• Tags
  • Documentation
  • Order
  • Register
  • Login
Duet3D Logo Duet3D
  • Tags
  • Documentation
  • Order
  • Register
  • Login

Duet3 6CH + 3CH expansion board - Missing steps.

Scheduled Pinned Locked Moved Solved
Tuning and tweaking
12
153
8.7k
Loading More Posts
  • Oldest to Newest
  • Newest to Oldest
  • Most Votes
Reply
  • Reply as topic
Log in to reply
This topic has been deleted. Only users with topic management privileges can see it.
  • undefined
    evomotors @dc42
    last edited by 16 Jan 2021, 20:02

    @dc42 Ok , none of my homing files contains G28, it's only in bed. let me remove it and run another test.

    1 Reply Last reply Reply Quote 0
    • undefined
      evomotors
      last edited by evomotors 16 Jan 2021, 20:08

      Restarted the printer:
      @dc42 not sure if it's expected fresh after restart

      Peak sync jitter 13, peak Rx sync delay 176
      

      Full log:

      M122 B1
      Diagnostics for board 1:
      Duet EXP3HC firmware version 3.3beta (2021-01-16 08:18:18)
      Bootloader ID: not available
      Never used RAM 154492, free system stack 200 words
      HEAT 104 CanAsync 92 CanRecv 86 TMC 64 MAIN 282 AIN 259
      Last reset 00:01:26 ago, cause: software
      Last software reset data not available
      Driver 0: position 0, 160.0 steps/mm, standstill, reads 8690, writes 0 timeouts 0, SG min/max not available, steps req 0 done 0
      Driver 1: position 0, 160.0 steps/mm, standstill, reads 8689, writes 0 timeouts 0, SG min/max not available, steps req 0 done 0
      Driver 2: position 0, 172.0 steps/mm, standstill, reads 8689, writes 0 timeouts 0, SG min/max not available, steps req 0 done 0
      Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0
      Peak sync jitter 13, peak Rx sync delay 176, resyncs 0, no step interrupt scheduled
      VIN: 24.7V, V12: 12.3V
      MCU temperature: min 43.8C, current 44.0C, max 44.0C
      Ticks since heat task active 99, ADC conversions started 86340, completed 86340, timed out 0
      Last sensors broadcast 0x00000000 found 0 103 ticks ago, loop time 0
      CAN messages queued 24, send timeouts 0, received 105, lost 0, free buffers 36, error reg 4f

      Now will run print

      1 Reply Last reply Reply Quote 0
      • undefined
        evomotors
        last edited by evomotors 16 Jan 2021, 20:38

        @dc42
        No G28 anywhere, no homing moves between M122 commands. And I only ran M122 once after pausing the print. This time I didn't stop, just pause. Still reporting missing steps.

