3, max 12.4, under voltage events: 0 Heap OK, handles allocated/used 198/90, heap memory allocated/used/recyclable 4096/4016/612, gc cycles 2 Events: 4 queued, 4 completed Driver 0: standstill, SG min n/a, mspos 744, reads 38237, writes 14 timeouts 0 Driver 1: standstill, SG min n/a, mspos 360, reads 38237, writes 14 timeouts 0 Driver 2: standstill, SG min n/a, mspos 56, reads 38237, writes 14 timeouts 0 Driver 3: standstill, SG min n/a, mspos 248, reads 38237, writes 14 timeouts 0 Driver 4: standstill, SG min n/a, mspos 520, reads 38238, writes 14 timeouts 0 Driver 5: standstill, SG min n/a, mspos 952, reads 38238, writes 14 timeouts 0 Date/time: 2023-01-21 13:34:27 Slowest loop: 5.62ms; fastest: 0.06ms === Storage === Free file entries: 9 SD card 0 detected, interface speed: 25.0MBytes/sec SD card longest read time 2.4ms, write time 0.0ms, max retries 0 === Move === DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000 no step interrupt scheduled === DDARing 0 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is doing "G4 P500" in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0 Queue2 is idle in state(s) 0 Q0 segments left 0, axes/extruders owned 0x0000000 Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === Filament sensors === Extruder 0: no data received Extruder 1: no data received Extruder 2: no data received Extruder 3: no data received === CAN === Messages queued 95, received 195, lost 0, boc 0 Longest wait 1ms for reply type 6018, peak Tx sync delay 62, free buffers 50 (min 49), ts 35/34/0 Tx timeouts 0,0,0,0,0,0 === Network === Slowest loop: 9.56ms; fastest: 0.03ms Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0) HTTP sessions: 1 of 8 = Ethernet = State: active Error counts: 0 0 0 0 0 0 Socket states: 5 2 2 2 2 0 0 0 = WiFi = Network state is disabled WiFi module is disabled Failed messages: pending 0, notready 0, noresp 0 Socket states: 0 0 0 0 0 0 0 0 === Multicast handler === Responder is inactive, messages received 0, responses 0
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@dc42
Ok, so here's the most minimalistic version I can create:daemon.g
while global.daemonActive == true set global.deactivateToolAfterFilamentChange = false while iterations < #global.displayChar0 var lineIndex = iterations ;cache iterations value here since we have a 2D array and need this line counter later again while iterations < #(global.displayChar0[var.lineIndex]) M150 R{global.RGBWhite[0]} U{global.RGBWhite[1]} B{global.RGBWhite[2]} P{global.displayChar0[var.lineIndex][iterations] > 0 ? global.displayDefaultBrightness : 0} S1 F1 M150 R0 U0 B0 P0 S1 F0 ;announce last LED with a dummy G4 P500
Most notably, if I remove the
set global.deactivateToolAfterFilamentChange = false
line, things work fine... However, that piece of code has been running for months just fine, this issue only started appearing with my use of LEDs and/or custom arrays.And the globals (these are created inside a macro that is called from config.g)
if !exists(global.displayChar0) global displayChar0 = {{0,1,1,1,1,1,1,0},{1,1,1,1,1,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,0}} global displayChar1 = {{0,0,1,1,1,0,0,0},{0,0,1,1,1,1,0,0},{0,0,1,1,1,1,1,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0}} global displayChar2 = {{0,1,1,1,1,1,1,0},{1,1,1,1,1,1,1,1},{1,1,1,0,0,1,1,1},{0,1,1,1,0,0,0,0},{0,0,0,1,1,1,0,0},{0,0,0,0,0,1,1,1},{1,1,1,1,1,1,1,1},{1,1,1,1,1,1,1,1}} global displayChar3 = {{0,1,1,1,1,1,1,1},{1,1,1,1,1,1,1,1},{1,1,1,0,0,0,0,0},{0,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,1},{1,1,1,0,0,0,0,0},{1,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,1}} global RGBRed = {255,0,0} global RGBGreen = {0,255,0} global RGBBlue = {0,0,255} global RGBWhite = {255,255,255}
All of the above code has been copied together from various macros, it's usually a lot more generic and this is just the smallest version of the overall stuff that I can produce.
