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    M568 no longer needed?

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    • TechButterflyundefined
      TechButterfly
      last edited by

      I'm trying to start the hot end heater, but when I select a temp in DWC, I get a message that says M568 command is no longer needed. Where is that coming from? I can't find a reference to M568 anywhere. What does this message mean and how do I fix it? Thanks!

      deckingmanundefined 1 Reply Last reply Reply Quote 0
      • Phaedruxundefined
        Phaedrux Moderator
        last edited by Phaedrux

        Can you check your installed firmware and DWC versions? Sounds like you may have a mismatch. Or maybe a tool change file with the command in it?

        Need more information on your setup to know what's going on.

        Send M122 in the gcode console and post the results here.

        Z-Bot CoreXY Build | Thingiverse Profile

        TechButterflyundefined 1 Reply Last reply Reply Quote 0
        • TechButterflyundefined
          TechButterfly @Phaedrux
          last edited by

          @phaedrux

          I have a Panel Due 7i connected with the 4 pin cable. I actually can start the hot end heater from the Panel Due - it's DWC that gives me the M568 message.

          Here's the results of M122:

          m122
          === Diagnostics ===
          RepRapFirmware for Duet 3 MB6HC version 3.2.2 running on Duet 3 MB6HC v1.01 or later (SBC mode)
          Board ID: 08DJM-956BA-NA3TN-6J9F6-3SN6N-TB8UU
          Used output buffers: 1 of 40 (10 max)
          === RTOS ===
          Static ram: 149788
          Dynamic ram: 62448 of which 24 recycled
          Never used RAM 146572, free system stack 190 words
          Tasks: Linux(ready,75) HEAT(blocked,297) CanReceiv(blocked,927) CanSender(blocked,371) CanClock(blocked,352) TMC(blocked,53) MAIN(running,1165) IDLE(ready,19)
          Owned mutexes: HTTP(MAIN)
          === Platform ===
          Last reset 00:00:55 ago, cause: power up
          Last software reset at 2022-05-13 23:44, reason: User, none spinning, available RAM 146300, slot 2
          Software reset code 0x0012 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0x00000000 Task Linu Freestk 0 n/a
          Error status: 0x00
          Aux0 errors 0,0,0
          Aux1 errors 0,0,0
          MCU temperature: min 27.1, current 36.4, max 36.4
          Supply voltage: min 23.8, current 23.9, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes
          12V rail voltage: min 11.9, current 12.0, max 12.0, under voltage events: 0
          Driver 0: position 0, standstill, reads 52147, writes 14 timeouts 0, SG min/max 0/0
          Driver 1: position 0, standstill, reads 52147, writes 14 timeouts 0, SG min/max 0/0
          Driver 2: position 0, standstill, reads 52147, writes 14 timeouts 0, SG min/max 0/0
          Driver 3: position 0, standstill, reads 52147, writes 14 timeouts 0, SG min/max 0/0
          Driver 4: position 0, standstill, reads 52150, writes 11 timeouts 0, SG min/max 0/0
          Driver 5: position 0, standstill, reads 52150, writes 11 timeouts 0, SG min/max 0/0
          Date/time: 2022-05-14 00:12:21
          Slowest loop: 0.47ms; fastest: 0.05ms
          === Storage ===
          Free file entries: 10
          SD card 0 not detected, interface speed: 37.5MBytes/sec
          SD card longest read time 0.0ms, write time 0.0ms, max retries 0
          === Move ===
          DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000
          === MainDDARing ===
          Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
          === AuxDDARing ===
          Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
          === Heat ===
          Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
          === GCodes ===
          Segments left: 0
          Movement lock held by null
          HTTP* is doing "M122" in state(s) 0
          Telnet is idle in state(s) 0
          File is idle in state(s) 0
          USB is idle in state(s) 0
          Aux is idle in state(s) 0
          Trigger* is idle in state(s) 0
          Queue is idle in state(s) 0
          LCD is idle in state(s) 0
          SBC is idle in state(s) 0
          Daemon is idle in state(s) 0
          Aux2 is idle in state(s) 0
          Autopause is idle in state(s) 0
          Code queue is empty.
          === CAN ===
          Messages queued 103, send timeouts 379, received 0, lost 0, longest wait 0ms for reply type 0, free buffers 48
          === SBC interface ===
          State: 4, failed transfers: 1
          Last transfer: 1ms ago
          RX/TX seq numbers: 25240/25240
          SPI underruns 0, overruns 0
          Number of disconnects: 0, IAP RAM available 0x2c8a8
          Buffer RX/TX: 0/0-0
          === Duet Control Server ===
          Duet Control Server v3.4.1-rc1
          Code buffer space: 4096
          Configured SPI speed: 8000000Hz, TfrRdy pin glitches: 0
          Full transfers per second: 18.05, max time between full transfers: 215.8ms, max pin wait times: 10.3ms/74.3ms
          Codes per second: 0.03
          Maximum length of RX/TX data transfers: 2556/688
          
          dc42undefined 1 Reply Last reply Reply Quote 0
          • deckingmanundefined
            deckingman @TechButterfly
            last edited by