        M122
        === Diagnostics ===
        RepRapFirmware for Duet 3 MB6HC version 3.3beta running on Duet 3 MB6HC v1.01 or later (SBC mode)
        Board ID: 08DJM-956L2-G43S8-6JKDL-3SJ6L-1802G
        Used output buffers: 1 of 40 (12 max)
        === RTOS ===
        Static ram: 149772
        Dynamic ram: 64248 of which 104 recycled
        Never used RAM 140548, free system stack 130 words
        Tasks: Linux(ready,141) HEAT(blocked,299) CanReceiv(blocked,893) CanSender(blocked,346) CanClock(blocked,326) TMC(blocked,52) MAIN(running,655) IDLE(ready,19)
        Owned mutexes: HTTP(MAIN)
        === Platform ===
        Last reset 00:30:20 ago, cause: power up
        Last software reset at 2021-01-16 20:06, reason: MemoryProtectionFault mmarValid daccViol, GCodes spinning, available RAM 140596, slot 1
        Software reset code 0x4163 HFSR 0x00000000 CFSR 0x00000082 ICSR 0x00400804 BFAR 0x00000038 SP 0x204235e8 Task MAIN Freestk 1658 ok
        Stack: 00000000 00000001 00000001 00000000 20423633 0046dd2d 0046d97c 61010000 2042ad78 00000000 00000000 0046dd37 00000000 00000000 3ca3d70a 0000000a 4374da1d 2042b29c 00000000 00000001 00000000 0046d9e7 2042b29c fffc0000 003fffff 0046dd27 00000000
        Error status: 0x00
        Aux0 errors 0,0,0
        Aux1 errors 0,0,0
        MCU temperature: min 35.0, current 37.3, max 37.4
        Supply voltage: min 24.0, current 24.3, max 24.5, under voltage events: 0, over voltage events: 0, power good: yes
        12V rail voltage: min 12.1, current 12.2, max 12.2, under voltage events: 0
        Driver 0: position 79788, standstill, reads 18682, writes 3 timeouts 0, SG min/max 0/240
        Driver 1: position -219, standstill, reads 18682, writes 3 timeouts 0, SG min/max 0/240
        Driver 2: position 1321, standstill, reads 18682, writes 3 timeouts 0, SG min/max 0/240
        Driver 3: position 0, standstill, reads 18682, writes 3 timeouts 0, SG min/max 0/254
        Driver 4: position 0, standstill, reads 18685, writes 0 timeouts 0, SG min/max not available
        Driver 5: position 0, standstill, reads 18684, writes 0 timeouts 0, SG min/max not available
        Date/time: 2021-01-16 20:36:44
        Slowest loop: 183.43ms; fastest: 0.03ms
        === Storage ===
        Free file entries: 10
        SD card 0 not detected, interface speed: 37.5MBytes/sec
        SD card longest read time 0.0ms, write time 0.0ms, max retries 0
        === Move ===
        DMs created 125, maxWait 768639ms, bed compensation in use: mesh, comp offset 0.000
        === MainDDARing ===
        Scheduled moves 13893, completed moves 13893, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 2], CDDA state -1
        === AuxDDARing ===
        Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
        === Heat ===
        Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
        Heater 0 is on, I-accum = 0.4
        Heater 1 is on, I-accum = 0.3
        === GCodes ===
        Segments left: 0
        Movement lock held by null
        HTTP* is doing "M122" in state(s) 0
        Telnet is idle in state(s) 0
        File* is idle in state(s) 0
        USB is idle in state(s) 0
        Aux is idle in state(s) 0
        Trigger* is idle in state(s) 0
        Queue* is idle in state(s) 0
        LCD is idle in state(s) 0
        SBC is idle in state(s) 0
        Daemon is idle in state(s) 0
        Aux2 is idle in state(s) 0
        Autopause is idle in state(s) 0
        Code queue is empty.
        === CAN ===
        Messages queued 20932, send timeouts 0, received 67, lost 0, longest wait 19ms for reply type 6024, peak Tx sync delay 387, free buffers 48
        === SBC interface ===
        State: 4, failed transfers: 0
        Last transfer: 1ms ago
        RX/TX seq numbers: 4299/4299
        SPI underruns 0, overruns 0
        Number of disconnects: 0, IAP RAM available 0x2c478
        Buffer RX/TX: 0/0-0
        === Duet Control Server ===
        Duet Control Server v3.2.0
        Code buffer space: 4096
        Configured SPI speed: 8000000 Hz
        Full transfers per second: 38.79
        Maximum length of RX/TX data transfers: 3032/1688
        File /opt/dsf/sd/gcodes/ZR_BearingTopMount_FR.gcode is selected, paused
        M122 B1
        Diagnostics for board 1:
        Duet EXP3HC firmware version 3.3beta (2021-01-16 08:18:18)
        Bootloader ID: not available
        Never used RAM 154492, free system stack 165 words
        HEAT 92 CanAsync 92 CanRecv 86 TMC 30 MAIN 274 AIN 259
        Last reset 00:30:25 ago, cause: software
        Last software reset data not available
        Driver 0: position -252890, 160.0 steps/mm, standstill, reads 47021, writes 1 timeouts 0, SG min/max 0/431, steps req 4754028 done 4495266
        Driver 1: position 11122, 160.0 steps/mm, standstill, reads 47021, writes 1 timeouts 0, SG min/max 0/1023, steps req 4516310 done 4257548
        Driver 2: position 43107, 172.0 steps/mm, standstill, reads 47022, writes 1 timeouts 0, SG min/max 0/609, steps req 146093 done 148150
        Moves scheduled 13764, completed 13764, in progress 0, hiccups 462, step errors 0
        Peak sync jitter 15, peak Rx sync delay 48876, resyncs 16, no step interrupt scheduled
        VIN: 24.7V, V12: 12.3V
        MCU temperature: min 43.8C, current 44.0C, max 44.2C
        Ticks since heat task active 148, ADC conversions started 1825390, completed 1825388, timed out 0
        Last sensors broadcast 0x00000000 found 0 152 ticks ago, loop time 0
        CAN messages queued 43, send timeouts 0, received 29446, lost 76, free buffers 36, error reg 24
        1 Reply Last reply Reply Quote 0
        • undefined
          evomotors
          last edited by 16 Jan 2021, 20:49

          By the way, I just got this comment on my YouTube video:
          67344bfb-72fa-4b52-b290-b5d093504a9d-image.png

          1 Reply Last reply Reply Quote 0
          • undefined
            evomotors
            last edited by 16 Jan 2021, 21:38

            @dc42 Ok, I see your point, I added

            M122
            M122 B1

            To my startup GCode after all preparation moves. So it will execute just before actual print.

