Duet 3 - Motors only respond properly duing the home command
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could you please show an screenshot which button you press and tell me what movement the printer does exactly? (the jog which does not work)
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@Oliver3d the Z bottoms seem to do nothing, Y bottoms seem to move the motors very slowly, X bottoms seem to work better but its hard to tell if its 100% correct as I think more than one motor should be activated to create the correct movement in ether X of Y axis
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At the PanelDue those buttons did not work sometimes, so I prefer movement in the command line at the top. Could you try G91 and then G1 Z-100 etc. at the command line?
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@JoergS5 none
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or better with slow speed:
G91
G1 Z-100 F100
G1 X100 F100(did you try lowing current and speed? I configured a 2A stepper for 4 A and it stopped moving totally)
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@JoergS5 I trying typing in the Gcode and the DWC thinks its moving the motors and instantly changes the Z to 0.00 but nothing moves on the printer
M114
X:0.000 Y:0.000 Z:0.000 E:0.000 E0:0.0 Count 11500655 11500655 11500655 Machine 0.000 0.000 0.000 Bed comp 0.000 -
I know what David would say now: please make M122 and show the report...
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M122
=== Diagnostics ===
RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v0.6 or 1.0 (standalone mode)
Board ID: 08DJM-956L2-G43S4-6JTDJ-3SJ6L-9866G
Used output buffers: 1 of 40 (17 max)
=== RTOS ===
Static ram: 154604
Dynamic ram: 161668 of which 56 recycled
Exception stack ram used: 528
Never used ram: 76360
Tasks: NETWORK(ready,356) ETHERNET(blocked,424) HEAT(blocked,1192) CanReceiv(suspended,3820) CanSender(suspended,1420) CanClock(blocked,1424) TMC(blocked,60) MAIN(running,4528) IDLE(ready,76)
Owned mutexes:
=== Platform ===
Last reset 00:37:42 ago, cause: software
Last software reset at 2020-05-30 11:47, reason: User, spinning module GCodes, available RAM 76360 bytes (slot 0)
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
Error status: 0
MCU temperature: min 40.2, current 40.9, max 41.0
Supply voltage: min 11.0, current 11.2, max 11.4, under voltage events: 0, over voltage events: 0, power good: yes
12V rail voltage: min 10.3, current 10.5, max 10.7, under voltage events: 0
Driver 0: standstill, reads 24358, writes 45 timeouts 0, SG min/max 0/538
Driver 1: standstill, reads 24361, writes 45 timeouts 0, SG min/max 0/533
Driver 2: standstill, reads 24361, writes 45 timeouts 0, SG min/max 0/512
Driver 3: standstill, reads 24394, writes 14 timeouts 0, SG min/max 0/0
Driver 4: standstill, reads 24397, writes 11 timeouts 0, SG min/max 0/0
Driver 5: standstill, reads 24399, writes 11 timeouts 0, SG min/max 0/0
Date/time: 2020-05-30 12:25:06
Slowest loop: 78.72ms; fastest: 0.22ms
=== Storage ===
Free file entries: 10
SD card 0 detected, interface speed: 25.0MBytes/sec
SD card longest read time 3.5ms, write time 36.7ms, max retries 0
=== Move ===
Hiccups: 39690(0), FreeDm: 375, MinFreeDm: 369, MaxWait: 858529ms
Bed compensation in use: none, comp offset 0.000
=== MainDDARing ===
Scheduled moves: 67, completed moves: 67, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
=== AuxDDARing ===
Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
=== Heat ===
Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
=== GCodes ===
Segments left: 0
Movement lock held by null
HTTP is idle in state(s) 0
Telnet is idle in state(s) 0
File is idle in state(s) 0
USB is idle in state(s) 0
Aux is idle in state(s) 0
Trigger is idle in state(s) 0
Queue is idle in state(s) 0
LCD is idle in state(s) 0
SBC is idle in state(s) 0
Daemon is idle in state(s) 0
Aux2 is idle in state(s) 0
Autopause is idle in state(s) 0
Code queue is empty.
=== Network ===
Slowest loop: 148.97ms; fastest: 0.03ms
Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
HTTP sessions: 2 of 8- Ethernet -
State: active
Error counts: 0 0 0 0 0
Socket states: 5 2 2 2 2 0 0 0
=== CAN ===
Messages sent 9060, longest wait 0ms for type 0
=== Linux interface ===
State: 0, failed transfers: 0
Last transfer: 2262962ms ago
RX/TX seq numbers: 0/1
SPI underruns 0, overruns 0
Number of disconnects: 0
Buffer RX/TX: 0/0-0
- Ethernet -
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I don't see errors, but I am not an M122 expert.
