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    Duet3 6CH + 3CH expansion board - Missing steps.

    Scheduled Pinned Locked Moved Solved
    Tuning and tweaking
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    • evomotorsundefined
      evomotors @dc42
      last edited by

      @dc42 said in Duet3 6CH + 3CH expansion board - Missing steps.:

      OK, perhaps you were homing between running the first M122 and starting the print?

      I do have G28 Z in bed.g and it's been calling before every print. Let me change that. But I will still need to home somehow.

      1 Reply Last reply Reply Quote 0
      • evomotorsundefined
        evomotors @dc42
        last edited by

        @dc42 Ok , none of my homing files contains G28, it's only in bed. let me remove it and run another test.

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        • evomotorsundefined
          evomotors
          last edited by evomotors

          Restarted the printer:
          @dc42 not sure if it's expected fresh after restart

          Peak sync jitter 13, peak Rx sync delay 176
          

          Full log:

          M122 B1
          Diagnostics for board 1:
          Duet EXP3HC firmware version 3.3beta (2021-01-16 08:18:18)
          Bootloader ID: not available
          Never used RAM 154492, free system stack 200 words
          HEAT 104 CanAsync 92 CanRecv 86 TMC 64 MAIN 282 AIN 259
          Last reset 00:01:26 ago, cause: software
          Last software reset data not available
          Driver 0: position 0, 160.0 steps/mm,  standstill, reads 8690, writes 0 timeouts 0, SG min/max not available, steps req 0 done 0
          Driver 1: position 0, 160.0 steps/mm,  standstill, reads 8689, writes 0 timeouts 0, SG min/max not available, steps req 0 done 0
          Driver 2: position 0, 172.0 steps/mm,  standstill, reads 8689, writes 0 timeouts 0, SG min/max not available, steps req 0 done 0
          Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0
          Peak sync jitter 13, peak Rx sync delay 176, resyncs 0, no step interrupt scheduled
          VIN: 24.7V, V12: 12.3V
          MCU temperature: min 43.8C, current 44.0C, max 44.0C
          Ticks since heat task active 99, ADC conversions started 86340, completed 86340, timed out 0
          Last sensors broadcast 0x00000000 found 0 103 ticks ago, loop time 0
          CAN messages queued 24, send timeouts 0, received 105, lost 0, free buffers 36, error reg 4f
          

          Now will run print

          1 Reply Last reply Reply Quote 0
          • evomotorsundefined
            evomotors
            last edited by evomotors

            @dc42
            No G28 anywhere, no homing moves between M122 commands. And I only ran M122 once after pausing the print. This time I didn't stop, just pause. Still reporting missing steps.