            1 Reply Last reply Reply Quote 0
            • undefined
              evomotors
              last edited by evomotors 16 Jan 2021, 21:58

              @dc42 I added M112 & M112 B1 to the end of my start GCode in slicer then power cycle the printer and started print job.

              These are all console enrties in chronological order:

              1/16/2021, 4:25:51 PM
              Connection established
              1/16/2021, 4:35:56 PM
              M32 "0:/gcodes/2ZR_BearingTopMount_FR.gcode"
              File 0:/gcodes/2ZR_BearingTopMount_FR.gcode selected for printing
              1/16/2021, 4:40:20 PM
              Leadscrew adjustments made: 0.196 0.148 0.149 0.184, points used 4, (mean, deviation) before (0.167, 0.017) after (0.000, 0.000)
              1/16/2021, 4:40:20 PM
              Bed Leveling Cycle: 1 - Difference was 0.017mm
              1/16/2021, 4:40:20 PM
              Leadscrew adjustments made: 0.005 -0.005 -0.005 -0.007, points used 4, (mean, deviation) before (-0.003, 0.003) after (0.000, 0.000)
              1/16/2021, 4:40:20 PM
              Bed Tramming Cycle: 2 - Difference was 0.003mm
              1/16/2021, 4:40:20 PM
              Height map loaded from file heightmap.csv
              1/16/2021, 4:40:46 PM
              === Diagnostics ===
              RepRapFirmware for Duet 3 MB6HC version 3.3beta running on Duet 3 MB6HC v1.01 or later (SBC mode)
              Board ID: 08DJM-956L2-G43S8-6JKDL-3SJ6L-1802G
              Used output buffers: 1 of 40 (10 max)
              === RTOS ===
              Static ram: 149772
              Dynamic ram: 64248 of which 104 recycled
              Never used RAM 140548, free system stack 126 words
              Tasks: Linux(ready,111) HEAT(blocked,299) CanReceiv(blocked,893) CanSender(blocked,354) CanClock(blocked,326) TMC(blocked,52) MAIN(running,615) IDLE(ready,19)
              Owned mutexes: File(MAIN)
              === Platform ===
              Last reset 00:15:28 ago, cause: power up
              Last software reset details not available
              Error status: 0x00
              Aux0 errors 0,0,0
              Aux1 errors 0,0,0
              MCU temperature: min 29.0, current 36.6, max 36.9
              Supply voltage: min 24.1, current 24.3, max 24.5, under voltage events: 0, over voltage events: 0, power good: yes
              12V rail voltage: min 12.1, current 12.2, max 12.2, under voltage events: 0
              Driver 0: position 39840, standstill, reads 53659, writes 18 timeouts 0, SG min/max 0/237
              Driver 1: position 37920, standstill, reads 53659, writes 18 timeouts 0, SG min/max 0/235
              Driver 2: position 64, standstill, reads 53659, writes 18 timeouts 0, SG min/max 0/235
              Driver 3: position 0, standstill, reads 53659, writes 18 timeouts 0, SG min/max 0/255
              Driver 4: position 0, standstill, reads 53666, writes 11 timeouts 0, SG min/max 0/0
              Driver 5: position 0, standstill, reads 53666, writes 11 timeouts 0, SG min/max 0/0
              Date/time: 2021-01-16 21:40:45
              Slowest loop: 203.63ms; fastest: 0.04ms
              === Storage ===
              Free file entries: 10
              SD card 0 not detected, interface speed: 37.5MBytes/sec
              SD card longest read time 0.0ms, write time 0.0ms, max retries 0
              === Move ===
              DMs created 125, maxWait 677116ms, bed compensation in use: mesh, comp offset 0.000
              === MainDDARing ===
              Scheduled moves 94, completed moves 89, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 2], CDDA state 3
              === AuxDDARing ===
              Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
              === Heat ===
              Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
              Heater 0 is on, I-accum = 0.4
              Heater 1 is on, I-accum = 0.3
              === GCodes ===
              Segments left: 0
              Movement lock held by null
              HTTP* is idle in state(s) 0
              Telnet is idle in state(s) 0
              File* is doing "M122" in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger* is idle in state(s) 0
              Queue is idle in state(s) 0
              LCD is idle in state(s) 0
              SBC is idle in state(s) 0
              Daemon is idle in state(s) 0
              Aux2 is idle in state(s) 0
              Autopause is idle in state(s) 0
              Code queue is empty.
              === CAN ===
              Messages queued 3723, send timeouts 0, received 32, lost 0, longest wait 1ms for reply type 6018, peak Tx sync delay 354, free buffers 48
              === SBC interface ===
              State: 0, failed transfers: 0
              Last transfer: 31ms ago