            @techbutterfly M568 was originally used to enable tool mixing up until firmware 1.19 or thereabouts. After that, setting a mixing ratio using M567 will automatically enable it. So M568 was deprecated and can now be used to set tool temperatures. So check all your configuration files for any instances of M568 and remove any that aren't being used to set tool temperatures.

            Ian
            https://somei3deas.wordpress.com/
            https://www.youtube.com/@deckingman

            1 Reply Last reply Reply Quote 0
            • dc42undefined
              dc42 administrators @TechButterfly
              last edited by

              @techbutterfly you are running an old version of firmware (version 3.2.2) and I suspect you are running a later version of DWC.

              Duet WiFi hardware designer and firmware engineer
              Please do not ask me for Duet support via PM or email, use the forum
              http://www.escher3d.com, https://miscsolutions.wordpress.com

              TechButterflyundefined 1 Reply Last reply Reply Quote 0
              • TechButterflyundefined
                TechButterfly @dc42
                last edited by

                @dc42 Hmm. Okay - can you tell me how, or point me to some instructions on how to upgrade to the correct firmware? Can it be done through the pi? I don't have easy access to the USB port on the MB6HC.

                Stephen6309undefined 1 Reply Last reply Reply Quote 0
                • Stephen6309undefined
                  Stephen6309 @TechButterfly
                  last edited by Stephen6309

                  @techbutterfly For the pi run: sudo apt update and then sudo apt upgrade in a termial like PuTTY.

                  TechButterflyundefined 1 Reply Last reply Reply Quote 0
                  • TechButterflyundefined
                    TechButterfly @Stephen6309
                    last edited by

                    @stephen6309 Thanks. I ran those but they didn't seem to do much and M122 still shows version 3.2.2. Can you tell what's going on here?

                    pi@duet3:~ $ sudo apt update
                    Get:1 http://raspbian.raspberrypi.org/raspbian buster InRelease [15.0 kB]
                    Hit:2 http://archive.raspberrypi.org/debian buster InRelease
                    Hit:3 https://pkg.duet3d.com unstable InRelease
                    Hit:4 https://pkg.duet3d.com stable InRelease
                    Get:5 http://raspbian.raspberrypi.org/raspbian buster/main armhf Packages [13.0                                                                                                                                                              MB]
                    Fetched 13.0 MB in 25s (514 kB/s)
                    Reading package lists... Done
                    Building dependency tree
                    Reading state information... Done
                    6 packages can be upgraded. Run 'apt list --upgradable' to see them.
                    
                    pi@duet3:~ $ apt list --upgradable
                    Listing... Done
                    libpulse-mainloop-glib0/oldstable 12.2-4+deb10u1+rpi3 armhf [upgradable from: 12.2-4+deb10u1]
                    libpulse0/oldstable 12.2-4+deb10u1+rpi3 armhf [upgradable from: 12.2-4+deb10u1]
                    libpulsedsp/oldstable 12.2-4+deb10u1+rpi3 armhf [upgradable from: 12.2-4+deb10u1]
                    pulseaudio-module-bluetooth/oldstable 12.2-4+deb10u1+rpi3 armhf [upgradable from: 12.2-4+deb10u1]
                    pulseaudio-utils/oldstable 12.2-4+deb10u1+rpi3 armhf [upgradable from: 12.2-4+deb10u1]
                    pulseaudio/oldstable 12.2-4+deb10u1+rpi3 armhf [upgradable from: 12.2-4+deb10u1]
                    
                    pi@duet3:~ $ sudo apt upgrade
                    Reading package lists... Done
                    Building dependency tree
                    Reading state information... Done
                    Calculating upgrade... Done
                    The following packages were automatically installed and are no longer required:
                      libxss1 rpi-eeprom-images
                    Use 'sudo apt autoremove' to remove them.
                    The following packages have been kept back:
                      libpulse-mainloop-glib0 libpulse0 libpulsedsp pulseaudio pulseaudio-module-bluetooth pulseaudio-utils
                    0 upgraded, 0 newly installed, 0 to remove and 6 not upgraded.
                    
                    Stephen6309undefined 1 Reply Last reply Reply Quote 0
                    • Stephen6309undefined
                      Stephen6309 @TechButterfly
                      last edited by

                      @techbutterfly Sometimes I have to run it at least twice. You might try a reboot of the pi, and run it again. For the unstable, it goes to 3.4.1.RC1 and stable is 3.4.0.