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@Oliver3d said in Duet 3 - Motors only respond properly duing the home command:
12V rail voltage: min 10.3, current 10.5, max 10.7, under voltage events: 0
12V rail voltage: min 10.3, current 10.5, max 10.7, under voltage events: 0 is near your limit of 10 V, but it was not lower than 10 limit of
M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
Do you have a good enough power supply? -
@JoergS5 I have 40amp at 12v
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but M122 reported only 11 V, if you have a PSU MeanWell or similar, there is a potentiometer where you can set voltate higher or lower (better all power turned off when you change it). I don't think this is the reason, but to exclude it from the list...
https://duet3d.dozuki.com/Wiki/Duet_3_Mainboard_6HC_Hardware_Overview says 12 V:
VIN in the range 12V-32V must be provided to the Duet. ...I don't know how strict this must be fulfilled.
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@JoergS5 I adjusted the voltage up to 12.6 measured at the supply voltage terminals of the Duet board
M122
=== Diagnostics ===
RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v0.6 or 1.0 (standalone mode)
Board ID: 08DJM-956L2-G43S4-6JTDJ-3SJ6L-9866G
Used output buffers: 1 of 40 (14 max)
=== RTOS ===
Static ram: 154604
Dynamic ram: 161668 of which 56 recycled
Exception stack ram used: 528
Never used ram: 76360
Tasks: NETWORK(ready,356) ETHERNET(blocked,436) HEAT(blocked,1200) CanReceiv(suspended,3820) CanSender(suspended,1432) CanClock(blocked,1436) TMC(blocked,192) MAIN(running,4528) IDLE(ready,76)
Owned mutexes:
=== Platform ===
Last reset 00:01:15 ago, cause: power up
Last software reset at 2020-05-30 11:47, reason: User, spinning module GCodes, available RAM 76360 bytes (slot 0)
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
Error status: 0
MCU temperature: min 31.7, current 40.2, max 40.3
Supply voltage: min 12.4, current 12.7, max 12.8, under voltage events: 0, over voltage events: 0, power good: yes
12V rail voltage: min 11.7, current 12.0, max 12.1, under voltage events: 0
Driver 0: standstill, reads 28910, writes 17 timeouts 0, SG min/max 0/506
Driver 1: standstill, reads 28911, writes 17 timeouts 0, SG min/max 0/513
Driver 2: standstill, reads 28911, writes 17 timeouts 0, SG min/max 0/535
Driver 3: standstill, reads 28915, writes 14 timeouts 0, SG min/max 0/0
Driver 4: standstill, reads 28919, writes 11 timeouts 0, SG min/max 0/0
Driver 5: standstill, reads 28919, writes 11 timeouts 0, SG min/max 0/0
Date/time: 2020-05-30 12:47:39
Slowest loop: 128.05ms; fastest: 0.22ms
=== Storage ===
Free file entries: 10
SD card 0 detected, interface speed: 25.0MBytes/sec
SD card longest read time 7.2ms, write time 0.0ms, max retries 0
=== Move ===
Hiccups: 27374(0), FreeDm: 375, MinFreeDm: 372, MaxWait: 11975ms
Bed compensation in use: none, comp offset 0.000
=== MainDDARing ===
Scheduled moves: 25, completed moves: 25, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
=== AuxDDARing ===
Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
=== Heat ===
Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
=== GCodes ===
Segments left: 0
Movement lock held by null
HTTP is idle in state(s) 0
Telnet is idle in state(s) 0
File is idle in state(s) 0
USB is idle in state(s) 0
Aux is idle in state(s) 0
Trigger is idle in state(s) 0
Queue is idle in state(s) 0
LCD is idle in state(s) 0
SBC is idle in state(s) 0
Daemon is idle in state(s) 0
Aux2 is idle in state(s) 0
Autopause is idle in state(s) 0
Code queue is empty.
=== Network ===
Slowest loop: 97.18ms; fastest: 0.03ms
Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
HTTP sessions: 2 of 8- Ethernet -
State: active
Error counts: 0 0 0 0 0
Socket states: 2 2 2 2 2 0 0 0
=== CAN ===
Messages sent 304, longest wait 0ms for type 0
=== Linux interface ===
State: 0, failed transfers: 0
Last transfer: 75770ms ago
RX/TX seq numbers: 0/1
SPI underruns 0, overruns 0
Number of disconnects: 0
Buffer RX/TX: 0/0-0
- Ethernet -
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And now it's working all ok?
( sorry, ) -
@JoergS5 I wish it was that easy.
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One last idea today: please put in to the command line: M669 and validate that type is Delta (K3).
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M669
Kinematics is Linear delta