Firmware from 2.02 to 2.05.1
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@flyingscot I’ve given you some upvotes, you should be able to post them now.
Ian
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@droftarts
M122
=== Diagnostics ===
RepRapFirmware for Duet 2 WiFi/Ethernet version 2.01(RTOS) running on Duet WiFi 1.02 or later
Board ID: 08DGM-917NK-F23T0-6JTF0-3SJ6J-TY84G
Used output buffers: 3 of 20 (15 max)
=== RTOS ===
Static ram: 28476
Dynamic ram: 96284 of which 16 recycled
Exception stack ram used: 508
Never used ram: 5788
Tasks: NETWORK(ready,464) HEAT(blocked,1248) MAIN(running,3132)
Owned mutexes:
=== Platform ===
Last reset 00:21:16 ago, cause: software
Last software reset at 2021-05-14 23:23, reason: User, spinning module GCodes, available RAM 11488 bytes (slot 2)
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
Error status: 16
Free file entries: 9
SD card 0 detected, interface speed: 20.0MBytes/sec
SD card longest block write time: 360.5ms, max retries 0
MCU temperature: min 31.3, current 31.9, max 32.4
Supply voltage: min 11.8, current 11.9, max 12.2, under voltage events: 0, over voltage events: 0
Driver 0: standstill, SG min/max 0/307
Driver 1: standstill, SG min/max 0/225
Driver 2: standstill, SG min/max 0/0
Driver 3: standstill, SG min/max 0/259
Driver 4: standstill, SG min/max 0/0
Date/time: 2021-05-15 00:27:32
Slowest loop: 78.47ms; fastest: 0.08ms
=== Move ===
Hiccups: 0, StepErrors: 0, LaErrors: 0, FreeDm: 240, MinFreeDm: 150, MaxWait: 2ms, Underruns: 0, 0
Scheduled moves: 1557, completed moves: 1558
Bed compensation in use: none
Bed probe heights: 0.355 -0.692 0.000 0.000 0.000
=== Heat ===
Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1
Heater 0 is on, I-accum = 0.2
Heater 1 is on, I-accum = 0.8
=== GCodes ===
Segments left: 0
Stack records: 2 allocated, 0 in use
Movement lock held by null
http is idle in state(s) 0
telnet is idle in state(s) 0
file is idle in state(s) 0
serial is idle in state(s) 0
aux is idle in state(s) 0
daemon is idle in state(s) 0
queue is idle in state(s) 0
autopause is idle in state(s) 0
Code queue is empty.
=== Network ===
Slowest loop: 362.38ms; fastest: 0.08ms
Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
HTTP sessions: 1 of 8- WiFi -
Network state is running
WiFi module is connected to access point
Failed messages: pending 0, notready 0, noresp 1
WiFi firmware version 1.22
WiFi MAC address bc:dd:c2:89:a1:95
WiFi Vcc 3.42, reset reason Turned on by main processor
WiFi flash size 4194304, free heap 28600
WiFi IP address 192.168.1.100
WiFi signal strength -38dBm, reconnections 0, sleep mode modem
Socket states: 0 0 0 0 0 0 0 0
=== Expansion ===
This is the one that stutters and slows during radial moves both x and y motors.