            M122
            === Diagnostics ===
            RepRapFirmware for Duet 3 MB6HC version 3.3beta running on Duet 3 MB6HC v1.01 or later (SBC mode)
            Board ID: 08DJM-956L2-G43S8-6JKDL-3SJ6L-1802G
            Used output buffers: 1 of 40 (12 max)
            === RTOS ===
            Static ram: 149772
            Dynamic ram: 64248 of which 104 recycled
            Never used RAM 140548, free system stack 130 words
            Tasks: Linux(ready,141) HEAT(blocked,299) CanReceiv(blocked,893) CanSender(blocked,346) CanClock(blocked,326) TMC(blocked,52) MAIN(running,655) IDLE(ready,19)
            Owned mutexes: HTTP(MAIN)
            === Platform ===
            Last reset 00:30:20 ago, cause: power up
            Last software reset at 2021-01-16 20:06, reason: MemoryProtectionFault mmarValid daccViol, GCodes spinning, available RAM 140596, slot 1
            Software reset code 0x4163 HFSR 0x00000000 CFSR 0x00000082 ICSR 0x00400804 BFAR 0x00000038 SP 0x204235e8 Task MAIN Freestk 1658 ok
            Stack: 00000000 00000001 00000001 00000000 20423633 0046dd2d 0046d97c 61010000 2042ad78 00000000 00000000 0046dd37 00000000 00000000 3ca3d70a 0000000a 4374da1d 2042b29c 00000000 00000001 00000000 0046d9e7 2042b29c fffc0000 003fffff 0046dd27 00000000
            Error status: 0x00
            Aux0 errors 0,0,0
            Aux1 errors 0,0,0
            MCU temperature: min 35.0, current 37.3, max 37.4
            Supply voltage: min 24.0, current 24.3, max 24.5, under voltage events: 0, over voltage events: 0, power good: yes
            12V rail voltage: min 12.1, current 12.2, max 12.2, under voltage events: 0
            Driver 0: position 79788, standstill, reads 18682, writes 3 timeouts 0, SG min/max 0/240
            Driver 1: position -219, standstill, reads 18682, writes 3 timeouts 0, SG min/max 0/240
            Driver 2: position 1321, standstill, reads 18682, writes 3 timeouts 0, SG min/max 0/240
            Driver 3: position 0, standstill, reads 18682, writes 3 timeouts 0, SG min/max 0/254
            Driver 4: position 0, standstill, reads 18685, writes 0 timeouts 0, SG min/max not available
            Driver 5: position 0, standstill, reads 18684, writes 0 timeouts 0, SG min/max not available
            Date/time: 2021-01-16 20:36:44
            Slowest loop: 183.43ms; fastest: 0.03ms
            === Storage ===
            Free file entries: 10
            SD card 0 not detected, interface speed: 37.5MBytes/sec
            SD card longest read time 0.0ms, write time 0.0ms, max retries 0
            === Move ===
            DMs created 125, maxWait 768639ms, bed compensation in use: mesh, comp offset 0.000
            === MainDDARing ===
            Scheduled moves 13893, completed moves 13893, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 2], CDDA state -1
            === AuxDDARing ===
            Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
            === Heat ===
            Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
            Heater 0 is on, I-accum = 0.4
            Heater 1 is on, I-accum = 0.3
            === GCodes ===
            Segments left: 0
            Movement lock held by null
            HTTP* is doing "M122" in state(s) 0
            Telnet is idle in state(s) 0
            File* is idle in state(s) 0
            USB is idle in state(s) 0
            Aux is idle in state(s) 0
            Trigger* is idle in state(s) 0
            Queue* is idle in state(s) 0
            LCD is idle in state(s) 0
            SBC is idle in state(s) 0
            Daemon is idle in state(s) 0
            Aux2 is idle in state(s) 0
            Autopause is idle in state(s) 0
            Code queue is empty.
            === CAN ===
            Messages queued 20932, send timeouts 0, received 67, lost 0, longest wait 19ms for reply type 6024, peak Tx sync delay 387, free buffers 48
            === SBC interface ===
            State: 4, failed transfers: 0
            Last transfer: 1ms ago
            RX/TX seq numbers: 4299/4299
            SPI underruns 0, overruns 0
            Number of disconnects: 0, IAP RAM available 0x2c478
            Buffer RX/TX: 0/0-0
            === Duet Control Server ===
            Duet Control Server v3.2.0
            Code buffer space: 4096
            Configured SPI speed: 8000000 Hz
            Full transfers per second: 38.79
            Maximum length of RX/TX data transfers: 3032/1688
            File /opt/dsf/sd/gcodes/ZR_BearingTopMount_FR.gcode is selected, paused
            
            M122 B1
            Diagnostics for board 1:
            Duet EXP3HC firmware version 3.3beta (2021-01-16 08:18:18)
            Bootloader ID: not available
            Never used RAM 154492, free system stack 165 words
            HEAT 92 CanAsync 92 CanRecv 86 TMC 30 MAIN 274 AIN 259
            Last reset 00:30:25 ago, cause: software
            Last software reset data not available
            Driver 0: position -252890, 160.0 steps/mm,  standstill, reads 47021, writes 1 timeouts 0, SG min/max 0/431, steps req 4754028 done 4495266
            Driver 1: position 11122, 160.0 steps/mm,  standstill, reads 47021, writes 1 timeouts 0, SG min/max 0/1023, steps req 4516310 done 4257548
            Driver 2: position 43107, 172.0 steps/mm,  standstill, reads 47022, writes 1 timeouts 0, SG min/max 0/609, steps req 146093 done 148150
            Moves scheduled 13764, completed 13764, in progress 0, hiccups 462, step errors 0
            Peak sync jitter 15, peak Rx sync delay 48876, resyncs 16, no step interrupt scheduled
            VIN: 24.7V, V12: 12.3V
            MCU temperature: min 43.8C, current 44.0C, max 44.2C
            Ticks since heat task active 148, ADC conversions started 1825390, completed 1825388, timed out 0
            Last sensors broadcast 0x00000000 found 0 152 ticks ago, loop time 0
            CAN messages queued 43, send timeouts 0, received 29446, lost 76, free buffers 36, error reg 24
            
            1 Reply Last reply Reply Quote 0
            • evomotorsundefined
              evomotors
              last edited by

              By the way, I just got this comment on my YouTube video:
              67344bfb-72fa-4b52-b290-b5d093504a9d-image.png

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              • evomotorsundefined
                evomotors
                last edited by

                @dc42 Ok, I see your point, I added

                M122
                M122 B1
                

                To my startup GCode after all preparation moves. So it will execute just before actual print.