              RX/TX seq numbers: 32108/32108
              SPI underruns 0, overruns 0
              Number of disconnects: 0, IAP RAM available 0x2c478
              Buffer RX/TX: 504/1744-0
              1/16/2021, 4:40:47 PM === Duet Control Server ===
              Duet Control Server v3.2.0
              File:
              Buffered code: M122 B1
              Buffered code: M83 ;relative extrusion mode
              Buffered code: G10
              Buffered code: ;LAYER_COUNT:205
              Buffered code: ;LAYER:0
              Buffered code: M107
              Buffered code: G0 F6000 X239.301 Y214.311 Z0.2
              Buffered code: G11
              Buffered code: G1 F1200 X239.779 Y213.81 E0.02303
              Buffered code: G1 X240.312 Y213.368 E0.02303
              Buffered code: G1 X240.892 Y212.99 E0.02303
              Buffered code: G1 X241.512 Y212.681 E0.02304
              Buffered code: G1 X242.164 Y212.446 E0.02305
              Buffered code: G1 X242.838 Y212.288 E0.02303
              Buffered code: G1 X243.703 Y212.2 E0.02892
              Buffered code: G1 X244.192 Y212.189 E0.01627
              Buffered code: G1 X248.16 Y212.189 E0.13198
              Buffered code: G1 X248.944 Y212.2 E0.02608
              Buffered code: G1 X249.571 Y212.239 E0.02089
              Buffered code: G1 X250.221 Y212.326 E0.02181
              Buffered code: G1 X250.899 Y212.466 E0.02303
              Buffered code: G1 X251.539 Y212.677 E0.02241
              Buffered code: G1 X252.018 Y212.865 E0.01711
              Buffered code: G1 X252.647 Y213.155 E0.02304
              Buffered code: G1 X253.403 Y213.633 E0.02975
              Buffered code: G1 X253.852 Y213.968 E0.01863
              Buffered code: G1 X253.926 Y214.025 E0.00311
              Buffered code: G1 X254.45 Y214.478 E0.02304
              ==> 1212 bytes
              Pending code: G1 X254.842 Y214.899 E0.01913
              Pending code: G1 X255.098 Y215.201 E0.01317
              Code buffer space: 2352
              Configured SPI speed: 8000000 Hz
              Full transfers per second: 22.65
              Maximum length of RX/TX data transfers: 3468/1236
              File /opt/dsf/sd/gcodes/2ZR_BearingTopMount_FR.gcode is selected, processing
              1/16/2021, 4:40:47 PM
              Diagnostics for board 1:
              Duet EXP3HC firmware version 3.3beta (2021-01-16 08:18:18)
              Bootloader ID: not available
              Never used RAM 154492, free system stack 166 words
              HEAT 92 CanAsync 92 CanRecv 86 TMC 30 MAIN 306 AIN 259
              Last reset 00:15:28 ago, cause: power up
              Last software reset data not available
              Driver 0: position -276160, 160.0 steps/mm, ok, reads 9067, writes 18 timeouts 0, SG min/max 0/212, steps req 1080640 done 822518
              Driver 1: position 53120, 160.0 steps/mm, ok, reads 9071, writes 18 timeouts 0, SG min/max 0/230, steps req 933120 done 675001
              Driver 2: position 3886, 172.0 steps/mm, ok, reads 9076, writes 18 timeouts 0, SG min/max 0/94, steps req 10750 done 10072
              Moves scheduled 29, completed 27, in progress 1, hiccups 0, step errors 0
              Peak sync jitter 15, peak Rx sync delay 187, resyncs 0, next step interrupt due in 68 ticks, enabled
              VIN: 24.7V, V12: 12.3V
              MCU temperature: min 43.8C, current 43.8C, max 44.0C
              Ticks since heat task active 155, ADC conversions started 928646, completed 928646, timed out 0
              Last sensors broadcast 0x00000000 found 0 159 ticks ago, loop time 0
              CAN messages queued 52, send timeouts 0, received 8373, lost 0, free buffers 36, error reg 110054
              1/16/2021, 4:46:45 PM
              M25
              Printing paused at X246.2 Y236.3 Z0.4
              1/16/2021, 4:46:53 PM
              M122
              === Diagnostics ===
              RepRapFirmware for Duet 3 MB6HC version 3.3beta running on Duet 3 MB6HC v1.01 or later (SBC mode)
              Board ID: 08DJM-956L2-G43S8-6JKDL-3SJ6L-1802G
              Used output buffers: 1 of 40 (14 max)
              === RTOS ===
              Static ram: 149772
              Dynamic ram: 64248 of which 104 recycled
              Never used RAM 140548, free system stack 126 words
              Tasks: Linux(ready,111) HEAT(blocked,299) CanReceiv(blocked,893) CanSender(blocked,346) CanClock(blocked,326) TMC(blocked,52) MAIN(running,615) IDLE(ready,19)
              Owned mutexes: HTTP(MAIN)
              === Platform ===
              Last reset 00:21:35 ago, cause: power up
              Last software reset details not available
              Error status: 0x00
              Aux0 errors 0,0,0
              Aux1 errors 0,0,0
              MCU temperature: min 36.5, current 37.2, max 37.2