M122
=== Diagnostics ===
RepRapFirmware for Duet 2 WiFi/Ethernet version 2.02(RTOS) running on Duet WiFi 1.02 or later
Board ID: 08DGM-917NK-F23T0-6JTF0-3SJ6J-TY84G
Used output buffers: 3 of 20 (13 max)
=== RTOS ===
Static ram: 25524
Dynamic ram: 98596 of which 12 recycled
Exception stack ram used: 416
Never used ram: 6524
Tasks: NETWORK(ready,544) HEAT(blocked,1232) MAIN(running,1692) IDLE(ready,200)
Owned mutexes:
=== Platform ===
Last reset 00:07:15 ago, cause: software
Last software reset at 2021-05-14 23:23, reason: User, spinning module GCodes, available RAM 11488 bytes (slot 2)
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
Error status: 16
Free file entries: 10
SD card 0 detected, interface speed: 20.0MBytes/sec
SD card longest block write time: 355.0ms, max retries 0
MCU temperature: min 29.9, current 30.8, max 31.2
Supply voltage: min 11.8, current 12.0, max 12.2, under voltage events: 0, over voltage events: 0, power good: yes
Driver 0: standstill, SG min/max 0/299
Driver 1: standstill, SG min/max 0/219
Driver 2: standstill, SG min/max 0/31
Driver 3: standstill, SG min/max 0/244
Driver 4: standstill, SG min/max 0/45
Date/time: 2021-05-14 23:59:23
Cache data hit count 1572954085
Slowest loop: 199.40ms; fastest: 0.07ms
I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0
=== Move ===
Hiccups: 0, StepErrors: 0, LaErrors: 0, FreeDm: 240, MinFreeDm: 150, MaxWait: 83163ms, Underruns: 0, 0
Scheduled moves: 0, completed moves: 0
Bed compensation in use: none
Bed probe heights: 0.100 -0.095 0.000 0.000 0.000
=== Heat ===
Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1
Heater 0 is on, I-accum = 0.2
Heater 1 is on, I-accum = 0.5
=== GCodes ===
Segments left: 0
Stack records: 2 allocated, 0 in use
Movement lock held by null
http is idle in state(s) 0
telnet is idle in state(s) 0
file is idle in state(s) 0
serial is idle in state(s) 0
aux is idle in state(s) 0
daemon is idle in state(s) 0
queue is idle in state(s) 0
autopause is idle in state(s) 0
Code queue is empty.
=== Network ===
Slowest loop: 355.16ms; fastest: 0.00ms
Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
HTTP sessions: 1 of 8- WiFi -
Network state is running
WiFi module is connected to access point
Failed messages: pending 0, notready 0, noresp 0
WiFi firmware version 1.22
WiFi MAC address bc:dd:c2:89:a1:95
WiFi Vcc 3.42, reset reason Turned on by main processor
WiFi flash size 4194304, free heap 29000
WiFi IP address 192.168.1.100
WiFi signal strength -39dBm, reconnections 0, sleep mode modem
Socket states: 0 0 0 0 0 0 0 0
- WiFi -
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Config
; General preferences
M111 S0 ; Debugging off
G21 ; Work in millimetres
G90 ; Send absolute coordinates...
M83 ; ...but relative extruder movesM555 P1 ; Set firmware compatibility to look like RepRapFirmare
M564 H0 ; Limit axis:M572 D0 S0.22 ; Set extruder pressure advance.
M667 S1 ; Select CoreXY mode; Network
M550 P"dBOT" ; Set machine name
M552 S1 ; Enable network
M587 S"BT-2TA8SR" P"9T9eXAftdqtvfJ" ; Configure access point. You can delete this line once connected
M586 P0 S1 ; Enable HTTP
M586 P1 S0 ; Disable FTP
M586 P2 S0 ; Disable Telnet; Drives
M584 X0 Y1 Z2:4 E3 ; 2 Z motors connected to driver outputs 2 & 4
M671 X-80:480 Y200:200 S10 ; Z lead screws are at (-80,200) (480,200)M579 X1.0015 Y1.003
M569 P0 S0 ; Drive 0 goes forwards
M569 P1 S1 ; Drive 1 goes forwards
M569 P2 S0 ; Drive 2 goes backwards
M569 P3 S1 ; Drive 3 goes backwards
M569 P4 S0 ; Drive 4 goes backwards
M350 X128 Y128 Z128 E16 ; Configure microstepping without interpolation
M92 X800 Y800 Z3200 E408 ; Set steps per mm
M566 X600 Y600 Z120 E2000 ; Set maximum instantaneous speed changes (mm/min)
M203 X9000 Y9000 Z600 E6000 ; Set maximum speeds (mm/min)