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                • evomotorsundefined
                  evomotors
                  last edited by evomotors

                  @dc42 I added M112 & M112 B1 to the end of my start GCode in slicer then power cycle the printer and started print job.

                  These are all console enrties in chronological order:

                  1/16/2021, 4:25:51 PM
                  Connection established
                  
                  1/16/2021, 4:35:56 PM	
                  M32 "0:/gcodes/2ZR_BearingTopMount_FR.gcode"
                  File 0:/gcodes/2ZR_BearingTopMount_FR.gcode selected for printing
                  
                  1/16/2021, 4:40:20 PM	
                  Leadscrew adjustments made: 0.196 0.148 0.149 0.184, points used 4, (mean, deviation) before (0.167, 0.017) after (0.000, 0.000)
                  
                  1/16/2021, 4:40:20 PM	
                  Bed Leveling Cycle: 1 - Difference was 0.017mm
                  
                  1/16/2021, 4:40:20 PM	
                  Leadscrew adjustments made: 0.005 -0.005 -0.005 -0.007, points used 4, (mean, deviation) before (-0.003, 0.003) after (0.000, 0.000)
                  
                  1/16/2021, 4:40:20 PM	
                  Bed Tramming Cycle: 2 - Difference was 0.003mm
                  
                  1/16/2021, 4:40:20 PM	
                  Height map loaded from file heightmap.csv
                  
                  1/16/2021, 4:40:46 PM	
                  === Diagnostics ===
                  RepRapFirmware for Duet 3 MB6HC version 3.3beta running on Duet 3 MB6HC v1.01 or later (SBC mode)
                  Board ID: 08DJM-956L2-G43S8-6JKDL-3SJ6L-1802G
                  Used output buffers: 1 of 40 (10 max)
                  === RTOS ===
                  Static ram: 149772
                  Dynamic ram: 64248 of which 104 recycled
                  Never used RAM 140548, free system stack 126 words
                  Tasks: Linux(ready,111) HEAT(blocked,299) CanReceiv(blocked,893) CanSender(blocked,354) CanClock(blocked,326) TMC(blocked,52) MAIN(running,615) IDLE(ready,19)
                  Owned mutexes: File(MAIN)
                  === Platform ===
                  Last reset 00:15:28 ago, cause: power up
                  Last software reset details not available
                  Error status: 0x00
                  Aux0 errors 0,0,0
                  Aux1 errors 0,0,0
                  MCU temperature: min 29.0, current 36.6, max 36.9
                  Supply voltage: min 24.1, current 24.3, max 24.5, under voltage events: 0, over voltage events: 0, power good: yes
                  12V rail voltage: min 12.1, current 12.2, max 12.2, under voltage events: 0
                  Driver 0: position 39840, standstill, reads 53659, writes 18 timeouts 0, SG min/max 0/237
                  Driver 1: position 37920, standstill, reads 53659, writes 18 timeouts 0, SG min/max 0/235
                  Driver 2: position 64, standstill, reads 53659, writes 18 timeouts 0, SG min/max 0/235
                  Driver 3: position 0, standstill, reads 53659, writes 18 timeouts 0, SG min/max 0/255
                  Driver 4: position 0, standstill, reads 53666, writes 11 timeouts 0, SG min/max 0/0
                  Driver 5: position 0, standstill, reads 53666, writes 11 timeouts 0, SG min/max 0/0
                  Date/time: 2021-01-16 21:40:45
                  Slowest loop: 203.63ms; fastest: 0.04ms
                  === Storage ===
                  Free file entries: 10
                  SD card 0 not detected, interface speed: 37.5MBytes/sec
                  SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                  === Move ===
                  DMs created 125, maxWait 677116ms, bed compensation in use: mesh, comp offset 0.000
                  === MainDDARing ===
                  Scheduled moves 94, completed moves 89, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 2], CDDA state 3
                  === AuxDDARing ===
                  Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                  === Heat ===
                  Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                  Heater 0 is on, I-accum = 0.4
                  Heater 1 is on, I-accum = 0.3
                  === GCodes ===
                  Segments left: 0
                  Movement lock held by null
                  HTTP* is idle in state(s) 0
                  Telnet is idle in state(s) 0
                  File* is doing "M122" in state(s) 0
                  USB is idle in state(s) 0
                  Aux is idle in state(s) 0
                  Trigger* is idle in state(s) 0
                  Queue is idle in state(s) 0
                  LCD is idle in state(s) 0
                  SBC is idle in state(s) 0
                  Daemon is idle in state(s) 0
                  Aux2 is idle in state(s) 0
                  Autopause is idle in state(s) 0
                  Code queue is empty.
                  === CAN ===
                  Messages queued 3723, send timeouts 0, received 32, lost 0, longest wait 1ms for reply type 6018, peak Tx sync delay 354, free buffers 48
                  === SBC interface ===
                  State: 0, failed transfers: 0
                  Last transfer: 31ms ago
                  RX/TX seq numbers: 32108/32108
                  SPI underruns 0, overruns 0
                  Number of disconnects: 0, IAP RAM available 0x2c478
                  Buffer RX/TX: 504/1744-0
                  