              Supply voltage: min 24.1, current 24.3, max 24.5, under voltage events: 0, over voltage events: 0, power good: yes
              12V rail voltage: min 12.1, current 12.2, max 12.2, under voltage events: 0
              Driver 0: position 73845, standstill, reads 62142, writes 0 timeouts 0, SG min/max 0/233
              Driver 1: position 5906, standstill, reads 62142, writes 0 timeouts 0, SG min/max 0/230
              Driver 2: position 1080, standstill, reads 62143, writes 0 timeouts 0, SG min/max 0/231
              Driver 3: position 0, standstill, reads 62143, writes 0 timeouts 0, SG min/max 0/250
              Driver 4: position 0, standstill, reads 62143, writes 0 timeouts 0, SG min/max not available
              Driver 5: position 0, standstill, reads 62143, writes 0 timeouts 0, SG min/max not available
              Date/time: 2021-01-16 21:46:52
              Slowest loop: 39.49ms; fastest: 0.04ms
              === Storage ===
              Free file entries: 10
              SD card 0 not detected, interface speed: 37.5MBytes/sec
              SD card longest read time 0.0ms, write time 0.0ms, max retries 0
              === Move ===
              DMs created 125, maxWait 0ms, bed compensation in use: mesh, comp offset 0.000
              === MainDDARing ===
              Scheduled moves 4372, completed moves 4372, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
              === AuxDDARing ===
              Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
              === Heat ===
              Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
              Heater 0 is on, I-accum = 0.4
              Heater 1 is on, I-accum = 0.3
              === GCodes ===
              Segments left: 0
              Movement lock held by null
              HTTP* is doing "M122" in state(s) 0
              Telnet is idle in state(s) 0
              File* is idle in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger* is idle in state(s) 0
              Queue* is idle in state(s) 0
              LCD is idle in state(s) 0
              SBC is idle in state(s) 0
              Daemon is idle in state(s) 0
              Aux2 is idle in state(s) 0
              Autopause is idle in state(s) 0
              Code queue is empty.
              === CAN ===
              Messages queued 5754, send timeouts 0, received 24, lost 0, longest wait 21ms for reply type 6024, peak Tx sync delay 373, free buffers 48
              === SBC interface ===
              State: 4, failed transfers: 0
              Last transfer: 1ms ago
              RX/TX seq numbers: 47336/47336
              SPI underruns 0, overruns 0
              Number of disconnects: 0, IAP RAM available 0x2c478
              Buffer RX/TX: 0/0-0
              === Duet Control Server ===
              Duet Control Server v3.2.0
              Code buffer space: 4096
              Configured SPI speed: 8000000 Hz
              Full transfers per second: 41.53
              Maximum length of RX/TX data transfers: 4664/1664
              File /opt/dsf/sd/gcodes/2ZR_BearingTopMount_FR.gcode is selected, paused
              1/16/2021, 4:47:01 PM
              M122 B1
              Diagnostics for board 1:
              Duet EXP3HC firmware version 3.3beta (2021-01-16 08:18:18)
              Bootloader ID: not available
              Never used RAM 154492, free system stack 165 words
              HEAT 92 CanAsync 92 CanRecv 86 TMC 30 MAIN 282 AIN 259
              Last reset 00:21:43 ago, cause: power up
              Last software reset data not available
              Driver 0: position -257449, 160.0 steps/mm, standstill, reads 50071, writes 0 timeouts 0, SG min/max 0/897, steps req 1128627 done 1136804
              Driver 1: position 12303, 160.0 steps/mm, standstill, reads 50071, writes 0 timeouts 0, SG min/max 0/810, steps req 1156019 done 1164193
              Driver 2: position 12182, 172.0 steps/mm, standstill, reads 50069, writes 0 timeouts 0, SG min/max 0/703, steps req 44372 done 45391
              Moves scheduled 4269, completed 4269, in progress 0, hiccups 110, step errors 0
              Peak sync jitter 15, peak Rx sync delay 47157, resyncs 17, no step interrupt scheduled
              VIN: 24.7V, V12: 12.3V
              MCU temperature: min 43.8C, current 44.0C, max 44.0C
              Ticks since heat task active 80, ADC conversions started 1303072, completed 1303070, timed out 0
              Last sensors broadcast 0x00000000 found 0 84 ticks ago, loop time 0
              CAN messages queued 24, send timeouts 0, received 7601, lost 56, free buffers 36, error reg 3c
              1 Reply Last reply Reply Quote 0
              • undefined
                dc42 administrators
                last edited by 16 Jan 2021, 22:34