Here's another M122 from that minimal code:
M122 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.5beta1+ (2023-01-20 09:47:33) running on Duet 3 MB6HC v1.02 or later (standalone mode) Board ID: 08DJM-9P63L-DJ3T0-6J1F4-3S06S-9A1V9 Used output buffers: 3 of 40 (19 max) === RTOS === Static ram: 151340 Dynamic ram: 113436 of which 0 recycled Never used RAM 80984, free system stack 200 words Tasks: NETWORK(ready,27.2%,241) ETHERNET(notifyWait,0.2%,434) ACCEL(notifyWait,0.0%,348) HEAT(notifyWait,0.0%,342) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,798) CanSender(notifyWait,0.0%,335) CanClock(delaying,0.0%,352) TMC(notifyWait,7.1%,90) MAIN(running,64.5%,953) IDLE(ready,1.0%,30), total 100.0% Owned mutexes: === Platform === Last reset 00:00:12 ago, cause: software Last software reset at 2023-01-21 14:42, reason: StuckInSpinLoop, Gcodes spinning, available RAM 80984, slot 2 Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a80f BFAR 0x00000000 SP 0x20419664 Task IDLE Freestk 44 ok Stack: 004901dd 00490bb2 61000000 a5a5a5a5 004901dd a5a5a5a5 2041aea4 0003f273 20424e2c 2041f370 2041967c 20424e24 00000004 20424ec8 20424ec8 2041967c 00000000 00000001 204196d8 4e49414d 00000000 00000000 00000001 00000001 014858ad 00000000 00000000 Error status: 0x00 Step timer max interval 126 MCU temperature: min 41.4, current 41.5, max 42.4 Supply voltage: min 23.8, current 23.8, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.3, current 12.4, max 12.4, under voltage events: 0 Heap OK, handles allocated/used 99/89, heap memory allocated/used/recyclable 4096/3548/156, gc cycles 1 Events: 3 queued, 3 completed Driver 0: standstill, SG min n/a, mspos 744, reads 3000, writes 14 timeouts 0 Driver 1: standstill, SG min n/a, mspos 360, reads 3000, writes 14 timeouts 0 Driver 2: standstill, SG min n/a, mspos 56, reads 3000, writes 14 timeouts 0 Driver 3: standstill, SG min n/a, mspos 248, reads 3000, writes 14 timeouts 0 Driver 4: standstill, SG min n/a, mspos 520, reads 3001, writes 14 timeouts 0 Driver 5: standstill, SG min n/a, mspos 952, reads 3001, writes 14 timeouts 0 Date/time: 2023-01-21 14:43:16 Slowest loop: 5.40ms; fastest: 0.06ms === Storage === Free file entries: 10 SD card 0 detected, interface speed: 25.0MBytes/sec SD card longest read time 2.4ms, write time 0.0ms, max retries 0 === Move === DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000 no step interrupt scheduled === DDARing 0 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0 Queue2 is idle in state(s) 0 Q0 segments left 0, axes/extruders owned 0x0000000 Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === Filament sensors === Extruder 0: no data received Extruder 1: no data received Extruder 2: no data received Extruder 3: no data received === CAN === Messages queued 144, received 308, lost 0, boc 0 Longest wait 1ms for reply type 6018, peak Tx sync delay 157, free buffers 50 (min 49), ts 62/61/0 Tx timeouts 0,0,0,0,0,0 === Network === Slowest loop: 9.07ms; fastest: 0.03ms Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0) HTTP sessions: 1 of 8 = Ethernet = State: active Error counts: 0 0 0 0 0 0 Socket states: 5 2 2 2 2 0 0 0 = WiFi = Network state is disabled WiFi module is disabled Failed messages: pending 0, notready 0, noresp 0 Socket states: 0 0 0 0 0 0 0 0 === Multicast handler === Responder is inactive, messages received 0, responses 0
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@dc42
Hm, i think I might have created a macro that causes this all on its own without daemon.g ( I just call this macro as is without any params for this test)var brightness = global.displayDefaultBrightness if exists(param.B) set var.brightness = param.B var activeLEDs = 0 if exists(param.S) set var.activeLEDs = floor(param.S * global.displayLEDCount) var displayContent = "progress" ^ var.activeLEDs if global.lastDisplayContent != var.displayContent set global.lastDisplayContent = var.displayContent while iterations < global.displayLEDCount ;M150 R{param.C[0]} U{param.C[1]} B{param.C[2]} P{iterations < var.activeLEDs ? var.brightness : 0} S1 F1 ;3.5+ var isFrame = iterations < 8 || iterations > 55 var isProgress = false ;todo var isActive = var.isFrame || var.isProgress M150 R255 U0 B0 P{var.isActive ? var.brightness : 0} S1 F1 M150 R0 U0 B0 P0 S1 F0 ;announce last LED with a dummy