                  1/16/2021, 4:40:47 PM	=== Duet Control Server ===
                  Duet Control Server v3.2.0
                  File:
                  Buffered code: M122 B1
                  Buffered code: M83 ;relative extrusion mode
                  Buffered code: G10
                  Buffered code: ;LAYER_COUNT:205
                  Buffered code: ;LAYER:0
                  Buffered code: M107
                  Buffered code: G0 F6000 X239.301 Y214.311 Z0.2
                  Buffered code: G11
                  Buffered code: G1 F1200 X239.779 Y213.81 E0.02303
                  Buffered code: G1 X240.312 Y213.368 E0.02303
                  Buffered code: G1 X240.892 Y212.99 E0.02303
                  Buffered code: G1 X241.512 Y212.681 E0.02304
                  Buffered code: G1 X242.164 Y212.446 E0.02305
                  Buffered code: G1 X242.838 Y212.288 E0.02303
                  Buffered code: G1 X243.703 Y212.2 E0.02892
                  Buffered code: G1 X244.192 Y212.189 E0.01627
                  Buffered code: G1 X248.16 Y212.189 E0.13198
                  Buffered code: G1 X248.944 Y212.2 E0.02608
                  Buffered code: G1 X249.571 Y212.239 E0.02089
                  Buffered code: G1 X250.221 Y212.326 E0.02181
                  Buffered code: G1 X250.899 Y212.466 E0.02303
                  Buffered code: G1 X251.539 Y212.677 E0.02241
                  Buffered code: G1 X252.018 Y212.865 E0.01711
                  Buffered code: G1 X252.647 Y213.155 E0.02304
                  Buffered code: G1 X253.403 Y213.633 E0.02975
                  Buffered code: G1 X253.852 Y213.968 E0.01863
                  Buffered code: G1 X253.926 Y214.025 E0.00311
                  Buffered code: G1 X254.45 Y214.478 E0.02304
                  ==> 1212 bytes
                  Pending code: G1 X254.842 Y214.899 E0.01913
                  Pending code: G1 X255.098 Y215.201 E0.01317
                  Code buffer space: 2352
                  Configured SPI speed: 8000000 Hz
                  Full transfers per second: 22.65
                  Maximum length of RX/TX data transfers: 3468/1236
                  File /opt/dsf/sd/gcodes/2ZR_BearingTopMount_FR.gcode is selected, processing
                  
