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    Magnetic sensor reads sensitivy wrong.

    Scheduled Pinned Locked Moved
    Filament Monitor
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    • alankilianundefined
      alankilian
      last edited by alankilian

      They do explain how to make sure the screws are tight, and if they ARE tight, how to disassemble the housing and make a change so the magnet is moved closer to the sensor:

      @alankilian said in Magnetic sensor reads sensitivy wrong.:

      If they are already tight, you could remove the 2 long screws to separate the two plastic parts and very slightly sand down the bottom surface of the top one (the one with the PCB attached) to move the sensor closer to the magnet.

      SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

      Alucardiundefined 2 Replies Last reply Reply Quote 0
      • Alucardiundefined
        Alucardi @alankilian
        last edited by Alucardi

        This post is deleted!
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        • Alucardiundefined
          Alucardi @alankilian
          last edited by Alucardi

          @alankilian even if agc is correct it has no affect on my issue sadly.
          It seems like the magnet is hitting the pcb so it is not spinning now. So something is wrong. Since agc is correct could it be a defective sensor? It should not be hitting the sensor if agc is within spec right?

          Skärmklipp.PNG Skärmklipp2.PNG

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          • alankilianundefined
            alankilian
            last edited by

            @Alucardi said in Magnetic sensor reads sensitivy wrong.:

            the magnet is hitting the pcb

            Try adding small pieces of paper between the PCB and the case now to get the magnet a little farther away from the sensor.

            I think you ALMOST have it working.

            SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

            Alucardiundefined 1 Reply Last reply Reply Quote 1
            • Alucardiundefined
              Alucardi @alankilian
              last edited by

              @alankilian i there is another issue with sensor. Look how it looks. This can’t be normal.
              B8E59221-6CEB-4154-83D3-3BE929E3C607.jpeg

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              • alankilianundefined
                alankilian
                last edited by

                What looks wrong to you?

                It looks just like mine.

                IMG_5965.JPG

                SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

                Alucardiundefined 1 Reply Last reply Reply Quote 0
                • Alucardiundefined
                  Alucardi @alankilian
                  last edited by

                  @alankilian top of the axel looks rough but seems to be ok.

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                  • alankilianundefined
                    alankilian
                    last edited by

                    You said it was grinding against the sensor a little bot. That probably make it look different from mine.

                    Just add some paper strips here until the magnet turns freely, reassemble it and see if it works.

                    IMG_5965.JPG

                    SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

                    Alucardiundefined 1 Reply Last reply Reply Quote 0
                    • Alucardiundefined
                      Alucardi @alankilian
                      last edited by Alucardi

                      @alankilian added paper between the housings and that seem to have done the trick.

                      You happen to know if it is possible to calibrate e-steps with this?

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                      • alankilianundefined
                        alankilian
                        last edited by

                        added paper between the housings and that seem to have done the trick

                        HEY! That's great news!

                        You happen to know if it is possible to calibrate e-steps with this?

                        Hmm.....

                        What are you thinking?
                        The sensor measures how many times the wheel goes around.
                        How would you go from the sensor output of mm/rev to total mm extruded?
                        Could you measure the diameter of the wheel and use that?

                        I calibrate eSteps using the "Measure 120mm, extrude 100mm, measure the leftovers and see how close to 10mm it is" and it's been fine for me.

                        SeemeCNC Rostock Max V3 converted to V3.2 with a Duet2 Ethernet Firmware 3.2 and SE300

                        Alucardiundefined 1 Reply Last reply Reply Quote 0
                        • Alucardiundefined
                          Alucardi @alankilian
                          last edited by

                          @alankilian i do it like that to. but i thought this would be a more precise tool to use. It says "measured sensitivity 25.43mm/rev, min 97% max 103% over 410.6mm" i assume that means over 410.6mm of filament.

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