This immediately makes the board crash every time, here's an M122 for this:
M122 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.5beta1+ (2023-01-20 09:47:33) running on Duet 3 MB6HC v1.02 or later (standalone mode) Board ID: 08DJM-9P63L-DJ3T0-6J1F4-3S06S-9A1V9 Used output buffers: 3 of 40 (22 max) === RTOS === Static ram: 151340 Dynamic ram: 113436 of which 0 recycled Never used RAM 80984, free system stack 200 words Tasks: NETWORK(ready,32.2%,221) ETHERNET(notifyWait,0.3%,432) ACCEL(notifyWait,0.0%,348) HEAT(notifyWait,0.0%,328) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,796) CanSender(notifyWait,0.0%,335) CanClock(delaying,0.0%,340) TMC(notifyWait,7.2%,90) MAIN(running,60.2%,953) IDLE(ready,0.2%,30), total 100.0% Owned mutexes: === Platform === Last reset 00:01:09 ago, cause: software Last software reset at 2023-01-21 14:56, reason: StuckInSpinLoop, Gcodes spinning, available RAM 80920, slot 2 Software reset code 0x4083 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0044a80f BFAR 0x00000000 SP 0x20419664 Task IDLE Freestk 44 ok Stack: 004901dd 00490bba 61000000 a5a5a5a5 004901dd a5a5a5a5 2041aea4 00021363 20424e2c 2041f370 2041967c 20424e24 00000004 20419100 20419100 2041967c 00000000 00000001 204196d8 4e49414d 00000000 00000000 00000001 00000001 02b69a1b 00000000 00000000 Error status: 0x00 Step timer max interval 139 MCU temperature: min 41.1, current 41.3, max 42.3 Supply voltage: min 23.8, current 23.9, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.3, current 12.4, max 12.4, under voltage events: 0 Heap OK, handles allocated/used 99/89, heap memory allocated/used/recyclable 4096/3776/384, gc cycles 1 Events: 4 queued, 4 completed Driver 0: standstill, SG min n/a, mspos 744, reads 61186, writes 14 timeouts 0 Driver 1: standstill, SG min n/a, mspos 360, reads 61186, writes 14 timeouts 0 Driver 2: standstill, SG min n/a, mspos 56, reads 61186, writes 14 timeouts 0 Driver 3: standstill, SG min n/a, mspos 248, reads 61186, writes 14 timeouts 0 Driver 4: standstill, SG min n/a, mspos 520, reads 61186, writes 14 timeouts 0 Driver 5: standstill, SG min n/a, mspos 952, reads 61186, writes 14 timeouts 0 Date/time: 2023-01-21 14:57:41 Slowest loop: 5.51ms; fastest: 0.06ms === Storage === Free file entries: 10 SD card 0 detected, interface speed: 25.0MBytes/sec SD card longest read time 2.4ms, write time 0.0ms, max retries 0 === Move === DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000 no step interrupt scheduled === DDARing 0 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0 Queue2 is idle in state(s) 0 Q0 segments left 0, axes/extruders owned 0x0000000 Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === Filament sensors === Extruder 0: no data received Extruder 1: no data received Extruder 2: no data received Extruder 3: no data received === CAN === Messages queued 657, received 1476, lost 0, boc 0 Longest wait 1ms for reply type 6042, peak Tx sync delay 276, free buffers 50 (min 49), ts 347/346/0 Tx timeouts 0,0,0,0,0,0 === Network === Slowest loop: 9.82ms; fastest: 0.03ms Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0) HTTP sessions: 1 of 8 = Ethernet = State: active Error counts: 0 0 0 1 0 0 Socket states: 5 2 2 2 2 0 0 0 = WiFi = Network state is disabled WiFi module is disabled Failed messages: pending 0, notready 0, noresp 0 Socket states: 0 0 0 0 0 0 0 0 === Multicast handler === Responder is inactive, messages received 0, responses 0
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@dc42
It looks like this line is the culprit:var isActive = var.isFrame || var.isProgress
, when I remove it (and directly use that expression below), it works fine...Disregard, now that line works fine, so probably some random component to it again...
