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    CNC Duet 3 DWC Homing button error.

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    • Max3Dundefined
      Max3D
      last edited by

      I cannot seem to find anything related to the G28 homing error I receive when I attempt to use the homing buttons on the DWC. The macros work fine after boot making the DWC buttons turn blue (I placed the M564 H0 code in the config file). Endstops and soft limits on the axes are working fine, no hard crashes, etc...

      After moving all the axes to various positions and attempting to use the DWC blue homing buttons I receive a G28 error and the axis returns to a yellow "not homed" status. What am I doing wrong or is this normal for CNC mode?

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      • jay_s_ukundefined
        jay_s_uk
        last edited by

        @Max3D you'd be best off posting a copy of your config.g and all your homing files (homall.g, homex,g, homey.g and homez.g)

        Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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        • Max3Dundefined
          Max3D
          last edited by

          The issue is related to the DWC's homing buttons on the dashboard that change color indicating the status of the axes. Does the DWC homing buttons reference my macros? I guess what I am looking for is a point of reference where the DWC looks at the config in indicating homing status for all axes or can I edit the DWC's gcode for the buttons...

          Phaedruxundefined 1 Reply Last reply Reply Quote 0
          • Max3Dundefined
            Max3D
            last edited by

            Here is my config.g

            ; Configuration file for Duet 3 (firmware version 3)
            ; executed by the firmware on start-up
            ;
            ; generated by RepRapFirmware Configuration Tool v3.1.4 on Wed Jul 29 2020 15:25:39 GMT-0700 (Pacific Daylight Time)
            
            ; General preferences
            M453			       					; CNC Mode
            G90                            			; send absolute coordinates...
            M83                            			; ...but relative extruder moves
            M550 P"Duet 3"                 			; set printer name
            M564 H0									; Allow axis movement before homing
            
            ; Drives
            M569 P0.2 S1                   			; physical drive 0.2 goes forwards
            M569 P0.0 S0                   			; physical drive 0.0 goes backwards Y axis right
            M569 P0.1 S0                   			; physical drive 0.1 goes backwards Y axis left
            M569 P0.3 S1                   			; physical drive 0.3 goes forwards
            M584 X0.2 Y0.0:0.1 Z0.3 E0.4:0.5:0.6 	; set drive mapping
            M350 X16 Y16 Z16 U16 I1        			; configure microstepping with interpolation U=dummy Y axis
            M92 X400.00 Y400.00 Z400.00      		; set steps per mm
            M566 X900.00 Y900.00 Z12.00    			; set maximum instantaneous speed changes (mm/min)
            M203 X2000.00 Y2000.00 Z500.00 			; set maximum speeds (mm/min)
            M201 X500.00 Y500.00 Z20.00    			; set accelerations (mm/s^2)
            M906 X3000 Y3000 Z3000 I30     			; set motor currents (mA) and motor idle factor in per cent
            M84 S30                        			; Set idle timeout
            
            ; Axis Limits
            M208 X0 Y0 Z0 S1               			; set axis minima
            M208 X500 Y400 Z70 S0          			; set axis maxima
            
            ; Endstops
            M574 X2 S1 P"!^io0.in"         			; configure active-high endstop for high end on X via pin !^io0.in
            M574 Y1 S1 P"!^io1.in"         			; configure active-high endstop for low end on Y via pin !^io1.in
            M574 Z2 S1 P"!^io2.in"         			; configure active-high endstop for high end on Z via pin !^io2.in
            
            ; Z-Probe
            M558 P0 H5 F120 T6000          			; disable Z probe but set dive height, probe speed and travel speed
            M557 X15:215 Y15:195 S20       			; define mesh grid
            
            ; Heaters
            
            ; Fans
            M950 F0 C"out7" Q500           			; create fan 0 on pin out7 and set its frequency
            M106 P0 S1 H-1                 			; set fan 0 value. Thermostatic control is turned off
            M950 F1 C"out8" Q500           			; create fan 1 on pin out8 and set its frequency
            M106 P1 S1 H-1                 			; set fan 1 value. Thermostatic control is turned off
            
            ;Tools
            
            ; Custom settings are not defined
            
            
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            • Phaedruxundefined
              Phaedrux Moderator @Max3D
              last edited by

              @Max3D said in CNC Duet 3 DWC Homing button error.:

              Does the DWC homing buttons reference my macros?

              Yes. Please post the files @jay_s_uk asked for.

