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    Tool board LC1 errors

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    • Phaedruxundefined
      Phaedrux Moderator @JayJay
      last edited by

      @JayJay said in Tool board LC1 errors:

      Error: G31: Invalid Z probe index Error: M558: Pin 121.io0.in is not free Warning: Board 121 does not have input handle 3000

      When do you get these error messages popping up?

      Z-Bot CoreXY Build | Thingiverse Profile

      JayJayundefined 1 Reply Last reply Reply Quote 0
      • JayJayundefined
        JayJay @Phaedrux
        last edited by

        @Phaedrux said in Tool board LC1 errors:

        @JayJay said in Tool board LC1 errors:

        Error: G31: Invalid Z probe index Error: M558: Pin 121.io0.in is not free Warning: Board 121 does not have input handle 3000

        When do you get these error messages popping up?

        At First boot then they dissappear, but i just updated the toolboard firmware and I think they have dissappeared for good now, so it seems like it is just the heater fault to overcome before I can even think about attempting to make it move.

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        • Phaedruxundefined
          Phaedrux Moderator @JayJay
          last edited by

          @JayJay said in Tool board LC1 errors:

          Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C

          https://duet3d.dozuki.com/Wiki/FAQ#Section_M307_Heater_1_appears_to_be_over_powered_If_left_on_at_full_power_its_temperature_is_predicted_to_reach_521C

          It's a warning.

          Z-Bot CoreXY Build | Thingiverse Profile

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          • A Former User?
            A Former User @Phaedrux
            last edited by

            @Phaedrux said in Tool board LC1 errors:

            @JayJay said in Tool board LC1 errors:

            Warning: M307: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C

            https://duet3d.dozuki.com/Wiki/FAQ#Section_M307_Heater_1_appears_to_be_over_powered_If_left_on_at_full_power_its_temperature_is_predicted_to_reach_521C

            It's a warning.

            The guy says his issue is with H1 showing as a fault and the temperature reading is showing to be Incorrect in DWC, surely the fact that H0 is over powered is a secondary issue at this point?

            Unless if course its H0 that has the fault and not H1.

            So to confirm: which one do you have a problem with the temperature display on

            H0= The heated bed?
            OR
            H1= The hot end

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            • Phaedruxundefined
              Phaedrux Moderator @A Former User
              last edited by

              @CaLviNx surely you see that adding T100000 to his thermistor setting should correct the erroneously high temp reading.

              Z-Bot CoreXY Build | Thingiverse Profile

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              • A Former User?
                A Former User @Phaedrux
                last edited by

                @Phaedrux said in Tool board LC1 errors:

                @CaLviNx surely you see that adding T100000 to his thermistor setting should correct the erroneously high temp reading.

                I'm not disagreeing with you but the guy quite clearly pointed out that, he had tried it with T100000 inserted and that had no effect, so unless the guy is lying the problem lies elsewhere and I fail to see the point in following up about the other heater being over powered instead of concentrating on the guys actual issue.

                dc42undefined 1 Reply Last reply Reply Quote 1
                • dc42undefined
                  dc42 administrators @A Former User
                  last edited by

                  @CaLviNx said in Tool board LC1 errors:

                  I'm not disagreeing with you but the guy quite clearly pointed out that, he had tried it with T100000 inserted and that had no effect

                  The default is T100000, so indeed adding T100000 should have no effect.

                  @JayJay, are you certain that the temperature sensor in your hot end is thermistor, not a PT100, and it is not shorted out or shorting to the hot end metalwork?

                  Duet WiFi hardware designer and firmware engineer
                  Please do not ask me for Duet support via PM or email, use the forum
                  http://www.escher3d.com, https://miscsolutions.wordpress.com

                  JayJayundefined 1 Reply Last reply Reply Quote 1
                  • JayJayundefined
                    JayJay @dc42
                    last edited by JayJay

                    @dc42 said in Tool board LC1 errors:

                    @JayJay, are you certain that the temperature sensor in your hot end is thermistor, not a PT100, and it is not shorted out or shorting to the hot end metalwork?

                    Thank you for the reply and kind assistance.

                    Yes the sensor is 100% a thermistor it is shielded in grp sheathing around the hotend etc.