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@dc42 Now I prevented it from crashing by moving a global set to a later place...
if global.lastDisplayContent != var.displayContent set global.lastDisplayContent = var.displayContent while iterations < global.displayLEDCount ;M150 R{param.C[0]} U{param.C[1]} B{param.C[2]} P{iterations < var.activeLEDs ? var.brightness : 0} S1 F1 ;3.5+ var isFrame = iterations < 8 || iterations > 55 var isProgress = false ;todo var isActive = var.isFrame || var.isProgress M150 R255 U0 B0 P{var.isActive ? var.brightness : 0} S1 F1 M150 R0 U0 B0 P0 S1 F0 ;announce last LED with a dummy
becomes:
if global.lastDisplayContent != var.displayContent while iterations < global.displayLEDCount ;M150 R{param.C[0]} U{param.C[1]} B{param.C[2]} P{iterations < var.activeLEDs ? var.brightness : 0} S1 F1 ;3.5+ var isFrame = iterations < 8 || iterations > 55 var isProgress = false ;todo var isActive = var.isFrame || var.isProgress M150 R255 U0 B0 P{var.isActive ? var.brightness : 0} S1 F1 M150 R0 U0 B0 P0 S1 F0 ;announce last LED with a dummy set global.lastDisplayContent = var.displayContent
Note how line #2 moved. This somewhat aligns with the crash in daemon.g where a global set also had critical impact on it...
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@Diamondback what values do you set for the global variables before running this macro? I tried the following values, but it doesn't crash.
global displayLEDCount=20
global lastDisplayContent="none"
global displayDefaultBrightness=10 -
global displayLEDCount = 64 global displayDefaultBrightness = 10 global lastDisplayContent = ""
The more I play around with it, the more I think it's a timing issue... Sometimes I can do things fine by updating the 64 dotstar pixels with 500ms delay between them but not with 100ms etc.
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@Diamondback said in 3.5b1 Reset reason: StuckInSpinLoop?:
global displayLEDCount = 64
global displayDefaultBrightness = 10
global lastDisplayContent = ""It still doesn't crash for me. Perhaps it depends on what global variables you have created already? Can you share your whole config.g file and any macros that it calls?
