Pause/resume issues in 3.5.0rc3+5?
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@gloomyandy Yeah I know, I meant the 3.5-mms-changes branch David made March first and the commits made to that branch March 4th [1] & [2] related to resume after pause. I stated the wrong branch name in the previous post(edited it by now).
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@Exerqtor please try the 3.5.0-rc.3+6 build at https://www.dropbox.com/scl/fo/x7ec0sg11a2zrevxoj3j8/h?rlkey=pcdfiv72z0dkkrbv5i8cem5fd&dl=0.
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@Exerqtor oops, that's the wrong firmware build. Give me a few minutes to correct it.
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@Exerqtor I've updated those files.
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@dc42
Aaah i just did a test with the first ones you supplied there and was about to repport that the issue is persistent.I'll try the NEWER ones after dinner and report back!
@dc42 Naah that build is borked! Now Z won't even move after homing. Or if i try to move the bed from PD / DWC nothing happens.
The printer reported Z0.54 after homing, and if i try to lower Z with 5mm the reported Z-height changes to 5.54 but no actual movement.
Don't know if M122 reports will help any, but here they are:
=== Diagnostics === RepRapFirmware for Duet 3 Mini 5+ version 3.5.0-rc.3+6 (2024-04-02 14:34:06) running on Duet 3 Mini5plus WiFi (standalone mode) Board ID: XNHXF-HR6KL-K65J0-409N2-K9W1Z-RV2MZ Used output buffers: 29 of 40 (40 max) === RTOS === Static ram: 103232 Dynamic ram: 126672 of which 12 recycled Never used RAM 8380, free system stack 135 words Tasks: NETWORK(2,nWait 7,16.1%,229) HEAT(3,nWait 6,0.0%,351) Move(4,nWait 6,0.0%,256) CanReceiv(6,nWait 1,0.1%,797) CanSender(5,nWait 7,0.0%,336) CanClock(7,delaying,0.0%,339) TMC(4,nWait 6,0.8%,68) MAIN(1,running,81.2%,654) IDLE(0,ready,0.9%,30) AIN(4,delaying,0.8%,260), total 100.0% Owned mutexes: WiFi(NETWORK) === Platform === Last reset 00:19:21 ago, cause: software Last software reset at 2024-04-02 15:40, reason: User, Gcodes spinning, available RAM 11360, slot 1 Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00489000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a Error status: 0x04 Aux0 errors 0,0,0 MCU revision 3, ADC conversions started 1161890, completed 1161890, timed out 0, errs 0 MCU temperature: min 39.6, current 43.6, max 47.8 Supply voltage: min 2.8, current 24.1, max 24.4, under voltage events: 0, over voltage events: 0, power good: yes Heap OK, handles allocated/used 99/43, heap memory allocated/used/recyclable 2048/1500/940, gc cycles 264 Events: 0 queued, 0 completed Driver 0: standstill, SG min 0, read errors 0, write errors 0, ifcnt 32, reads 61101, writes 32, timeouts 0, DMA errors 0, CC errors 0 Driver 1: standstill, SG min 0, read errors 0, write errors 0, ifcnt 32, reads 61101, writes 32, timeouts 0, DMA errors 0, CC errors 0 Driver 2: standstill, SG min 0, read errors 0, write errors 0, ifcnt 22, reads 61111, writes 22, timeouts 0, DMA errors 0, CC errors 0 Driver 3: standstill, SG min 0, read errors 0, write errors 0, ifcnt 21, reads 61111, writes 21, timeouts 0, DMA errors 0, CC errors 0 Driver 4: standstill, SG min 0, read errors 0, write errors 0, ifcnt 21, reads 61112, writes 21, timeouts 0, DMA errors 0, CC errors 0 Driver 5: not present Driver 6: not present Date/time: 2024-04-02 16:36:25 Cache data hit count 2117861953 Slowest loop: 164.57ms; fastest: 0.13ms === Storage === Free file entries: 16 SD card 0 detected, interface speed: 22.5MBytes/sec SD card longest read time 7.6ms, write time 8.1ms, max retries 0 === Move === DMs created 83, segments created 11, maxWait 737572ms, bed compensation in use: none, height map offset 0.000, max steps late 1, min interval 0, bad calcs 0, ebfmin 0.00, ebfmax 0.00 no step interrupt scheduled Moves shaped first try 5, on retry 0, too short 0, wrong shape 4, maybepossible 0 === DDARing 0 === Scheduled moves 25, completed 25, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === DDARing 1 === Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0 Heater 0 is on, I-accum = 0.4 Heater 1 is on, I-accum = 0.0 === GCodes === Movement locks held by null, null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 0 0 0 0, running macro Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is doing "G4 P250" in state(s) 0 0, running macro Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 File2 is idle in state(s) 0 Queue2 is idle in state(s) 0 Q0 segments left 0, axes/extruders owned 0x0000807 Code queue 0 is empty Q1 segments left 0, axes/extruders owned 0x0000000 Code queue 1 is empty === Filament sensors === check 0 clear 0 Extruder 0 sensor: no filament === CAN === Messages queued 10493, received 23836, lost 0, errs 1307, boc 0 Longest wait 2ms for reply type 6031, peak Tx sync delay 8139, free buffers 26 (min 25), ts 5810/5808/0 Tx timeouts 0,0,1,0,0,0 last cancelled message type 30 dest 127 === Network === Slowest loop: 