                Thanks for the additoinal data.

                I've just run your print up to the 93% finished mark. This is the data:

                m122b1
                Diagnostics for board 1:
                Duet EXP3HC firmware version 3.3beta (2021-01-16 19:11:54)
                Bootloader ID: SAME5x bootloader version 2.2 (2021-01-16b1)
                Never used RAM 154492, free system stack 142 words
                HEAT 92 CanAsync 92 CanRecv 79 TMC 30 MAIN 274 AIN 259
                Last reset 03:06:56 ago, cause: power up
                Last software reset data not available
                Driver 0: position 78458, 160.0 steps/mm, standstill, reads 11912, writes 2 timeouts 0, SG min/max 0/72, steps req 49298753 done 49298753
                Driver 1: position 82701, 160.0 steps/mm, standstill, reads 11912, writes 2 timeouts 0, SG min/max 0/72, steps req 50413393 done 50413393
                Driver 2: position 719839, 172.0 steps/mm, standstill, reads 11913, writes 2 timeouts 0, SG min/max 0/67, steps req 1793879 done 1791393
                Moves scheduled 210097, completed 210097, in progress 0, hiccups 15372, step errors 0
                Peak sync jitter 24, peak Rx sync delay 49110, resyncs 200, no step interrupt scheduled
                VIN: 24.4V, V12: 12.2V
                MCU temperature: min 44.1C, current 44.2C, max 44.4C
                Ticks since heat task active 40, ADC conversions started 11216032, completed 11216031, timed out 0
                Last sensors broadcast 0x00000000 found 0 44 ticks ago, loop time 0
                CAN messages queued 27, send timeouts 0, received 245625, lost 2226, free buffers 36, error reg 0

                So I am still not seeing any loss of XY done vs. requested steps, only a loss of 0.14% of E steps. This is with pressure advance set to zero. OTOH there have been 2226 lost CAN messages, presumably mostly movement messages, so moves will have been lost.

                My pause.g and resume.g are currently empty. You've provided your pause.g. Please provide your resume.g file too, then I will try again using your files, in case it makes a difference.

                I will work on fixing the lost CAN messages tomorrow or Monday.

                Duet WiFi hardware designer and firmware engineer
                Please do not ask me for Duet support via PM or email, use the forum
                http://www.escher3d.com, https://miscsolutions.wordpress.com

                undefined 1 Reply Last reply 16 Jan 2021, 23:07 Reply Quote 0
                • undefined
                  evomotors @dc42
                  last edited by 16 Jan 2021, 23:07

                  @dc42 said in Duet3 6CH + 3CH expansion board - Missing steps.:

                  Thanks for the additoinal data.