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@dc42
config.g;M929 S3 ;enable debug logging ;M575 P1 S1 B57600 ;Enable PanelDue Port G90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"V-Core Toolchanger" ; set printer name ; Enable network M552 P0.0.0.0 S1 M669 K1 ; select CoreXY mode G4 S2 ; wait for expansion boards to start ; Drives ;XY1: back left ;XY2: back right M569 P0.2 S0 ; stepper XY1 M569 P0.3 S0 ; stepper XY2 M569 P0.4 S1 ; stepper Coupler M569 P100.0 S0 ; stepper E0 M569 P100.1 S0 ; stepper E1 M569 P100.2 S0 ; stepper E2 M569 P100.3 S0 ; stepper E3 M569 P0.0 S0 ; stepper Z1 M569 P0.1 S0 ; stepper Z2 M569 P0.5 S0 ; stepper Z3 M584 X0.3 Y0.2 C0.4 ; set drive mapping (motion system X Y C) M584 E100.0:100.1:100.2:100.3 ; set drive mapping (extruders) M584 Z0.0:0.1:0.5 ; set drive mapping (motion system Z) ;Leadscrew order (starting back center, then clockwise): ;1: back center ;2: front right ;3: front left M671 X-12:216:-203 Y222:-179:-179 S30 ; set Z leadscrew positions ; Axis Limits if !exists(global.hasRunInit) global minY = -266 global maxY = 115 M208 X-148:160 Y{global.minY,global.maxY} ; set axis minima & maxima M208 C0:250 Z-2:270 ; set axis minima & maxima M92 X80.00 Y80.00 ; X/Y: 1.8°/step ;M92 X160.00 Y160.00 ; X/Y: 0.9°/step M92 C200.00 ; C: E3D coupler M92 Z800.00 ; Z: TR8x4 leadscrews M350 X16 Y16 I1 ; configure microstepping with interpolation M350 C16 Z16 I1 ; configure microstepping with interpolation M566 X600 Y600 C2 Z50 ; set maximum instantaneous speed changes (mm/min) M203 X30000 Y30000 C10000 Z2000 ; set maximum speeds (mm/min) M201 X5000 Y5000 C500 Z350 ; set accelerations (mm/s^2) M204 P500 T5000 ;M204 P5000 T5000 M906 X2000 Y2000 ; set motor currents (mA) and motor idle factor in per cent M906 C700 ; set motor currents (mA) and motor idle factor in per cent M906 Z1500 ; set motor currents (mA) and motor idle factor in per cent M906 E500:500:500:500 ; set motor currents (mA) and motor idle factor in per cent (4x LGX) M906 I50 ;only a single idle factor allowed for ALL steppers M84 S30 ; Set idle timeout ;=================== Extruder ====================== M92 E408:408:408:408 ; set steps per mm M350 E16:16:16:16 I1 ; configure microstepping M566 E500:500:500:500 ; set maximum instantaneous speed changes (mm/min) ; used to be at 1200 M203 E15000:15000:15000:15000 ; set maximum speeds (mm/min) M201 E3000:3000:3000:3000 ; set accelerations (mm/s^2) ;==================================================== ; Endstops M574 X2 S1 P"0.io0.in" ; configure active-high endstop for high end on X via pin xstop M574 Y1 S1 P"0.io1.in" ; configure active-high endstop for high end on Y via pin ystop M574 Z0 ; No Z-Endstop (use as probe instead) ; Z-Probe if !exists(global.hasRunInit) global zProbeSpeedFeed = 300 global zProbeSpeedFeedLevel = 1500 global zProbeSpeedTravel = 20000 global zProbeDiveHeightLevel = 30 global zProbeDiveHeightMesh = 3 global zProbePin = "0.io2.in" global zProbeType = 8 global zProbeTriggerValue = 200 global minXMesh = -146 global maxXMesh = 150 global minYMesh = -150 global maxYMesh = 150 global meshPointSpacing = 30 M558 K0 P{global.zProbeType} C{global.zProbePin} H{global.zProbeDiveHeightMesh} F{global.zProbeSpeedFeed} T{global.zProbeSpeedTravel} ; Z Endstop/probe M558 K2 P8 C"0.io4.in" H10 F100 T20000 ; tool