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    Firmware from 2.02 to 2.05.1

    Scheduled Pinned Locked Moved Solved
    Firmware installation
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    • droftartsundefined
      droftarts administrators @FlyingScot
      last edited by

      @flyingscot I’ve given you some upvotes, you should be able to post them now.

      Ian

      Bed-slinger - Mini5+ WiFi/1LC | RRP Fisher v1 - D2 WiFi | Polargraph - D2 WiFi | TronXY X5S - 6HC/Roto | CNC router - 6HC | Tractus3D T1250 - D2 Eth

      FlyingScotundefined 1 Reply Last reply Reply Quote 0
      • FlyingScotundefined
        FlyingScot @droftarts
        last edited by

        @droftarts
        M122
        === Diagnostics ===
        RepRapFirmware for Duet 2 WiFi/Ethernet version 2.01(RTOS) running on Duet WiFi 1.02 or later
        Board ID: 08DGM-917NK-F23T0-6JTF0-3SJ6J-TY84G
        Used output buffers: 3 of 20 (15 max)
        === RTOS ===
        Static ram: 28476
        Dynamic ram: 96284 of which 16 recycled
        Exception stack ram used: 508
        Never used ram: 5788
        Tasks: NETWORK(ready,464) HEAT(blocked,1248) MAIN(running,3132)
        Owned mutexes:
        === Platform ===
        Last reset 00:21:16 ago, cause: software
        Last software reset at 2021-05-14 23:23, reason: User, spinning module GCodes, available RAM 11488 bytes (slot 2)
        Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
        Error status: 16
        Free file entries: 9
        SD card 0 detected, interface speed: 20.0MBytes/sec
        SD card longest block write time: 360.5ms, max retries 0
        MCU temperature: min 31.3, current 31.9, max 32.4
        Supply voltage: min 11.8, current 11.9, max 12.2, under voltage events: 0, over voltage events: 0
        Driver 0: standstill, SG min/max 0/307
        Driver 1: standstill, SG min/max 0/225
        Driver 2: standstill, SG min/max 0/0
        Driver 3: standstill, SG min/max 0/259
        Driver 4: standstill, SG min/max 0/0
        Date/time: 2021-05-15 00:27:32
        Slowest loop: 78.47ms; fastest: 0.08ms
        === Move ===
        Hiccups: 0, StepErrors: 0, LaErrors: 0, FreeDm: 240, MinFreeDm: 150, MaxWait: 2ms, Underruns: 0, 0
        Scheduled moves: 1557, completed moves: 1558
        Bed compensation in use: none
        Bed probe heights: 0.355 -0.692 0.000 0.000 0.000
        === Heat ===
        Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1
        Heater 0 is on, I-accum = 0.2
        Heater 1 is on, I-accum = 0.8
        === GCodes ===
        Segments left: 0
        Stack records: 2 allocated, 0 in use
        Movement lock held by null
        http is idle in state(s) 0
        telnet is idle in state(s) 0
        file is idle in state(s) 0
        serial is idle in state(s) 0
        aux is idle in state(s) 0
        daemon is idle in state(s) 0
        queue is idle in state(s) 0
        autopause is idle in state(s) 0
        Code queue is empty.
        === Network ===
        Slowest loop: 362.38ms; fastest: 0.08ms
        Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
        HTTP sessions: 1 of 8

        • WiFi -
          Network state is running
          WiFi module is connected to access point
          Failed messages: pending 0, notready 0, noresp 1
          WiFi firmware version 1.22
          WiFi MAC address bc:dd:c2:89:a1:95
          WiFi Vcc 3.42, reset reason Turned on by main processor
          WiFi flash size 4194304, free heap 28600
          WiFi IP address 192.168.1.100
          WiFi signal strength -38dBm, reconnections 0, sleep mode modem
          Socket states: 0 0 0 0 0 0 0 0
          === Expansion ===

        This is the one that stutters and slows during radial moves both x and y motors.

