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    Duet 3 mini 5+ need help with wiring and config

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    • Alucardiundefined
      Alucardi @Veti
      last edited by

      @Veti i tried and the value on the webui will just show 0. I have tried while homing to and it will not report a value, so bed will continue even if the pin is triggered by me. Pretty sure it should light blue when active also.

      I used these steps tio manually test also

      "To test the setup with the nozzle maybe a 100mm up from the bed you can check if the trigger signal is reaching the Duet by attempting to extend the pin by using the following command:

      M280 P0 S10

      If all is well the web interface should report a value of ”0” or "N/A" in the Z probe column when the pin is extended. You can then lightly touch the extended probe pin to check that the value in the Z probe Column changes to “1000”

      You can retract the pin again with

      M280 P0 S90"

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      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        How exactly do you have it wired? And what does the M558 M950 commands look like in your config.g? Does it match what I showed above?

        Are you wired to IO3 like this?

        BLTouchPitout.jpg

        Z-Bot CoreXY Build | Thingiverse Profile

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        • Alucardiundefined
          Alucardi @Phaedrux
          last edited by

          @Phaedrux it is just like in the picture, i made sure i have connection all the way to the probe using a multimeter so no broken wire.

          i have not amde any changes to M950 or M558, It is just as the config did them.

          M950 S0 C"io3.out"                                       ; create servo pin 0 for BLTouch
          M558 P9 C"^io3.in" H350 F350 T4800  B1                   ; set Z probe type to bltouch and the dive height + speeds + heater off while probing
          
          Phaedruxundefined 1 Reply Last reply Reply Quote 0
          • Phaedruxundefined
            Phaedrux Moderator @Alucardi
            last edited by

            @Alucardi said in Duet 3 mini 5+ need help with wiring and config:

            H350

            Change that to H5. 350mm dive height is possibly problematic. But maybe not your problem here.

            So just to recap. You're wired up to io_3 just like in the photo. Your config looks ok for io_3. And your deploy and retract macros look correct.

            When you power on does the BLTouch do a self test?
            Does sending M401 and M402 deploy and retract the pin?
            Does sending G30 deploy the pin?
            Does touching the pin after doing the G30 stop movement?

            Z-Bot CoreXY Build | Thingiverse Profile

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            • Alucardiundefined
              Alucardi @Phaedrux
              last edited by

              @Phaedrux

              When you power on does the BLTouch do a self test? Yes
              Does sending M401 and M402 deploy and retract the pin? Yes
              Does sending G30 deploy the pin? Yes it deploys during homing.
              Does touching the pin after doing the G30 stop movement? It reacts to me pushing it but wont stop bed going up.

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              • Phaedruxundefined
                Phaedrux Moderator
                last edited by Phaedrux

                Then I suspect a bad connection on the white wire to io_3.in. That's the trigger signal wire. Retest continuity. Recrimp it. Make sure it's in the shell properly. Make sure it's on the right pin.

                As an additional check, please send M98 P"config.g" and report any errors. Also send M558 P9 and see if it reports back what you'd expect.

                Also post your homeall.g

                Z-Bot CoreXY Build | Thingiverse Profile

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                • Alucardiundefined
                  Alucardi @Phaedrux
                  last edited by

                  @Phaedrux said in Duet 3 mini 5+ need help with wiring and config:

                  M558 P9

                  Gives me error
                  M558 P9
                  Error: M558: Missing Z probe pin name(s)

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                  • Alucardiundefined
                    Alucardi
                    last edited by

                    Homeall will be cleaned up and call for separate axels instead but i did it like this when i was trying to config sensorless homeing.