                  I've just run your print up to the 93% finished mark. This is the data:

                  m122b1
                  Diagnostics for board 1:
                  Duet EXP3HC firmware version 3.3beta (2021-01-16 19:11:54)
                  Bootloader ID: SAME5x bootloader version 2.2 (2021-01-16b1)
                  Never used RAM 154492, free system stack 142 words
                  HEAT 92 CanAsync 92 CanRecv 79 TMC 30 MAIN 274 AIN 259
                  Last reset 03:06:56 ago, cause: power up
                  Last software reset data not available
                  Driver 0: position 78458, 160.0 steps/mm, standstill, reads 11912, writes 2 timeouts 0, SG min/max 0/72, steps req 49298753 done 49298753
                  Driver 1: position 82701, 160.0 steps/mm, standstill, reads 11912, writes 2 timeouts 0, SG min/max 0/72, steps req 50413393 done 50413393
                  Driver 2: position 719839, 172.0 steps/mm, standstill, reads 11913, writes 2 timeouts 0, SG min/max 0/67, steps req 1793879 done 1791393
                  Moves scheduled 210097, completed 210097, in progress 0, hiccups 15372, step errors 0
                  Peak sync jitter 24, peak Rx sync delay 49110, resyncs 200, no step interrupt scheduled
                  VIN: 24.4V, V12: 12.2V
                  MCU temperature: min 44.1C, current 44.2C, max 44.4C
                  Ticks since heat task active 40, ADC conversions started 11216032, completed 11216031, timed out 0
                  Last sensors broadcast 0x00000000 found 0 44 ticks ago, loop time 0
                  CAN messages queued 27, send timeouts 0, received 245625, lost 2226, free buffers 36, error reg 0

                  So I am still not seeing any loss of XY done vs. requested steps, only a loss of 0.14% of E steps. This is with pressure advance set to zero. OTOH there have been 2226 lost CAN messages, presumably mostly movement messages, so moves will have been lost.

                  My pause.g and resume.g are currently empty. You've provided your pause.g. Please provide your resume.g file too, then I will try again using your files, in case it makes a difference.

                  I will work on fixing the lost CAN messages tomorrow or Monday.

                  So why it's not working for me? I'm not even talking about diagnostics. It is not printing when motors connected to expansion board. But works flawlessly when connected to Duet3.

                  All configs are attached. Compressed and renamed to txt
                  [0_1610838265664_RRF_3.3_Bakcup.zip](Uploading 100%) RRF_3.3_Bakcup.zip.txt

                  undefined 1 Reply Last reply 16 Jan 2021, 23:08 Reply Quote 0
                  • undefined
                    dc42 administrators @evomotors
                    last edited by 16 Jan 2021, 23:08

                    @evomotors said in Duet3 6CH + 3CH expansion board - Missing steps.:

                    It is not printing when motors connected to expansion board.

                    Please explain what you mean by this. I thought it was printing, but the print quality was poor.

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                    undefined 2 Replies Last reply 16 Jan 2021, 23:10 Reply Quote 0
                    • undefined
                      evomotors @dc42
                      last edited by 16 Jan 2021, 23:10

                      @dc42 said in Duet3 6CH + 3CH expansion board - Missing steps.:

                      @evomotors said in Duet3 6CH + 3CH expansion board - Missing steps.:

                      It is not printing when motors connected to expansion board.

                      Please explain what you mean by this. I thought it was printing, but the print quality was poor.

                      I'm taking about stuff that's happening on my videos. I cannot call this printing. Did you actually see the videos?

                      1 Reply Last reply Reply Quote 0
                      • undefined
                        evomotors @dc42
                        last edited by 16 Jan 2021, 23:12

                        @dc42 There are 2 videos I posted earlier in this thread. One showing motors connected to Duet3 and another then motors connected to expansion board. Please watch

                        1 Reply Last reply Reply Quote 0
                        • undefined
                          dc42 administrators
                          last edited by 16 Jan 2021, 23:31

                          I was confusing you with the other guy having a problem with print quality when the extruder is on an expansion board. I searched through the 128 posts in this thread and eventually found your video. It looks like it's printing correctly most of the time, but occasionally there is a big jolt which results in a shift in X and/or Y. That ties in with the lost CAN messages that are reported by M122 B1.

                          Duet WiFi hardware designer and firmware engineer
                          Please do not ask me for Duet support via PM or email, use the forum
                          http://www.escher3d.com, https://miscsolutions.wordpress.com

                          undefined undefined 2 Replies Last reply 16 Jan 2021, 23:37 Reply Quote 0
                          • undefined
                            evomotors @dc42
                            last edited by 16 Jan 2021, 23:37

                            @dc42 said in Duet3 6CH + 3CH expansion board - Missing steps.:

                            I was confusing you with the other guy having a problem with print quality when the extruder is on an expansion board. I searched through the 128 posts in this thread and eventually found your video. It looks like it's printing correctly most of the time, but occasionally there is a big jolt which results in a shift in X and/or Y. That ties in with the lost CAN messages that are reported by M122 B1.

