Duet3D Logo Duet3D
    • Tags
    • Documentation
    • Order
    • Register
    • Login

    Nozzle gets smashed against the bed

    Scheduled Pinned Locked Moved
    Other control boards
    6
    57
    2.6k
    Loading More Posts
    • Oldest to Newest
    • Newest to Oldest
    • Most Votes
    Reply
    • Reply as topic
    Log in to reply
    This topic has been deleted. Only users with topic management privileges can see it.
    • MJCTundefined
      MJCT @Phaedrux
      last edited by

      @Phaedrux
      I tried to use the formula when I was using the config tool, but that value was provided by the manufacturer. But I will double cheek it tomorrow

      1 Reply Last reply Reply Quote 0
      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        Who is the manufacturer? What type of printer is this?

        Z-Bot CoreXY Build | Thingiverse Profile

        MJCTundefined 1 Reply Last reply Reply Quote 0
        • MJCTundefined
          MJCT @Phaedrux
          last edited by

          @Phaedrux

          @Phaedrux said in Nozzle gets smashed against the bed:

          Who is the manufacturer? What type of printer is this?

          More on that tomorrow, I prefer to confirm first everything I say about a company on the web. It would be terribly unfair for them if I was making some kind of confusion.
          The printer is a core XY based on V rails

          1 Reply Last reply Reply Quote 0
          • fcwiltundefined
            fcwilt @Phaedrux
            last edited by

            @Phaedrux said in Nozzle gets smashed against the bed:

            @MJCT said in Nozzle gets smashed against the bed:

            M92 X80.00 Y80.00 Z4000.00 E96.94 ; set steps per mm

            Z steps per mm of 4000 doesn't sound correct.

            Z_steps_per_mm = (motor_steps_per_rev * driver_microstep) / screw_lead

            That does not sound right. For a typical 8mm lead and 1.8 steppers the steps/mm would be 400. 4000 would mean a 0.8mm lead which doesn't seem likely.

            Frederick

            Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

            1 Reply Last reply Reply Quote 0
            • Vetiundefined
              Veti
              last edited by

              4000 is the default value in the configurator.
              this value was used for one the first 3d printers which used m5 threaded rods.

              here is a picture of the ones used some time ago.
              https://www.instructables.com/id/3D-Printer-Lead-Screw-Upgrade/

              most modern 3d printers now use a 4 start lead screw with a 8mm pitch which results in 400 steps per mm.

              if your printer really has one of the old ones, you should swap that out before you do any prints, as it will result it very poor prints.

              1 Reply Last reply Reply Quote 0
              • Vetiundefined
                Veti
                last edited by

                also you have a beta value of 4138. this is also the defaults and most likely wrong for your thermistor.
                you need to find the correct value, otherwise you are printing at the wrong temperature.

                MJCTundefined 1 Reply Last reply Reply Quote 0
                • MJCTundefined
                  MJCT @Phaedrux
                  last edited by

                  Hi,

                  Somehow, in the middle of all this crisis 400 sp mm transformed in 4000 sp mm. ~

                  The company information was : 1.8 deg (200 steps per rev), Leadscrew, Custom, Pitch 8, Gear ratio 1:1 and finally 400.00 microsteping.

                  When I was using the config tool I’m sure I’ve inputted 400.00, but instead of just clicking with the mouse at another area I probably pressed “Set”, and that reverts the value to the predefined 4000.00.

                  Lousy mistake that costed me dozens of hours and a lot of patience to all of us.

                  That’s why the G30 S-1 was returning values like 0.22... instead of 2.2... It was literally messing everything in the Z axis, tenfold.

                  Its now printing a test cub

                  1 Reply Last reply Reply Quote 0
                  • MJCTundefined
                    MJCT @Veti
                    last edited by

                    @Veti

                    @Veti said in Nozzle gets smashed against the bed:

                    also you have a beta value of 4138. this is also the defaults and most likely wrong for your thermistor.
                    you need to find the correct value, otherwise you are printing at the wrong temperature.

                    Yes, next step

                    jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                    • jay_s_ukundefined
                      jay_s_uk @MJCT
                      last edited by

                      @MJCT

                      We'll get you sorted

                      Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                      1 Reply Last reply Reply Quote 0
                      • MJCTundefined
                        MJCT
                        last edited by

                        The test cub printed just fine for a first print.

                        Once again, thank you all for your help.

                        fcwiltundefined 1 Reply Last reply Reply Quote 0
                        • fcwiltundefined
                          fcwilt @MJCT
                          last edited by

                          @MJCT said in Nozzle gets smashed against the bed:

                          The test cub printed just fine for a first print.

                          Once again, thank you all for your help.

                          Hi,

                          Glad you got it working.

                          Remember in the future that one of the tests you should make is to use the DWC to jog the axes a known amount and verify with a measuring device that the movement was correct.

                          Frederick

                          Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

                          MJCTundefined 1 Reply Last reply Reply Quote 0
                          • MJCTundefined
                            MJCT @fcwilt
                            last edited by

                            @fcwilt
                            Iep I understand that, and I did it, but because de dashboard buttons don’t indicate units, they just say "Z-5" for example, I made the mistake.

                            When that button was pressed, the Z axis moved exactly 5 cm which I confirmed as accurate with a tool (not 5mm as it should). But I was so angry and confused that I didn’t notice that the behaviour of the X and Y axis was different. For those the equivalent button only moved 5mm.

                            1 Reply Last reply Reply Quote 1
                            • First post
                              Last post
                            Unless otherwise noted, all forum content is licensed under CC-BY-SA