                    M400							; finishes all current moves and and thus clears the buffer
                    M913 X50 Y50 					; drop motor current to 33%
                    M569 P0.0 D3 V60   		 		; reduce V to ensure stealthChop is enabled
                    M569 P0.1 D3 V60   		 		; reduce V to ensure stealthChop is enabled
                    M915 P0.0 S1 R0 F0 H400		; sensitivity X, don’t take action, don’t filter
                    M915 P0.1 S1 R0 F0 H400		; sensitivity Y, don’t take action, don’t filter
                    M400 							; finishes all current moves and and thus clears the buffer
                    G91								; relative positioning
                    G1 H1 Z10 F5000	    	   		; lift Z relative to current position
                    G1 H1 X5
                    G4 P300
                    G1 H1 X20 F3000
                    G1 H1 X-400 F3000		   		; move to X
                    G1 H1 Y-5
                    G4 P200
                    G1 H1 Y-20 F3000
                    G1 H1 Y400 F3000 				; move to Y
                    M913 X100 Y100 					; return current to 100%
                    G90                   	  		; absolute positioning
                    G1 X167.5 Y167.5 F5000
                    G30 	  			    		; home Z by probing the bed
                    M402 							; retract probe
                    G1 Z5 F5000
                    M400							; finishes all current moves and and thus clears the buffer
                    M569 P0.0 D2  	    			; restore default for motor
                    M569 P0.1 D2					; restore default for motor
                    M913 X100 Y100 					; return current to 100%
                    M400							; finishes all current moves and and thus clears the buffer
                    
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                    • Phaedruxundefined
                      Phaedrux Moderator
                      last edited by

                      Ok how bout just M558

                      Z-Bot CoreXY Build | Thingiverse Profile

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                      • Alucardiundefined
                        Alucardi @Phaedrux
                        last edited by

                        @Phaedrux M558
                        Error: M558: Z probe 0 not found

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                        • Phaedruxundefined
                          Phaedrux Moderator
                          last edited by

                          Try again after a reboot, and post your entire config.g please.

                          Z-Bot CoreXY Build | Thingiverse Profile

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                          • Alucardiundefined
                            Alucardi @Phaedrux
                            last edited by Alucardi

                            @Phaedrux

                            now it worked. M558 P9 still give same error though

                            "m558
                            Z Probe 0: type 9, input pin io3.in, output pin nil, dive height 350.0mm, probe speed 350mm/min, travel speed 4800mm/min, recovery time 0.00 sec, heaters suspended, max taps 1, max diff 0.03"

                            G90                                                      ; send absolute coordinates...
                            M83                                                      ; ...but relative extruder moves
                            M550 P"Hevo"                                             ; set printer name
                            M669 K1                                                  ; select CoreXY mode
                            
                            ; Network
                            M552 S1                                                  ; enable network
                            M586 P0 S1                                               ; enable HTTP
                            M586 P1 S0                                               ; disable FTP
                            M586 P2 S0                                               ; disable Telnet
                            
                            ; Drives
                            M569 P0.0 S1 D2 	                        	         ; physical drive 0.0 goes forwards
                            M569 P0.1 S1 D2                      		             ; physical drive 0.1 goes forwards
                            M569 P0.2 S1 D2                                          ; physical drive 0.2 goes forwards
                            M569 P0.3 S1 D2                                          ; physical drive 0.3 goes forwards
                            M569 P0.4 S1 D2                                          ; physical drive 0.4 goes forwards
                            M584 X0.0 Y0.1 Z0.2:0.3 E0.4                             ; set drive mapping
                            M350 E16 I0	                                             ; configure microstepping without interpolation
                            M350 X16 Y16 Z8 I1                                       ; configure microstepping with interpolation
                            M92 X160.00 Y160.00 Z1600.00 E407.00                     ; set steps per mm
                            M566 X380.00 Y380.00 Z20.00 E4000.00                     ; set maximum instantaneous speed changes (mm/min)
                            M203 X12000.00 Y12000.00 Z500.00 E4000.00                ; set maximum speeds (mm/min)
                            M201 X1200.00 Y1200.00 Z300.00 E5000.00                  ; set accelerations (mm/s^2)
                            M906 X900 Y900 Z1200 E450 I30           	             ; set motor currents (mA) and motor idle factor in per cent
                            M84 S30                                                  ; Set idle timeout
                            