length switch G31 K0 X0 Y0 Z0 P200 ;G31 K1 X0 Y0 Z0 P200 G31 K2 X0 Y0 Z0 P200 ;G31 K0 X0 Y0 Z0 P{global.zProbeTriggerValue} ; set Z probe trigger value, offset and trigger height, offsets here are hardcoded in leveling macro as well M557 X{global.minXMesh, global.maxXMesh} Y{global.minYMesh, global.maxYMesh} S{global.meshPointSpacing} ; define mesh grid M376 H30 ; Set bed correction taper ; Heaters M308 S0 P"100.temp0" Y"thermistor" T100000 B3950 ; configure sensor 0 as thermistor M950 H0 C"100.out0" T0 Q10 ; create bed heater output and map it to sensor 0 M143 H0 S121 ; set temperature limit for heater 0 to 121C M307 H0 B0 R0.676 C345.1 D2.68 S1.00 V24.3 ; Bed PID Tuning M140 H0 ; map heated bed to heater 0 M308 S1 P"0.temp1" Y"thermistor" T100000 B4725 C7.06e-8 ; configure sensor 1 as thermistor M950 H1 C"0.out1" T1 ; create nozzle heater output and map it to sensor 1 M143 H1 S301 ; set temperature limit for heater 1 to 301C M308 S2 P"0.temp2" Y"thermistor" T100000 B4725 C7.06e-8 ; configure sensor 2 as thermistor M950 H2 C"0.out2" T2 ; create nozzle heater output and map it to sensor 2 M143 H2 S301 ; set temperature limit for heater 2 to 301C M308 S3 P"100.temp1" Y"thermistor" T100000 B4725 C7.06e-8 ; configure sensor 3 as thermistor M950 H3 C"100.out1" T3 ; create nozzle heater output and map it to sensor 3 M143 H3 S301 ; set temperature limit for heater 3 to 301C M308 S4 P"100.temp2" Y"thermistor" T100000 B4725 C7.06e-8 ; configure sensor 2 as thermistor M950 H4 C"100.out2" T4 ; create nozzle heater output and map it to sensor 2 M143 H4 S301 ; set temperature limit for heater 2 to 301C M302 S190 R190 ;Cold extrusion settings M307 H1 R4.637 K0.673:0.218 D2.31 E1.35 S1.00 B0 V24.2 ; PID Tuning T0 M307 H2 R4.174 K0.555:0.276 D1.96 E1.35 S1.00 B0 V24.2 ; PID Tuning T1 M307 H3 R4.301 K0.536:0.105 D1.89 E1.35 S1.00 B0 V24.2 ; PID Tuning T2 M307 H4 R3.780 K0.576:0.060 D1.57 E1.35 S1.00 B0 V24.2 ; PID Tuning T3 ; Fans M950 F0 C"0.out7" ; Hotend Fan Tool 0 M106 P0 S255 L255 H1 T50 C"T0 Hotend" ; Hotend Fan Tool 0 M950 F1 C"0.out4" Q50 ; Layer Fan Tool 0 M106 P1 S0 H-1 C"T0" ; Layer Fan Tool 0 M950 F2 C"0.out8" ; Hotend Fan Tool 1 M106 P2 S255 L255 H2 T50 C"T1 Hotend" ; Hotend Fan Tool 1 M950 F3 C"0.out5" Q50 ; Layer Fan Tool 1 M106 P3 S0 H-1 C"T1" ; Layer Fan Tool 1 M950 F4 C"100.out5" ; Hotend Fan Tool 2 M106 P4 S255 L255 H3 T50 C"T2 Hotend" ; Hotend Fan Tool 2 M950 F5 C"100.out3" Q50 ; Layer Fan Tool 2 M106 P5 S0 H-1 C"T2" ; Layer Fan Tool 2 M950 F6 C"100.out6" ; Hotend Fan Tool 3 M106 P6 S255 L255 H4 T50 C"T3 Hotend" ; Hotend Fan Tool 3 M950 F7 C"100.out4" Q50 ; Layer Fan Tool 3 M106 P7 S0 H-1 C"T3" ; Layer Fan Tool 3 ;Static layer fan M950 F8 C"0.out0" Q65535 ; static layer fan M106 P8 S0 H-1 I1 L0.2 C"RSCS" ; Tools M563 P0 D0 H1 F1 ; define tool 0 G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C M563 P1 D1 H2 F3 ; define tool 1 G10 P1 R0 S0 ; set initial tool 1 active and standby temperatures to 0C M563 P2 D2 H3 F5 ; define tool 2 G10 P2 R0 S0 ; set initial tool 2 active and standby temperatures to 0C M563 P3 D3 H4 F7 ; define tool 3 G10 P3 R0 S0 ; set initial tool 3 active and standby temperatures to 0C M563 P4 S"Pen" ; define tool 4 (Pen) ;Dock present switches M950 J0 C"0.io7.in" ; Tool 0 Dock switch M950 J1 C"0.io8.in" ; Tool 1 Dock switch M950 J2 