              Z-Bot CoreXY Build | Thingiverse Profile

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              • Max3Dundefined
                Max3D
                last edited by

                All the homing files...

                code_t; homeall.g
                ; called to home all axes
                ;
                ; generated by RepRapFirmware Configuration Tool v3.1.4 on Wed Jul 29 2020 15:25:39 GMT-0700 (Pacific Daylight Time)
                G91                     ; relative positioning
                G1 H2 Z5 F1000          ; lift Z relative to current position
                G1 H1 X500 Y-400 F1000  ; move quickly to X and Y axis endstops and stop there (first pass)
                G1 H2 X-5 Y5 F1000      ; go back a few mm
                G1 H1 X500 Y-400 F500   ; move slowly to X and Y axis endstops once more (second pass)
                G1 H1 Z70 F500          ; move Z up stopping at the endstop
                G90                     ; absolute positioning
                G92 Z70                 ; set Z position to axis maximum (you may want to adjust this)
                
                ; Uncomment the following lines to lift Z after probing
                ;G91                    ; relative positioning
                ;G1 Z5 F100             ; lift Z relative to current position
                ;G90                    ; absolute positioning
                
                
                
                ; homex.g
                ; called to home the X axis
                ;
                ; generated by RepRapFirmware Configuration Tool v3.1.4 on Wed Jul 29 2020 15:25:39 GMT-0700 (Pacific Daylight Time)
                G91              ; relative positioning
                G1 H2 Z5 F1000   ; lift Z relative to current position
                G1 H1 X500 F1000 ; move quickly to X axis endstop and stop there (first pass)
                G1 H2 X-10 F1000   ; go back a few mm
                G1 H1 X500 F500  ; move slowly to X axis endstop once more (second pass)
                G1 H2 Z-5 F1000  ; lower Z again
                G90              ; absolute positioning
                
                
                
                ; homey.g
                ; called to home the Y axis
                ;
                ; generated by RepRapFirmware Configuration Tool v3.1.4 on Wed Jul 29 2020 15:25:40 GMT-0700 (Pacific Daylight Time)
                G91                ; relative positioning
                G1 H2 Z5 F1000     ; lift Z relative to current position
                G1 H1 Y-400 F1000  ; move quickly to Y axis endstop and stop there (first pass)
                G1 H2 Y10 F1000    ; go back a few mm
                G1 H1 Y-400 F500   ; move slowly to Y axis endstop once more (second pass)
                G1 H2 Z-5 F1000    ; lower Z again
                G90                ; absolute positioning
                
                
                
                ; homez.g
                ; called to home the Z axis
                ;
                ; generated by RepRapFirmware Configuration Tool v3.1.4 on Wed Jul 29 2020 15:25:40 GMT-0700 (Pacific Daylight Time)
                G91             ; relative positioning
                G1 H2 Z5 F1000  ; lift Z relative to current position
                G1 H1 Z70 F500  ; move Z up until the endstop is triggered
                G1 H2 Z-5 F500 ; move Z back a few mm
                G1 H1 Z70 F500  ; move Z up until the endstop is triggered
                G92 Z70         ; set Z position to axis maximum (you may want to adjust this)
                
                ; Uncomment the following lines to lift Z after probing
                ;G91            ; relative positioning
                ;G1 Z5 F100     ; lift Z relative to current position
                ;G90            ; absolute positioning
                
                
                
                ext
                
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                • jay_s_ukundefined
                  jay_s_uk
                  last edited by

                  @Max3D Your homing files look fine.
                  If you press the homing buttons once they are homed, they will turn from yellow to blue until the axis rehomes again.

                  If you press the buttons, does that axis successfully rehome?
                  I would also not be including M564 H0 in your config file

                  Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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                  • Max3Dundefined
                    Max3D
                    last edited by

                    I removed the m564 H0, and reset after saving config.g. Went to dashboard and hit the 'Home All' button then received the pink dialog with the "G28 Error: Homing failed".

                    Ran the 'Home All' macro successfully with DWC responding with color change to blue on all axes, then hit the 'Home X' DWC button and then received the pink dialog with the "G28 X Error: Homing failed". DWC 'HOME X' button now yellow and the yellow banner stating: "! The following axis is not homed X".

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                    • jay_s_ukundefined
                      jay_s_uk
                      last edited by

                      Does the x axis move at all when you try to home it?
                      Have you checked the statuses of your endstops to ensure they show as triggered or not correctly?

                      Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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                      • Max3Dundefined
                        Max3D
                        last edited by

                        Nothing on the axis (no stepper movement). Endstops are triggered when homed and not when spindle is in the middle of the bed.

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                        • A Former User?
                          A Former User
                          last edited by

                          homeall.g and g28 x doesn't do the same thing, homeall.g and g28 does.

                          can you run your homex.g macro without errors?

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                          • Max3Dundefined
                            Max3D
                            last edited by

                            Just ran homex.g macro from the all axes homed position, homex.g ran without error and axis re-homed.