        M122
        === Diagnostics ===
        RepRapFirmware for Duet 2 WiFi/Ethernet version 2.02(RTOS) running on Duet WiFi 1.02 or later
        Board ID: 08DGM-917NK-F23T0-6JTF0-3SJ6J-TY84G
        Used output buffers: 3 of 20 (13 max)
        === RTOS ===
        Static ram: 25524
        Dynamic ram: 98596 of which 12 recycled
        Exception stack ram used: 416
        Never used ram: 6524
        Tasks: NETWORK(ready,544) HEAT(blocked,1232) MAIN(running,1692) IDLE(ready,200)
        Owned mutexes:
        === Platform ===
        Last reset 00:07:15 ago, cause: software
        Last software reset at 2021-05-14 23:23, reason: User, spinning module GCodes, available RAM 11488 bytes (slot 2)
        Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
        Error status: 16
        Free file entries: 10
        SD card 0 detected, interface speed: 20.0MBytes/sec
        SD card longest block write time: 355.0ms, max retries 0
        MCU temperature: min 29.9, current 30.8, max 31.2
        Supply voltage: min 11.8, current 12.0, max 12.2, under voltage events: 0, over voltage events: 0, power good: yes
        Driver 0: standstill, SG min/max 0/299
        Driver 1: standstill, SG min/max 0/219
        Driver 2: standstill, SG min/max 0/31
        Driver 3: standstill, SG min/max 0/244
        Driver 4: standstill, SG min/max 0/45
        Date/time: 2021-05-14 23:59:23
        Cache data hit count 1572954085
        Slowest loop: 199.40ms; fastest: 0.07ms
        I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0
        === Move ===
        Hiccups: 0, StepErrors: 0, LaErrors: 0, FreeDm: 240, MinFreeDm: 150, MaxWait: 83163ms, Underruns: 0, 0
        Scheduled moves: 0, completed moves: 0
        Bed compensation in use: none
        Bed probe heights: 0.100 -0.095 0.000 0.000 0.000
        === Heat ===
        Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1
        Heater 0 is on, I-accum = 0.2
        Heater 1 is on, I-accum = 0.5
        === GCodes ===
        Segments left: 0
        Stack records: 2 allocated, 0 in use
        Movement lock held by null
        http is idle in state(s) 0
        telnet is idle in state(s) 0
        file is idle in state(s) 0
        serial is idle in state(s) 0
        aux is idle in state(s) 0
        daemon is idle in state(s) 0
        queue is idle in state(s) 0
        autopause is idle in state(s) 0
        Code queue is empty.
        === Network ===
        Slowest loop: 355.16ms; fastest: 0.00ms
        Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
        HTTP sessions: 1 of 8

        • WiFi -
          Network state is running
          WiFi module is connected to access point
          Failed messages: pending 0, notready 0, noresp 0
          WiFi firmware version 1.22
          WiFi MAC address bc:dd:c2:89:a1:95
          WiFi Vcc 3.42, reset reason Turned on by main processor
          WiFi flash size 4194304, free heap 29000
          WiFi IP address 192.168.1.100
          WiFi signal strength -39dBm, reconnections 0, sleep mode modem
          Socket states: 0 0 0 0 0 0 0 0
        FlyingScotundefined 1 Reply Last reply Reply Quote 0
        • FlyingScotundefined
          FlyingScot @FlyingScot
          last edited by

          @flyingscot

          Config

          ; General preferences
          M111 S0 ; Debugging off
          G21 ; Work in millimetres
          G90 ; Send absolute coordinates...
          M83 ; ...but relative extruder moves

          M555 P1 ; Set firmware compatibility to look like RepRapFirmare
          M564 H0 ; Limit axis

          :M572 D0 S0.22 ; Set extruder pressure advance.
          M667 S1 ; Select CoreXY mode

          ; Network
          M550 P"dBOT" ; Set machine name
          M552 S1 ; Enable network
          M587 S"BT-2TA8SR" P"9T9eXAftdqtvfJ" ; Configure access point. You can delete this line once connected
          M586 P0 S1 ; Enable HTTP
          M586 P1 S0 ; Disable FTP
          M586 P2 S0 ; Disable Telnet

          ; Drives
          M584 X0 Y1 Z2:4 E3 ; 2 Z motors connected to driver outputs 2 & 4
          M671 X-80:480 Y200:200 S10 ; Z lead screws are at (-80,200) (480,200)

          M579 X1.0015 Y1.003
          M569 P0 S0 ; Drive 0 goes forwards
          M569 P1 S1 ; Drive 1 goes forwards
          M569 P2 S0 ; Drive 2 goes backwards
          M569 P3 S1 ; Drive 3 goes backwards
          M569 P4 S0 ; Drive 4 goes backwards
          M350 X128 Y128 Z128 E16 ; Configure microstepping without interpolation
          M92 X800 Y800 Z3200 E408 ; Set steps per mm
          M566 X600 Y600 Z120 E2000 ; Set maximum instantaneous speed changes (mm/min)
          M203 X9000 Y9000 Z600 E6000 ; Set maximum speeds (mm/min)
          M201 X600 Y600 Z300 E5000 ; Set accelerations (mm/s^2)
          M205 X15 : set x and y jerk
          M906 X1000 Y1000 Z1200 E1200 I30 ; Set motor currents (mA) and motor idle factor in per cent
          M84 S30 ; Set idle timeout

          ; Axis Limits
          M208 X0 Y0 Z0 S1 ; Set axis minima
          M208 X380 Y380 Z400 S0 ; Set axis maxima

          ; Endstops
          M574 X1 Y2 S0 ; Set active low endstops

          ; Z-Probe
          M574 Z1 S2 ; Set endstops controlled by probe
          M558 P8 I1 X0 Y0 Z1 F200 T1000 ; Set Z probe type to unmodulated and the dive height + speeds
          G31 P1000 X-50 Y5 Z0.612 ; Set Z probe trigger value, offset and trigger height
          M557 X20:380 Y40:380 S75 ; Define mesh grid
          :M591 D0 P5 C4 S0