                  1/16/2021, 4:40:47 PM	
                  Diagnostics for board 1:
                  Duet EXP3HC firmware version 3.3beta (2021-01-16 08:18:18)
                  Bootloader ID: not available
                  Never used RAM 154492, free system stack 166 words
                  HEAT 92 CanAsync 92 CanRecv 86 TMC 30 MAIN 306 AIN 259
                  Last reset 00:15:28 ago, cause: power up
                  Last software reset data not available
                  Driver 0: position -276160, 160.0 steps/mm,  ok, reads 9067, writes 18 timeouts 0, SG min/max 0/212, steps req 1080640 done 822518
                  Driver 1: position 53120, 160.0 steps/mm,  ok, reads 9071, writes 18 timeouts 0, SG min/max 0/230, steps req 933120 done 675001
                  Driver 2: position 3886, 172.0 steps/mm,  ok, reads 9076, writes 18 timeouts 0, SG min/max 0/94, steps req 10750 done 10072
                  Moves scheduled 29, completed 27, in progress 1, hiccups 0, step errors 0
                  Peak sync jitter 15, peak Rx sync delay 187, resyncs 0, next step interrupt due in 68 ticks, enabled
                  VIN: 24.7V, V12: 12.3V
                  MCU temperature: min 43.8C, current 43.8C, max 44.0C
                  Ticks since heat task active 155, ADC conversions started 928646, completed 928646, timed out 0
                  Last sensors broadcast 0x00000000 found 0 159 ticks ago, loop time 0
                  CAN messages queued 52, send timeouts 0, received 8373, lost 0, free buffers 36, error reg 110054
                  
                  1/16/2021, 4:46:45 PM	
                  M25
                  Printing paused at X246.2 Y236.3 Z0.4
                  
                  1/16/2021, 4:46:53 PM	
                  M122
                  === Diagnostics ===
                  RepRapFirmware for Duet 3 MB6HC version 3.3beta running on Duet 3 MB6HC v1.01 or later (SBC mode)
                  Board ID: 08DJM-956L2-G43S8-6JKDL-3SJ6L-1802G
                  Used output buffers: 1 of 40 (14 max)
                  === RTOS ===
                  Static ram: 149772
                  Dynamic ram: 64248 of which 104 recycled
                  Never used RAM 140548, free system stack 126 words
                  Tasks: Linux(ready,111) HEAT(blocked,299) CanReceiv(blocked,893) CanSender(blocked,346) CanClock(blocked,326) TMC(blocked,52) MAIN(running,615) IDLE(ready,19)
                  Owned mutexes: HTTP(MAIN)
                  === Platform ===
                  Last reset 00:21:35 ago, cause: power up
                  Last software reset details not available
                  Error status: 0x00
                  Aux0 errors 0,0,0
                  Aux1 errors 0,0,0
                  MCU temperature: min 36.5, current 37.2, max 37.2
                  Supply voltage: min 24.1, current 24.3, max 24.5, under voltage events: 0, over voltage events: 0, power good: yes
                  12V rail voltage: min 12.1, current 12.2, max 12.2, under voltage events: 0
                  Driver 0: position 73845, standstill, reads 62142, writes 0 timeouts 0, SG min/max 0/233
                  Driver 1: position 5906, standstill, reads 62142, writes 0 timeouts 0, SG min/max 0/230
                  Driver 2: position 1080, standstill, reads 62143, writes 0 timeouts 0, SG min/max 0/231
                  Driver 3: position 0, standstill, reads 62143, writes 0 timeouts 0, SG min/max 0/250
                  Driver 4: position 0, standstill, reads 62143, writes 0 timeouts 0, SG min/max not available
                  Driver 5: position 0, standstill, reads 62143, writes 0 timeouts 0, SG min/max not available
                  Date/time: 2021-01-16 21:46:52
                  Slowest loop: 39.49ms; fastest: 0.04ms
                  === Storage ===
                  Free file entries: 10
                  SD card 0 not detected, interface speed: 37.5MBytes/sec
                  SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                  === Move ===
                  DMs created 125, maxWait 0ms, bed compensation in use: mesh, comp offset 0.000
                  === MainDDARing ===
                  Scheduled moves 4372, completed moves 4372, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                  === AuxDDARing ===
                  Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                  === Heat ===
                  Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                  Heater 0 is on, I-accum = 0.4
                  Heater 1 is on, I-accum = 0.3
                  === GCodes ===
                  Segments left: 0
                  Movement lock held by null
                  HTTP* is doing "M122" in state(s) 0
                  Telnet is idle in state(s) 0
                  File* is idle in state(s) 0
                  USB is idle in state(s) 0
                  Aux is idle in state(s) 0
                  Trigger* is idle in state(s) 0
                  Queue* is idle in state(s) 0
                  LCD is idle in state(s) 0
                  SBC is idle in state(s) 0
                  Daemon is idle in state(s) 0
                  Aux2 is idle in state(s) 0
                  Autopause is idle in state(s) 0
                  Code queue is empty.
                  === CAN ===
                  Messages queued 5754, send timeouts 0, received 24, lost 0, longest wait 21ms for reply type 6024, peak Tx sync delay 373, free buffers 48
                  === SBC interface ===
                  State: 4, failed transfers: 0
                  Last transfer: 1ms ago
                  RX/TX seq numbers: 47336/47336
                  SPI underruns 0, overruns 0
                  Number of disconnects: 0, IAP RAM available 0x2c478
                  Buffer RX/TX: 0/0-0
                  === Duet Control Server ===
                  Duet Control Server v3.2.0
                  Code buffer space: 4096
                  Configured SPI speed: 8000000 Hz
                  Full transfers per second: 41.53
                  Maximum length of RX/TX data transfers: 4664/1664
                  File /opt/dsf/sd/gcodes/2ZR_BearingTopMount_FR.gcode is selected, paused
                  