                    But I think I may have a faulty toolboard, as I moved the very same sensor from "temp0" to "temp1" and changed the config.g to:

                    M308 S1 P"121.temp1" Y"thermistor" B4725 C7.06e-8

                    And now the temp is reading correct and the same as the bed temp (when at room temp)

                    But I now receive the following error message as soon as I try to home X :

                    Warning: motor phase B may be disconnected reported by driver(s) 0
                    Warning: motor phase A may be disconnected reported by driver(s) 0

                    Driver0 is where the extruder motor is mapped to and i checked the wires to find the base pairs with a meter and located them in the plug accordingly, the only thing that could be wrong there is that the motor might round the wrong way but why DWC is now reporting Driver0 as being disconnected when i home X is beyond me.

                    This is my home X, Y & Z files

                    Home X

                    ; homex.g
                    ;
                    ; called to home the X axis
                    ;
                    G91                     ; Switch to relative positioning moves
                    G1 H2 Z5 F6000          ; Drop the Z axis (the bed) by 5mm relative to it's current position
                    G1 H1 X-350 F3000       ; Fast travel the X axis close to it's endstop & stop 
                    G1 H2 X5 F6000          ; Move the X axis back by 5mm
                    G1 H1 X-350 F240        ; Slow travel the X axis until it triggers it's endstop
                    G1 H2 Z5 F1000          ; Drop the Z axis (the bed) by 5mm relative to it's current position
                    G90                     ; Revert back to absolute positioning moves
                    

                    Home Y

                    ; homey.g
                    ;
                    ; called to home the Y axis
                    ;
                    G91                     ; Switch to relative positioning
                    G1 H2 Z5 F6000          ; Drop the Z axis (the bed) by 5mm relative to it's current position
                    G1 H1 Y-350 F3000       ; Fast travel the Y axis close to it's endstop & stop
                    G1 H2 Y5 F3000          ; Move the Y axis away from it's endstop by 5mm
                    G1 H1 Y-350 F240        ; Slow travel the X axis until it triggers it's endstop
                    G1 H2 Z-5 F1000         ; Drop the Z axis (the bed) by 5mm relative to it's current position away from the nozzle
                    G90                     ; Revert back to absolute positioning
                    

                    Home Z

                    ; homez.g
                    ;
                    ; called to home the Z axis
                    ;
                    G91                     ; Switch to relative positioning moves
                    G1 H2 Z5 F6000          ; Drop the Z axis (the bed) by 5mm relative to it's current position
                    G1 H1 Z-350 F3000       ; Fast travel the Z axis (the bed) up closer to it's endstop & stop
                    G1 H2 Z5 F1500          ; Move the Z axis (the bed) away from the IR probe by 5mm 
                    G1 H1 Z-350 F240        ; Slow travel the Z axis (the bed) until it triggers the IR Sensor
                    G91                     ; Switch to relative positioning moves
                    G1 Z5 F1000             ; Drop the Z axis (the bed) by 5mm relative to it's current position away from the nozzle
                    G90                     ; Revert back to absolute positioning moves
                    
                    A Former User? 1 Reply Last reply Reply Quote 0
                    • A Former User?
                      A Former User @JayJay
                      last edited by

                      @JayJay

                      Your drive mapping M584 is in conflict with what you have in your M569

                      in M584 you have

                      M584 X0.0 Y0.1 Z0.3:0.4:0.5 
                      

                      But in M569

                      You have the following

                      M569 P121.0 S1                                                  ; Driver 121.0 is connected to the extruder motor output (Driver 0) on the toolboard LC1 & goes forwards
                      M569 P0.1 S1                                                    ; Driver 0.1 is connected to the Z1 axis motor (Front Left) on the mainboard 6HC & goes forwards
                      M569 P0.2 S1                                                    ; Driver 0.2 is connected to the Z2 axis motor (Front Right) on the mainboard 6HC & goes forwards
                      M569 P0.3 S1                                                    ; Driver 0.3 is connected to the Z3 axis motor (Centre Rear) on the mainboard 6HC & goes forwards
                      M569 P0.4 S1                                                    ; Driver 0.4 is connected to the X axis motor on the mainboard 6HC & goes forwards
                      M569 P0.5 S1                                                    ; Driver 0.5 is connected to the Y axis motor on the mainboard 6HC & goes forwards
                      

                      so you need to fix either one or the other to match how you have it wired

                      JayJayundefined 1 Reply Last reply Reply Quote 2
                      • JayJayundefined
                        JayJay @A Former User
                        last edited by

                        @CaLviNx said in Tool board LC1 errors:

                        so you need to fix either one or the other to match how you have it wired

                        @CaLviNx

                        Thank you so very much, an excellent spot, the M569 commands are correct .

                        I have edited M584 to match and that got rid of the driver0 error and everything is now homing. thank you again.

                        please accept my apologies in advance as I will no doubt be back with more rookie questions.

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