C"100.io5.in" ; Tool 2 Dock switch M950 J3 C"100.io6.in" ; Tool 3 Dock switch ;additional tool related switches M950 J4 C"0.io3.in" ;potential toolhead tool present switch, not installed atm, but already wired up inside the box ;Filament sensors, not installed atm, but already wired up inside the box M591 D0 P4 C"100.io0.in" S1 L23.2 R70:150 E5 M591 D1 P4 C"100.io1.in" S1 L23.2 R70:150 E5 M591 D2 P4 C"100.io2.in" S1 L23.2 R70:150 E5 M591 D3 P4 C"100.io3.in" S1 L23.2 R70:150 E5 M950 S0 C"0.out9" Q333 ;PebbleWiper Servo M280 P0 S70 ;Servo in idle position M950 P1 C"0.io5.out" ;Light switch PWM ;Toolhead Dotstar M150 X0 ;Accelerometer M955 P0 C"spi.cs2+spi.cs3" ;Inputshaping ;M593 P"zvddd" F70 S0.2 ; Miscellaneous M98 P"/macros/Misc/ToolheadDisplay/InitToolheadDisplay" M98 P"/macros/Misc/Lights/On" M98 P"/sys/config-tools.g" if !exists(global.hasRunInit) global pebbleFeedSpeedDefault = 300 global pebbleFeedSpeed = global.pebbleFeedSpeedDefault global deactivateToolAfterFilamentChange = false global displayActiveToolOnHead = true global hasRunInit = true global daemonActive = false
InitToolheadDisplay
if !exists(global.displayLEDCount) global displayLEDCount = 64 global displayDefaultBrightness = 10 global lastDisplayContent = "" ;global displayDigit = {null, null, null, null, null, null, null, null, null, null} ;enable once we can set individual elements of arrays ;set global.displayDigit[0] = {{0,1,1,1,1,1,1,0},{1,1,1,1,1,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,0}} ;set global.displayDigit[1] = {{0,0,1,1,1,0,0,0},{0,0,1,1,1,1,0,0},{0,0,1,1,1,1,1,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0}} ;set global.displayDigit[2] = {{0,1,1,1,1,1,1,0},{1,1,1,1,1,1,1,1},{1,1,1,0,0,1,1,1},{0,1,1,1,0,0,0,0},{0,0,0,1,1,1,0,0},{0,0,0,0,0,1,1,1},{1,1,1,1,1,1,1,1},{1,1,1,1,1,1,1,1}} ;set global.displayDigit[3] = {{0,1,1,1,1,1,1,1},{1,1,1,1,1,1,1,1},{1,1,1,0,0,0,0,0},{0,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,1},{1,1,1,0,0,0,0,0},{1,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,1}} if !exists(global.displayChar0) && boards[0].firmwareVersion != "3.4.5" global displayChar0 = {{0,1,1,1,1,1,1,0},{1,1,1,1,1,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,0,0,1,1,1},{1,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,0}} global displayChar1 = {{0,0,1,1,1,0,0,0},{0,0,1,1,1,1,0,0},{0,0,1,1,1,1,1,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0},{0,0,1,1,1,0,0,0}} global displayChar2 = {{0,1,1,1,1,1,1,0},{1,1,1,1,1,1,1,1},{1,1,1,0,0,1,1,1},{0,1,1,1,0,0,0,0},{0,0,0,1,1,1,0,0},{0,0,0,0,0,1,1,1},{1,1,1,1,1,1,1,1},{1,1,1,1,1,1,1,1}} global displayChar3 = {{0,1,1,1,1,1,1,1},{1,1,1,1,1,1,1,1},{1,1,1,0,0,0,0,0},{0,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,1},{1,1,1,0,0,0,0,0},{1,1,1,1,1,1,1,1},{0,1,1,1,1,1,1,1}} global RGBOff = {0,0,0,0} global RGBRed = {255,0,0,25} global RGBGreen = {0,255,0,10} global RGBBlue = {0,0,255,45} global RGBWhite = {255,255,255,10}
Lights/On
M42 P1 S230
config-tools.g