                  1/16/2021, 4:47:01 PM	
                  M122 B1
                  Diagnostics for board 1:
                  Duet EXP3HC firmware version 3.3beta (2021-01-16 08:18:18)
                  Bootloader ID: not available
                  Never used RAM 154492, free system stack 165 words
                  HEAT 92 CanAsync 92 CanRecv 86 TMC 30 MAIN 282 AIN 259
                  Last reset 00:21:43 ago, cause: power up
                  Last software reset data not available
                  Driver 0: position -257449, 160.0 steps/mm,  standstill, reads 50071, writes 0 timeouts 0, SG min/max 0/897, steps req 1128627 done 1136804
                  Driver 1: position 12303, 160.0 steps/mm,  standstill, reads 50071, writes 0 timeouts 0, SG min/max 0/810, steps req 1156019 done 1164193
                  Driver 2: position 12182, 172.0 steps/mm,  standstill, reads 50069, writes 0 timeouts 0, SG min/max 0/703, steps req 44372 done 45391
                  Moves scheduled 4269, completed 4269, in progress 0, hiccups 110, step errors 0
                  Peak sync jitter 15, peak Rx sync delay 47157, resyncs 17, no step interrupt scheduled
                  VIN: 24.7V, V12: 12.3V
                  MCU temperature: min 43.8C, current 44.0C, max 44.0C
                  Ticks since heat task active 80, ADC conversions started 1303072, completed 1303070, timed out 0
                  Last sensors broadcast 0x00000000 found 0 84 ticks ago, loop time 0
                  CAN messages queued 24, send timeouts 0, received 7601, lost 56, free buffers 36, error reg 3c
                  
                  1 Reply Last reply Reply Quote 0
                  • dc42undefined
                    dc42 administrators
                    last edited by

                    Thanks for the additoinal data.

                    I've just run your print up to the 93% finished mark. This is the data:

                    m122b1
                    Diagnostics for board 1:
                    Duet EXP3HC firmware version 3.3beta (2021-01-16 19:11:54)
                    Bootloader ID: SAME5x bootloader version 2.2 (2021-01-16b1)
                    Never used RAM 154492, free system stack 142 words
                    HEAT 92 CanAsync 92 CanRecv 79 TMC 30 MAIN 274 AIN 259
                    Last reset 03:06:56 ago, cause: power up
                    Last software reset data not available
                    Driver 0: position 78458, 160.0 steps/mm,  standstill, reads 11912, writes 2 timeouts 0, SG min/max 0/72, steps req 49298753 done 49298753
                    Driver 1: position 82701, 160.0 steps/mm,  standstill, reads 11912, writes 2 timeouts 0, SG min/max 0/72, steps req 50413393 done 50413393
                    Driver 2: position 719839, 172.0 steps/mm,  standstill, reads 11913, writes 2 timeouts 0, SG min/max 0/67, steps req 1793879 done 1791393
                    Moves scheduled 210097, completed 210097, in progress 0, hiccups 15372, step errors 0
                    Peak sync jitter 24, peak Rx sync delay 49110, resyncs 200, no step interrupt scheduled
                    VIN: 24.4V, V12: 12.2V
                    MCU temperature: min 44.1C, current 44.2C, max 44.4C
                    Ticks since heat task active 40, ADC conversions started 11216032, completed 11216031, timed out 0
                    Last sensors broadcast 0x00000000 found 0 44 ticks ago, loop time 0
                    CAN messages queued 27, send timeouts 0, received 245625, lost 2226, free buffers 36, error reg 0
                    

                    So I am still not seeing any loss of XY done vs. requested steps, only a loss of 0.14% of E steps. This is with pressure advance set to zero. OTOH there have been 2226 lost CAN messages, presumably mostly movement messages, so moves will have been lost.