201.24ms; fastest: 0.00ms Responder states: MQTT(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) HTTP sessions: 2 of 8 === WiFi === Interface state: active Module is connected to access point Failed messages: pending 0, notrdy 1, noresp 1 Firmware version 2.1beta7 MAC address c4:5b:be:ce:91:93 Module reset reason: Power up, Vcc 3.37, flash size 2097152, free heap 36232 WiFi IP address 192.168.10.x Signal strength -54dBm, channel 6, mode 802.11n, reconnections 0 Clock register 00002001 Socket states: 0 0 0 0 0 0 0 0 M122 B121 Diagnostics for board 121: Duet TOOL1LC rev 1.1 or later firmware version 3.5.0-rc.3+6 (2024-04-02 12:49:31) Bootloader ID: SAMC21 bootloader version 2.8 (2023-07-25) All averaging filters OK Never used RAM 3928, free system stack 134 words Tasks: Move(3,nWait 7,0.0%,135) HEAT(2,nWait 6,0.4%,105) CanAsync(5,nWait 4,0.0%,51) CanRecv(3,nWait 1,0.0%,71) CanClock(5,nWait 1,0.0%,59) ACCEL(3,nWait 6,0.0%,53) TMC(2,nWait 6,3.4%,53) MAIN(1,running,91.2%,315) IDLE(0,ready,0.0%,27) AIN(2,delaying,4.9%,112), total 100.0% Owned mutexes: Last reset 00:19:29 ago, cause: power up Last software reset at 2024-03-12 16:55, reason: StackOverflow, available RAM 2968, slot 0 Software reset code 0x0100 ICSR 0x0042600e SP 0x20007f34 Task Move Freestk 3342 ok Stack: 20004a80 20004ab4 0001cf33 20004c98 20004938 00000000 0001c011 20003320 fffffffd a5a5a5a5 00000000 20007f8c 00000000 20007f8c 0001cc97 00000000 200017c4 20001748 0001c4d7 20001748 200017c4 00000032 454c4449 00022700 0001ac77 200018e0 200018e0 Driver 0: pos 0, 568.8 steps/mm, standstill, SG min 0, read errors 0, write errors 0, ifcnt 11, reads 60547, writes 11, timeouts 0, DMA errors 0, CC errors 0, steps req 0 done 0 Moves scheduled 0, completed 0, in progress 0, hiccups 0, segs 0, step errors 0, maxLate 0 maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0, ebfmin 0.00 max 0.00 Peak sync jitter -2/9, peak Rx sync delay 219, resyncs 0/0, no timer interrupt scheduled VIN voltage: min 23.7, current 24.7, max 24.9 MCU temperature: min 65.2C, current 71.7C, max 71.7C Last sensors broadcast 0x00000012 found 2 15 ticks ago, 0 ordering errs, loop time 0 CAN messages queued 24032, send timeouts 0, received 10573, lost 0, errs 0, boc 0, free buffers 18, min 18, error reg 0 dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0 Accelerometer: LIS3DH, status: 00 I2C bus errors 0, naks 3, contentions 0, other errors 0 === Filament sensors === Interrupt 5726621 to 0us, poll 4 to 1432us Driver 0: ok
I just saw that the printer state is permanently "Busy" now after trying to home & lower Z. Dispite the printer not doing anything.
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@Exerqtor I'm sorry about that, I'm about to run a print to test the correction.
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@dc42 Nothing to say sorry for, it's a pre-release afterall
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@Exerqtor I've updated the files, same link as before. A remaining issue I have noticed is that when resuming after a pause there is a slight delay between restoring the XYZ position and starting printing again. I think I know the reason for that and I'll look into it tomorrow.
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@dc42 Okok, I'll pull them, try one least time and report back before hitting the bunk.
A little bit off topic, but: I don't know if this is expected behaviour or (or when it got introduced), but for some reason this command:
M291 S4 R"Bed tramming" P"Are you sure you want to tram the bed?" K{"YES","CANCEL",}
Don't end up posting a message on PD, just DWC.
And I can confirm that the resume now works again, and that the Z-issues is resolved. I didn't notice any delay between between restoring the XYZ position and starting printing again though, at least not more than it's "allways" been.
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@Exerqtor which version of PanelDueFirmware are you using?
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@dc42 Uuhm i'm quite sure it's 3.5.0-rc8 / the latest one avalible on github.
I'll check once i get home.
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@Exerqtor it works for me if I run that command from the DWC console, using the latest firmware build and PanaDueFirmware 3.5.0-rc6. I'll re-test using -rc8.
Edit: and using -rc8 it displays on both too. Does that box display on both DWC and PD when you run it from the DWC console?
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@dc42 Ok, then i bet i've forgot to install rc8 or something, I'll have a look later!
Didn't try the command in DWC console, but the if i trued running the bed leveling from PD (that command is part of bed.g) nothing popped up on PD, so i went to check in DWC an there it was displayed.
Edit:
Just got home and checked PD, it's got 3.5.0-rc8 installed like I thought. And i just tried to run a tram from the button on PD, now it displayed the message like it should. So idk what was going on yesterday tbh.