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                            • jay_s_ukundefined
                              jay_s_uk
                              last edited by

                              @Max3D so what did you do differently than your earlier post at 07:10? as what failed that time seems to have worked this time

                              Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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                              • Max3Dundefined
                                Max3D
                                last edited by

                                To try and simplify this... First time I used the Home all button and the homeall.g. Then I used the Home X button followed by the homex.g.

                                Every time I used the DWC buttons I receive the G28 error dialog box in the lower right of the browser screen with no machine movement.

                                Every time I use the macros (anyone) the axis homes and the status of the DWC buttons change from yellow to blue or stay blue.

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                                • Max3Dundefined
                                  Max3D
                                  last edited by

                                  Maybe this can help. I recently had to erase the firmware and flash from the RaspPi (mod 4 8gig) with bossac because the new Duet 3 board had some kind of early release bug that would execute the comments in the config,g as code and would not allow the sudo apt get update/upgrade to alter the firmware (currently running latest release downloaded in the last 10 days). I am running the CNC's DWC with monitor and input devices directly connected to the Pi, and not from any laptop connected to my home network.

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                                  • Phaedruxundefined
                                    Phaedrux Moderator
                                    last edited by

                                    Can you send M122 in the gcode console and post the results here?

                                    Also please check the version of DWC from the settings tab.

                                    Firmware and DWC should both be at 3.1.1

                                    G28 = homeall.g = home all button in dwc
                                    G28 x = homex.g = home x button in dwc
                                    etc, etc

                                    When you click the button in the DWC it marks the axis as unhommed and then tries to execute the commands in the macro to rehome. If it fails to do that for some reason you get left with an unhomed axis.

                                    Z-Bot CoreXY Build | Thingiverse Profile

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                                    • Max3Dundefined
                                      Max3D
                                      last edited by

                                      As I stated in my last reply. I did a sudo apt get update & upgrade from the RaspPi within the last 10 days. This is a new build. The board had a known firmware bug (beta release 12 or something to that affect) from what I have read here in the forum. The board would not detect the endstops when powered by usb during initial setup either, so I erased the board and then did flashed it with the RaspPi. DWC is at 3.1.1. and below are the diags from the M122. IF the board is glitchy then I need to have it replaced. I can't lose any more time on a bad board...

                                      03/09/2020, 12:44:42 Connected to duet3
                                      03/09/2020, 12:45:08 M122
                                      === Diagnostics ===
                                      RepRapFirmware for Duet 3 MB6HC version 3.1.1 running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode)
                                      Board ID: 08DJM-956L2-G43S8-6JTDA-3SJ6T-1B0AH
                                      Used output buffers: 1 of 40 (11 max)
                                      === RTOS ===
                                      Static ram: 154604
                                      Dynamic ram: 161808 of which 52 recycled
                                      Exception stack ram used: 224
                                      Never used ram: 76528
                                      Tasks: NETWORK(ready,1972) HEAT(blocked,1416) CanReceiv(suspended,3820) CanSender(suspended,1488) CanClock(blocked,1452) TMC(blocked,204) MAIN(running,5056) IDLE(ready,76)
                                      Owned mutexes:
                                      === Platform ===
                                      Last reset 00:01:27 ago, cause: power up
                                      Last software reset at 2020-09-02 22:57, reason: User, spinning module LinuxInterface, available RAM 76528 bytes (slot 3)
                                      Software reset code 0x0010 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0444a000 BFAR 0x00000000 SP 0xffffffff Task MAIN
                                      Error status: 0
                                      MCU temperature: min 25.8, current 33.5, max 33.6
                                      Supply voltage: min 19.5, current 24.1, max 24.5, under voltage events: 0, over voltage events: 0, power good: yes
                                      12V rail voltage: min 12.2, current 12.2, max 12.3, under voltage events: 0
                                      Driver 0: standstill, reads 35617, writes 14 timeouts 0, SG min/max 0/0
                                      Driver 1: standstill, reads 35617, writes 14 timeouts 0, SG min/max 0/0
                                      Driver 2: standstill, reads 35617, writes 14 timeouts 0, SG min/max 0/0
                                      Driver 3: standstill, reads 35618, writes 14 timeouts 0, SG min/max 0/0
                                      Driver 4: standstill, reads 35621, writes 11 timeouts 0, SG min/max 0/0
                                      Driver 5: standstill, reads 35622, writes 11 timeouts 0, SG min/max 0/0
                                      Date/time: 2020-09-03 12:45:07
                                      Slowest loop: 4.42ms; fastest: 0.14ms
                                      === Storage ===
                                      Free file entries: 10
                                      SD card 0 detected, interface speed: 25.0MBytes/sec
                                      SD card longest read time 2.5ms, write time 0.0ms, max retries 0
                                      === Move ===
                                      Hiccups: 0(0), FreeDm: 375, MinFreeDm: 375, MaxWait: 0ms
                                      Bed compensation in use: none, comp offset 0.000
                                      === MainDDARing ===
                                      Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                                      === AuxDDARing ===
                                      Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
                                      === Heat ===
                                      Bed heaters = -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                      === GCodes ===
                                      Segments left: 0
                                      Movement lock held by null
                                      HTTP* is ready with "M122" in state(s) 0
                                      Telnet is idle in state(s) 0
                                      File is idle in state(s) 0
                                      USB is idle in state(s) 0
                                      Aux is idle in state(s) 0
                                      Trigger* is idle in state(s) 0
                                      Queue is idle in state(s) 0
                                      LCD is idle in state(s) 0
                                      SBC is idle in state(s) 0
                                      Daemon* is idle in state(s) 0
                                      Aux2 is idle in state(s) 0
                                      Autopause is idle in state(s) 0
                                      Code queue is empty.
                                      === Network ===
                                      Slowest loop: 0.97ms; fastest: 0.01ms
                                      Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                                      HTTP sessions: 0 of 8