                    My pause.g and resume.g are currently empty. You've provided your pause.g. Please provide your resume.g file too, then I will try again using your files, in case it makes a difference.

                    I will work on fixing the lost CAN messages tomorrow or Monday.

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

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                    • evomotorsundefined
                      evomotors @dc42
                      last edited by

                      @dc42 said in Duet3 6CH + 3CH expansion board - Missing steps.:

                      Thanks for the additoinal data.

                      I've just run your print up to the 93% finished mark. This is the data:

                      m122b1
                      Diagnostics for board 1:
                      Duet EXP3HC firmware version 3.3beta (2021-01-16 19:11:54)
                      Bootloader ID: SAME5x bootloader version 2.2 (2021-01-16b1)
                      Never used RAM 154492, free system stack 142 words
                      HEAT 92 CanAsync 92 CanRecv 79 TMC 30 MAIN 274 AIN 259
                      Last reset 03:06:56 ago, cause: power up
                      Last software reset data not available
                      Driver 0: position 78458, 160.0 steps/mm,  standstill, reads 11912, writes 2 timeouts 0, SG min/max 0/72, steps req 49298753 done 49298753
                      Driver 1: position 82701, 160.0 steps/mm,  standstill, reads 11912, writes 2 timeouts 0, SG min/max 0/72, steps req 50413393 done 50413393
                      Driver 2: position 719839, 172.0 steps/mm,  standstill, reads 11913, writes 2 timeouts 0, SG min/max 0/67, steps req 1793879 done 1791393
                      Moves scheduled 210097, completed 210097, in progress 0, hiccups 15372, step errors 0
                      Peak sync jitter 24, peak Rx sync delay 49110, resyncs 200, no step interrupt scheduled
                      VIN: 24.4V, V12: 12.2V
                      MCU temperature: min 44.1C, current 44.2C, max 44.4C
                      Ticks since heat task active 40, ADC conversions started 11216032, completed 11216031, timed out 0
                      Last sensors broadcast 0x00000000 found 0 44 ticks ago, loop time 0
                      CAN messages queued 27, send timeouts 0, received 245625, lost 2226, free buffers 36, error reg 0
                      

                      So I am still not seeing any loss of XY done vs. requested steps, only a loss of 0.14% of E steps. This is with pressure advance set to zero. OTOH there have been 2226 lost CAN messages, presumably mostly movement messages, so moves will have been lost.

                      My pause.g and resume.g are currently empty. You've provided your pause.g. Please provide your resume.g file too, then I will try again using your files, in case it makes a difference.

                      I will work on fixing the lost CAN messages tomorrow or Monday.

                      So why it's not working for me? I'm not even talking about diagnostics. It is not printing when motors connected to expansion board. But works flawlessly when connected to Duet3.

                      All configs are attached. Compressed and renamed to txt
                      [0_1610838265664_RRF_3.3_Bakcup.zip](Uploading 100%) RRF_3.3_Bakcup.zip.txt

                      dc42undefined 1 Reply Last reply Reply Quote 0
                      • dc42undefined
                        dc42 administrators @evomotors
                        last edited by

                        @evomotors said in Duet3 6CH + 3CH expansion board - Missing steps.:

                        It is not printing when motors connected to expansion board.

                        Please explain what you mean by this. I thought it was printing, but the print quality was poor.

                        Duet WiFi hardware designer and firmware engineer
                        Please do not ask me for Duet support via PM or email, use the forum
                        http://www.escher3d.com, https://miscsolutions.wordpress.com

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                        • evomotorsundefined
                          evomotors @dc42
                          last edited by

                          @dc42 said in Duet3 6CH + 3CH expansion board - Missing steps.:

                          @evomotors said in Duet3 6CH + 3CH expansion board - Missing steps.:

                          It is not printing when motors connected to expansion board.

                          Please explain what you mean by this. I thought it was printing, but the print quality was poor.

                          I'm taking about stuff that's happening on my videos. I cannot call this printing. Did you actually see the videos?