                            The bottom line is when I connect XY motors to Duet3 board that problem disappears, but E steps still missing or not synchronized with XY movement and that produces bad quality print. Unfortunately I cannot connect extruder to duet3 as well as Duet3 has 6 stepper drivers, but I need 7.

                            1 Reply Last reply Reply Quote 0
                            • undefined
                              jbarros @dc42
                              last edited by 16 Jan 2021, 23:38

                              @dc42 said in Duet3 6CH + 3CH expansion board - Missing steps.:

                              I was confusing you with the other guy having a problem with print quality when the extruder is on an expansion board.

                              If you're refering to a ToolBoard then I'm the guy 🙂 and this is my thread: https://forum.duet3d.com/topic/20899/duet3d-6hc-toolboard-missing-filament-on-curves

                              1 Reply Last reply Reply Quote 0
                              • undefined
                                dc42 administrators
                                last edited by dc42 16 Jan 2021, 23:56

                                Yes, it figures that extrusion will be affected as well. Most of the moves in a print involve X, Y and E movement. So even if you move X and Y to the main board, there is still a CAN packet sent for the E movement.

                                I think the reason we haven't seen this before is that your print uses sequences of tiny movements, smaller than our other tests use. For example:

                                G0 F12000 X273.288 Y248.054
                                G1 F4800 X273.303 Y248.082 E0.00106
                                G1 X273.539 Y248.591 E0.01866
                                G1 X273.542 Y248.6 E0.00032
                                G1 X273.603 Y248.759 E0.00566
                                G1 X273.682 Y248.966 E0.00737
                                G1 X273.759 Y249.171 E0.00728
                                G1 X273.763 Y249.184 E0.00045

                                Here are those moves imported into a spreadsheet. The columns are X, Y, change in X, change in Y, move distance, and move time.

                                d21e1da1-2f59-4adb-93e4-f0637b734902-image.png

                                There are really small moves. The fourth one is less than 10 microns long and it will execute in just 120 microseconds. The longest one takes only 7 milliseconds and all the rest are below 3 milliseconds. So the system is having to process a very high rate of moves. Still, I don't see any evidence that the CAN bus is being overloaded, so I expect to resolve the issues with this print by improving the efficiency of processing the incoming move commands on the expansion board.

                                Duet WiFi hardware designer and firmware engineer
                                Please do not ask me for Duet support via PM or email, use the forum
                                http://www.escher3d.com, https://miscsolutions.wordpress.com

                                undefined 2 Replies Last reply 17 Jan 2021, 00:10 Reply Quote 0
                                • undefined
                                  evomotors @dc42
                                  last edited by 17 Jan 2021, 00:10

                                  @dc42 Could my issue exists due to faulty Duet board ? I'm dead in the water. I cannot print at all for several weeks already.

                                  undefined 1 Reply Last reply 17 Jan 2021, 01:26 Reply Quote 0
                                  • undefined
                                    Luke'sLaboratory @evomotors
                                    last edited by 17 Jan 2021, 01:26

                                    @evomotors

                                    @dc42 said:

                                    So I am still not seeing any loss of XY done vs. requested steps, only a loss of 0.14% of E steps. This is with pressure advance set to zero. OTOH there have been 2226 lost CAN messages, presumably mostly movement messages, so moves will have been lost.

                                    Luke
                                    http://lukeslab.online

                                    1 Reply Last reply Reply Quote 0
                                    • undefined
                                      evomotors @dc42
                                      last edited by 18 Jan 2021, 14:21

                                      @dc42 do you have any time estimates? I’m wondering when I’ll be able to print.

                                      1 Reply Last reply Reply Quote 0
                                      • undefined
                                        evomotors
                                        last edited by 19 Jan 2021, 18:48

                                        Can I have some updates? Please...

                                        1 Reply Last reply Reply Quote 1
                                        • undefined
                                          Phaedrux Moderator
                                          last edited by 19 Jan 2021, 18:52

                                          Still being worked on. Thanks for your patience.

                                          Z-Bot CoreXY Build | Thingiverse Profile

                                          1 Reply Last reply Reply Quote 0
                                          127 out of 153
                                          • First post
                                            127/153
                                            Last post
                                          Unless otherwise noted, all forum content is licensed under CC-BY-SA