          ; Heaters
          M305 P0 T100000 B3950 C0 R4700 ; Set thermistor + ADC parameters for heater 0
          M143 H0 S120 ; Set temperature limit for heater 0 to 120C
          M305 P1 T100000 B4725 C7.06e-8 R4700 ; Set thermistor + ADC parameters for heater 1
          M143 H1 S285 ; Set temperature limit for heater 1 to 280C
          M307 H1 A318.9 C165.3 D2.7 B0
          M307 H0 A312.4 C710.8 D0.8 B0

          ; Fans
          M106 P0 S255 ; Set fan 0 tool fan half speed
          M106 P1 S1 I0 F500 T45 H1 ; Set fan 1 tool1 heatsink fan on at 45 degrees
          M106 P2 S0 ; Set fan 2 is turned off

          M501

          ; Tools
          M563 P0 D0 H1 F0 ; Define tool 0
          G10 P0 X0 Y0 Z0 ; Set tool 0 axis offsets
          G10 P0 R0 S0 ; Set initial tool 0 active and standby temperatures to 0C

          ; Automatic saving after power loss is not enabled

          ; Custom settings are not configured
          T0

          Phaedruxundefined 1 Reply Last reply Reply Quote 0
          • Phaedruxundefined
            Phaedrux Moderator @FlyingScot
            last edited by

            @flyingscot said in Firmware from 2.02 to 2.05.1:

            M350 X128 Y128 Z128 E16 ; Configure microstepping without interpolation
            M92 X800 Y800 Z3200 E408 ; Set steps per mm

            Try again, but switch to x16 microsteps with interpolation enabled I1. Adjust the steps per mm accordingly.

            The difference may be that it's using quad stepping in older firmware but not in the newer firmware.

            Z-Bot CoreXY Build | Thingiverse Profile

            FlyingScotundefined 1 Reply Last reply Reply Quote 0
            • FlyingScotundefined
              FlyingScot @Phaedrux
              last edited by

              @phaedrux Morning

              Unfortunately it is still the same.
              its strange printing a circle anticlockwise the speed is not constant it slows down between 2 o'clock and 10 o'clock and again between 8 o'clock and 4 o'clock,
              Back to 2.01 and its fine.
              Printer is a core x,y

              Change to config was:
              M350 X16 Y16 Z16 E16 I1 ; Configure microstepping
              M92 X100 Y100 Z400 E408 ; Set steps per mm

              Art

              dc42undefined 1 Reply Last reply Reply Quote 0
              • dc42undefined
                dc42 administrators @FlyingScot
                last edited by

                @flyingscot said in Firmware from 2.02 to 2.05.1:

                its strange printing a circle anticlockwise the speed is not constant it slows down between 2 o'clock and 10 o'clock and again between 8 o'clock and 4 o'clock,
                Back to 2.01 and its fine.

                Is the circle commanded using G2/G3 or using a sequence of G1 moves?

                The usual cause of slowing down on curves is jerk set too low in M566.

                Duet WiFi hardware designer and firmware engineer
                Please do not ask me for Duet support via PM or email, use the forum
                http://www.escher3d.com, https://miscsolutions.wordpress.com

                FlyingScotundefined 1 Reply Last reply Reply Quote 0
                • FlyingScotundefined
                  FlyingScot @dc42
                  last edited by FlyingScot

                  @dc42 I will look into not sure where to look. The test file is a cylinder drawn in solidworks saved as an stl and sliced with cura. it prints well with V2.01 but not in V2.02.

                  M566 in config is: M566 X600 Y600 Z120 E2000

                  Art

                  dc42undefined 1 Reply Last reply Reply Quote 0
                  • dc42undefined
                    dc42 administrators @FlyingScot
                    last edited by

                    @flyingscot, check that the GCode file does not contain any M205 commands, because they would change the jerk limit. I don't remember which RRF version was the first to support M205.

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                    FlyingScotundefined 1 Reply Last reply Reply Quote 0
                    • FlyingScotundefined
                      FlyingScot @dc42
                      last edited by

                      @dc42 The circle is generated by G1 moves and there is no M205 in the GCode.

                      Art

                      FlyingScotundefined 1 Reply Last reply Reply Quote 0
                      • FlyingScotundefined
                        FlyingScot @FlyingScot
                        last edited by

                        @flyingscot Its now running well on v2.05. It must have been the microstepping with interpolation that fixed it.

                        I did go back to 2.02 and the problem returned. Back to 2.05 and all is well.

                        Thanks for your help

                        Art

                        1 Reply Last reply Reply Quote 0
                        • Phaedruxundefined
                          Phaedrux Moderator
                          last edited by

                          Glad it's working well now. I suspect that if you'd run with the higher stepping on 2.05 and done a M122 it would have shown some hiccups.

                          Z-Bot CoreXY Build | Thingiverse Profile

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