if !exists(global.hasRunInit) ;global toolNozzleSizes = {0,0,0,0} ;global toolNozzleMaterials = {"brass","brass","brass","brass"} global tool0NozzleSize = "0.0" global tool1NozzleSize = "0.0" global tool2NozzleSize = "0.0" global tool3NozzleSize = "0.0" global tool0NozzleMaterial = "" global tool1NozzleMaterial = "" global tool2NozzleMaterial = "" global tool3NozzleMaterial = "" M98 P"/sys/config-tools-size.g" M98 P"/sys/config-tools-material.g" ;Z-Offset: If nozzle is too close to bed _reduce_ offset (negative number becomes more negative) ; If nozzle is too far away, _increase_ offset (negative number becomes less negative) ;Tool offsets G10 P0 X-8.340 Y39.270 Z-4.190 G10 P1 X-8.480 Y39.310 Z-4.020 G10 P2 X-8.180 Y38.930 Z-4.200 G10 P3 X-8.360 Y39.060 Z-4.506 G10 P4 X0 Y46.5 Z-20.000 ; set tool 4 axis offsets ; Filament Nozzle PA R-Distance R-Speed ; -------------- -------- ----- ------------ --------- ; Generic PETG 0.25 0.175 0.6 2100 ; --- 0.3 0.13 0.6 2100 ; --- 0.4 0.1 0.6 2100 ; --- 0.6 0.05 0.6 2100 ; --- 0.8 0.03 0.6 2100 ; Generic PLA 0.25 0.0 0.6 2100 ; --- 0.3 0.0 0.6 2100 ; --- 0.4 0.08 0.6 2100 ; --- 0.6 0.0 0.6 2100 ; --- 0.8 0.0 0.6 2100 ; BioFusion 0.25 0.0 0.6 2100 ; --- 0.3 0.09 0.6 2100 ; --- 0.4 0.07 0.6 2100 ; --- 0.6 0.0 0.6 2100 ; --- 0.8 0.035 0.6 2100 ; PA-CF 0.3 0.0 0.6 2100 ; --- 0.4 0.0 0.6 2100 ; PC-CF 0.3 0.0 0.6 2100 ; --- 0.4 0.0 0.6 2100 ; PA12 0.25 0.0 0.6 2100 ; --- 0.3 0.0 0.6 2100 ; --- 0.4 0.13 0.6 2100 ; --- 0.6 0.0 0.6 2100 ; --- 0.8 0.0 0.6 2100 ; Wood 0.8 0.04 0.6 2100 ; TPU 0.4 0.0 1.0 2100 ;https://ozh.github.io/ascii-tables/
config-tools-size.g
set global.tool0NozzleSize = "0.4" set global.tool1NozzleSize = "0.4" set global.tool2NozzleSize = "0.4" set global.tool3NozzleSize = "0.6"
config-tools-material.g
set global.tool0NozzleMaterial = "brass" set global.tool1NozzleMaterial = "brass" set global.tool2NozzleMaterial = "brass" set global.tool3NozzleMaterial = "nozzlex" ;set global.toolNozzleMaterials = {"brass","brass","brass","nozzlex"}
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@Diamondback thanks.
I still couldn't make it crash with your files, but I eventually got a crash with a similar M122 report to yours after running this macro several times:
var activeLEDs=10 while iterations < 1000 var displayContent = "progress" ^ var.activeLEDs set global.lastDisplayContent = var.displayContent echo "Done"
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@dc42 Yea it seems quite random what exactly triggers it, the only things in common for me seem to be some of interaction with custom variables/arrays and possibly the dotstar LEDs, ofc, either one could be a coincidence...
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@Diamondback I suspect it's an interaction between DWC polling the object model (which involves reading some values from the heap) and garbage collection of the heap taking place because string or array variables are being reassigned.
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@dc42 I played around with the DWC polling time this morning but didn't get any immediate results, I'll play around with it some more and see if I can maybe make it go away by setting it much higher?
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@Diamondback my next step will be to disconnect DWC completely and then see if I can provoke the reset by sending the command to run the macro over USB.
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@dc42 Hm, I guess I can try the same by having the issue triggered by daemon.g and not having any browser connected to it? Or does DWC still do stuff in the background then somehow?