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                          • evomotorsundefined
                            evomotors @dc42
                            last edited by

                            @dc42 There are 2 videos I posted earlier in this thread. One showing motors connected to Duet3 and another then motors connected to expansion board. Please watch

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                            • dc42undefined
                              dc42 administrators
                              last edited by

                              I was confusing you with the other guy having a problem with print quality when the extruder is on an expansion board. I searched through the 128 posts in this thread and eventually found your video. It looks like it's printing correctly most of the time, but occasionally there is a big jolt which results in a shift in X and/or Y. That ties in with the lost CAN messages that are reported by M122 B1.

                              Duet WiFi hardware designer and firmware engineer
                              Please do not ask me for Duet support via PM or email, use the forum
                              http://www.escher3d.com, https://miscsolutions.wordpress.com

                              evomotorsundefined jbarrosundefined 2 Replies Last reply Reply Quote 0
                              • evomotorsundefined
                                evomotors @dc42
                                last edited by

                                @dc42 said in Duet3 6CH + 3CH expansion board - Missing steps.:

                                I was confusing you with the other guy having a problem with print quality when the extruder is on an expansion board. I searched through the 128 posts in this thread and eventually found your video. It looks like it's printing correctly most of the time, but occasionally there is a big jolt which results in a shift in X and/or Y. That ties in with the lost CAN messages that are reported by M122 B1.

                                The bottom line is when I connect XY motors to Duet3 board that problem disappears, but E steps still missing or not synchronized with XY movement and that produces bad quality print. Unfortunately I cannot connect extruder to duet3 as well as Duet3 has 6 stepper drivers, but I need 7.

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                                • jbarrosundefined
                                  jbarros @dc42
                                  last edited by

                                  @dc42 said in Duet3 6CH + 3CH expansion board - Missing steps.:

                                  I was confusing you with the other guy having a problem with print quality when the extruder is on an expansion board.

                                  If you're refering to a ToolBoard then I'm the guy 🙂 and this is my thread: https://forum.duet3d.com/topic/20899/duet3d-6hc-toolboard-missing-filament-on-curves

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                                  • dc42undefined
                                    dc42 administrators
                                    last edited by dc42

                                    Yes, it figures that extrusion will be affected as well. Most of the moves in a print involve X, Y and E movement. So even if you move X and Y to the main board, there is still a CAN packet sent for the E movement.

                                    I think the reason we haven't seen this before is that your print uses sequences of tiny movements, smaller than our other tests use. For example:

                                    G0 F12000 X273.288 Y248.054
                                    G1 F4800 X273.303 Y248.082 E0.00106
                                    G1 X273.539 Y248.591 E0.01866
                                    G1 X273.542 Y248.6 E0.00032
                                    G1 X273.603 Y248.759 E0.00566
                                    G1 X273.682 Y248.966 E0.00737
                                    G1 X273.759 Y249.171 E0.00728
                                    G1 X273.763 Y249.184 E0.00045
                                    

                                    Here are those moves imported into a spreadsheet. The columns are X, Y, change in X, change in Y, move distance, and move time.

                                    d21e1da1-2f59-4adb-93e4-f0637b734902-image.png

                                    There are really small moves. The fourth one is less than 10 microns long and it will execute in just 120 microseconds. The longest one takes only 7 milliseconds and all the rest are below 3 milliseconds. So the system is having to process a very high rate of moves. Still, I don't see any evidence that the CAN bus is being overloaded, so I expect to resolve the issues with this print by improving the efficiency of processing the incoming move commands on the expansion board.

                                    Duet WiFi hardware designer and firmware engineer
                                    Please do not ask me for Duet support via PM or email, use the forum
                                    http://www.escher3d.com, https://miscsolutions.wordpress.com

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                                    • evomotorsundefined
                                      evomotors @dc42
                                      last edited by

                                      @dc42 Could my issue exists due to faulty Duet board ? I'm dead in the water. I cannot print at all for several weeks already.

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                                      • Luke'sLaboratoryundefined
                                        Luke'sLaboratory @evomotors
                                        last edited by

                                        @evomotors

                                        @dc42 said:

                                        So I am still not seeing any loss of XY done vs. requested steps, only a loss of 0.14% of E steps. This is with pressure advance set to zero. OTOH there have been 2226 lost CAN messages, presumably mostly movement messages, so moves will have been lost.

                                        Luke
                                        http://lukeslab.online

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                                        • evomotorsundefined
                                          evomotors @dc42
                                          last edited by

                                          @dc42 do you have any time estimates? I’m wondering when I’ll be able to print.

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                                          • evomotorsundefined
                                            evomotors
                                            last edited by

                                            Can I have some updates? Please...

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