                            ; Axis Limits
                            M208 X0 Y0 Z-0.5 S1                                      ; set axis minima
                            M208 X330 Y343 Z450 S0                                   ; set axis maxima
                            M671 X-45:380 Y170:170 S1								 ; leadscrew positions
                            
                            ; Endstops
                            M574 X1 S3                                               ; configure sensorless endstop for high end on X
                            M574 Y2 S3                                               ; configure sensorless endstop for high end on Y
                            M574 Z1 S2                                               ; configure Z-probe endstop for low end on Z
                            
                            ; Z-Probe
                            M950 S0 C"io3.out"                                       ; create servo pin 0 for BLTouch
                            M558 P9 C"^io3.in" H350 F350 T4800 B1                    ; set Z probe type to bltouch and the dive height + speeds + heater off while probing
                            G31 P500 X25 Y-20 Z0.85                                  ; set Z probe trigger value, offset and trigger height
                            M557 X25:310 Y25:310 P6                                  ; define mesh grid + Probe points
                            
                            ; Heaters
                            M308 S0 P"temp0" Y"thermistor" T100000 B4138             ; configure sensor 0 as thermistor on pin temp0
                            M950 H0 C"out0" T0                                       ; create bed heater output on out0 and map it to sensor 0
                            M307 H0 B0 S0.70                                         ; disable bang-bang mode for the bed heater and set PWM limit
                            M140 H0                                                  ; map heated bed to heater 0
                            M143 H0 S120                                             ; set temperature limit for heater 0 to 120C
                            M308 S1 P"temp1" Y"thermistor" T500000 B4723 C1.19622e-7 ; configure sensor 1 as thermistor on pin temp1
                            M950 H1 C"out1" T1                                       ; create nozzle heater output on out1 and map it to sensor 1
                            M307 H1 B0 S1.00                                         ; disable bang-bang mode for heater  and set PWM limit
                            M143 H1 S350                                             ; set temperature limit for heater 1 to 350C
                            
                            ; Fans
                            M950 F0 C"out5" Q50                                      ; create fan 0 on pin out5 and set its frequency
                            M106 P0 C"Hotend fan " S0 H1 T50                         ; set fan 0 name and value. Thermostatic control is turned on
                            M950 F1 C"out6" Q1000                                    ; create fan 1 on pin out6 and set its frequency
                            M106 P1 C"Blower" S0 H-1                                 ; set fan 1 name and value. Thermostatic control is turned off
                            
                            ; Tools
                            M563 P0 D0 H1 F0 										 ; define tool 0
                            G10 P0 X0 Y0 Z0 										 ; set tool 0 axis offsets
                            G10 P0 R0 S0 											 ; set initial tool 0 active and standby temperatures to 0C
                            
                            ; Custom settings are not defined
                            
                            ; Miscellaneous
                            M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000"       ; set voltage thresholds and actions to run on power loss
                            
                            
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                            • Phaedruxundefined
                              Phaedrux Moderator
                              last edited by

                              Forget the M558 P9

                              Please fix the dive height M558 H5

                              Other than that it's down to the white trigger signal wire on io_3.in

                              Z-Bot CoreXY Build | Thingiverse Profile

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                              • Alucardiundefined
                                Alucardi @Phaedrux
                                last edited by

                                @Phaedrux guess it decided to break it self then during me changing the card. I have continuity all the way to under the connector on the blTouch it self down to the end of the connector going into the card.
                                I will however before i order a new one make a short harness and try it on the bench.

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                                • Alucardiundefined
                                  Alucardi @Phaedrux
                                  last edited by

                                  @Phaedrux it is working now. When i wired this up ages ago i connected ground further up so i only had to use one wire in the connector. I now reran one ground more. In the end i had 3 ground wires. that is why i had continuity on white.
                                  Only reason i figured it out was cause i had the stick from the multimeter on the ground at the mother board and hit the white wire by mistake.

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