                                      • Ethernet -
                                        State: disabled
                                        Error counts: 0 0 0 0 0
                                        Socket states: 0 0 0 0 0 0 0 0
                                        === CAN ===
                                        Messages sent 0, longest wait 0ms for type 0
                                        === Linux interface ===
                                        State: 0, failed transfers: 0
                                        Last transfer: 16ms ago
                                        RX/TX seq numbers: 1822/1823
                                        SPI underruns 0, overruns 0
                                        Number of disconnects: 0
                                        Buffer RX/TX: 0/0-0
                                        === Duet Control Server ===
                                        Duet Control Server v3.1.1
                                        Code buffer space: 4096
                                        Configured SPI speed: 8000000 Hz
                                        Full transfers per second: 0.04
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                                      • Phaedruxundefined
                                        Phaedrux Moderator
                                        last edited by Phaedrux

                                        Please bare with us while we troubleshoot your issue. If we send you a new board, but the problem is in the configuration, we didn't save you any time at all, because no problem was solved.

                                        Now I'm having some difficulty understanding the issue exactly.

                                        You say the endstops are working fine, but trying to home produces an error. How have you verified that the endstops are working if you can't home?

                                        If you go to the machine specific settings tab in DWC where the endstop status is displayed, does the status change when you manually trigger the endstops by hand?

                                        We need to verify that the endstop config is correct.

                                        ; Endstops
                                        M574 X2 S1 P"!^io0.in"         			; configure active-high endstop for high end on X via pin !^io0.in
                                        M574 Y1 S1 P"!^io1.in"         			; configure active-high endstop for low end on Y via pin !^io1.in
                                        M574 Z2 S1 P"!^io2.in"         			; configure active-high endstop for high end on Z via pin !^io2.in
                                        

                                        When you send G28 (or push the home all button in DWC) how much movement do you get? At what point does the error occur?

                                        Also, can you send M98 P"config.g" in the console and report the results here?

                                        Z-Bot CoreXY Build | Thingiverse Profile

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                                        • Max3Dundefined
                                          Max3D
                                          last edited by

                                          I am able to home using the macros, All, X, Y, and Z. The steppers start pushing the axes and the homing code executes the bump and rebump in beautiful harmony. When I use the macros the DWC's homing buttons turn from yellow to blue (all is well and dandy).

                                          I can move the spindle around the bed with the buttons on the DWC's dashboard in the "Machine Movement" section using the "(x,y,z)+/-50" on all axes. I can test the soft limits on the axis and will receive an error when I try to go beyond the config.g settings (X=500 Y=400 and Z+70).

                                          Using the macros, I can home an individual axis and then rehome without failure or any error code. When all the axes are homed I can see all the limit switches are lit with a red LED indicating they are triggered. I can go to the "machine specific" section of the DWC and verify that the endstops are triggered. Using the macros, I can rehome all day long without an error and each time the axes will do that beautiful bump and rebump, endstops lit up.

                                          BUT, whenever I try to use the DWC homing buttons (whether they are yellow or blue), I get the cute little pink dialog box with the dreaded "G28 Error: Homing failed" and the button turns yellow; not a peep out of the steppers. I go to the top of the dashboard page and type G28 and hit the send button and I get the same cute little G28 Error: Homing failed; steppers idling. It does not matter which DWC button (or G28 I send from the console) I use, the only thing that happens is the error dialog box (All = G28 Error:, X=G28 X Error:, Y=G28 Y Error:, Z=G28 Z Error:) and the button turns yellow. It is consistent no matter how many times I reboot, power down, or rest the after saving config.g.

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                                          • Max3Dundefined
                                            Max3D
                                            last edited by

                                            Sorry... The M98 P"config.g" returns "M98 P"config.g"" in the console.

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