M201 X600 Y600 Z300 E5000 ; Set accelerations (mm/s^2)
M205 X15 : set x and y jerk
M906 X1000 Y1000 Z1200 E1200 I30 ; Set motor currents (mA) and motor idle factor in per cent
M84 S30 ; Set idle timeout; Axis Limits
M208 X0 Y0 Z0 S1 ; Set axis minima
M208 X380 Y380 Z400 S0 ; Set axis maxima; Endstops
M574 X1 Y2 S0 ; Set active low endstops; Z-Probe
M574 Z1 S2 ; Set endstops controlled by probe
M558 P8 I1 X0 Y0 Z1 F200 T1000 ; Set Z probe type to unmodulated and the dive height + speeds
G31 P1000 X-50 Y5 Z0.612 ; Set Z probe trigger value, offset and trigger height
M557 X20:380 Y40:380 S75 ; Define mesh grid
:M591 D0 P5 C4 S0; Heaters
M305 P0 T100000 B3950 C0 R4700 ; Set thermistor + ADC parameters for heater 0
M143 H0 S120 ; Set temperature limit for heater 0 to 120C
M305 P1 T100000 B4725 C7.06e-8 R4700 ; Set thermistor + ADC parameters for heater 1
M143 H1 S285 ; Set temperature limit for heater 1 to 280C
M307 H1 A318.9 C165.3 D2.7 B0
M307 H0 A312.4 C710.8 D0.8 B0; Fans
M106 P0 S255 ; Set fan 0 tool fan half speed
M106 P1 S1 I0 F500 T45 H1 ; Set fan 1 tool1 heatsink fan on at 45 degrees
M106 P2 S0 ; Set fan 2 is turned offM501
; Tools
M563 P0 D0 H1 F0 ; Define tool 0
G10 P0 X0 Y0 Z0 ; Set tool 0 axis offsets
G10 P0 R0 S0 ; Set initial tool 0 active and standby temperatures to 0C; Automatic saving after power loss is not enabled
; Custom settings are not configured
T0 -
@flyingscot said in Firmware from 2.02 to 2.05.1:
M350 X128 Y128 Z128 E16 ; Configure microstepping without interpolation
M92 X800 Y800 Z3200 E408 ; Set steps per mmTry again, but switch to x16 microsteps with interpolation enabled
I1
. Adjust the steps per mm accordingly.The difference may be that it's using quad stepping in older firmware but not in the newer firmware.
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@phaedrux Morning
Unfortunately it is still the same.
its strange printing a circle anticlockwise the speed is not constant it slows down between 2 o'clock and 10 o'clock and again between 8 o'clock and 4 o'clock,
Back to 2.01 and its fine.
Printer is a core x,yChange to config was:
M350 X16 Y16 Z16 E16 I1 ; Configure microstepping
M92 X100 Y100 Z400 E408 ; Set steps per mmArt
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@flyingscot said in Firmware from 2.02 to 2.05.1:
its strange printing a circle anticlockwise the speed is not constant it slows down between 2 o'clock and 10 o'clock and again between 8 o'clock and 4 o'clock,
Back to 2.01 and its fine.Is the circle commanded using G2/G3 or using a sequence of G1 moves?
The usual cause of slowing down on curves is jerk set too low in M566.
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@dc42 I will look into not sure where to look. The test file is a cylinder drawn in solidworks saved as an stl and sliced with cura. it prints well with V2.01 but not in V2.02.
M566 in config is: M566 X600 Y600 Z120 E2000
Art
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@flyingscot, check that the GCode file does not contain any M205 commands, because they would change the jerk limit. I don't remember which RRF version was the first to support M205.
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@dc42 The circle is generated by G1 moves and there is no M205 in the GCode.
Art
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@flyingscot Its now running well on v2.05. It must have been the microstepping with interpolation that fixed it.
I did go back to 2.02 and the problem returned. Back to 2.05 and all is well.
Thanks for your help
Art
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Glad it's working well now. I suspect that if you'd run with the higher stepping on 2.05 and done a M122 it would have shown some hiccups.