                      TechButterflyundefined 1 Reply Last reply Reply Quote 0
                      • TechButterflyundefined
                        TechButterfly @Stephen6309
                        last edited by

                        @stephen6309 Thanks. Is there a way to specify stable or unstable? If there is, which should I choose?

                        Stephen6309undefined 1 Reply Last reply Reply Quote 0
                        • Stephen6309undefined
                          Stephen6309 @TechButterfly
                          last edited by

                          @techbutterfly See: https://docs.duet3d.com/en/User_manual/Machine_configuration/DSF_RPi

                          Unstable, if you want to try beta/rc firmware, but it may have bugs.

                          Stable is the released firmware.

                          TechButterflyundefined 1 Reply Last reply Reply Quote 0
                          • TechButterflyundefined
                            TechButterfly @Stephen6309
                            last edited by

                            @stephen6309 I would like to use the stable version. I followed the directions change to stable. But I'm still not getting any actual updates. I did run both update and upgrade multiple times and also rebooted the pi. What else can I try?

                            Here's what I'm getting in Putty:

                            pi@duet3:~ $ sudo apt update
                            Hit:1 http://raspbian.raspberrypi.org/raspbian buster InRelease
                            Hit:2 http://archive.raspberrypi.org/debian buster InRelease
                            Hit:3 https://pkg.duet3d.com stable InRelease
                            Reading package lists... Done
                            Building dependency tree
                            Reading state information... Done
                            6 packages can be upgraded. Run 'apt list --upgradable' to see them.
                            pi@duet3:~ $ sudo apt upgrade
                            Reading package lists... Done
                            Building dependency tree
                            Reading state information... Done
                            Calculating upgrade... Done
                            The following packages have been kept back:
                              libpulse-mainloop-glib0 libpulse0 libpulsedsp pulseaudio
                              pulseaudio-module-bluetooth pulseaudio-utils
                            0 upgraded, 0 newly installed, 0 to remove and 6 not upgraded.
                            pi@duet3:~ $
                            
                            
                            Stephen6309undefined 1 Reply Last reply Reply Quote 0
                            • Stephen6309undefined
                              Stephen6309 @TechButterfly
                              last edited by

                              @techbutterfly When it didn't work the first time, running it again fixed it. Have you tried turning it off and on again. 🙂

                              TechButterflyundefined 1 Reply Last reply Reply Quote 0
                              • TechButterflyundefined
                                TechButterfly @Stephen6309
                                last edited by

                                @stephen6309 Thanks, but I have turned it off and on again - twice. And also run both update and upgrade multiple times. I don't know what else to do. I was so close to getting this fancy duet working.

                                Stephen6309undefined 1 Reply Last reply Reply Quote 0
                                • Stephen6309undefined
                                  Stephen6309 @TechButterfly
                                  last edited by

                                  @techbutterfly The only suggestion I have left is to redo the PI sd card with the image at https://docs.duet3d.com/en/User_manual/Machine_configuration/SBC_setup

                                  Don't forget to save the sys files and macro files.

                                  1 Reply Last reply Reply Quote 0
                                  • Phaedruxundefined
                                    Phaedrux Moderator
                                    last edited by

                                    The firmware on the Duet seems not to have gotten updated during the sudo apt update, etc.

                                    You can try updating the firmware manually in a couple of ways.

                                    First, if you want to stay on the stable release branch, you can downgrade the pi software using these steps.

                                    https://docs.duet3d.com/en/User_manual/Machine_configuration/DSF_RPi#switch-to-stable-packages

                                    Then you can try and manually update the firmware by uploading the firmware bin file in DWC. It may prompt to install it. If not, you can send M997 to trigger an update.

                                    Upload these files in this order.

                                    https://github.com/Duet3D/RepRapFirmware/releases/download/3.4.0/Duet3_SDiap32_MB6HC.bin

                                    https://github.com/Duet3D/RepRapFirmware/releases/download/3.4.0/Duet3Firmware_MB6HC.bin

                                    That should get you to 3.4 all around. If not, and it's still stuck, you can use USB and bossa software to flash it with a PC as described here:

                                    https://docs.duet3d.com/en/User_manual/RepRapFirmware/Updating_firmware#fallback-procedure-2

                                    Z-Bot CoreXY Build | Thingiverse Profile

                                    TechButterflyundefined 1 Reply Last reply Reply Quote 0
                                    • TechButterflyundefined
                                      TechButterfly @Phaedrux
                                      last edited by

                                      @phaedrux Thanks for those detailed instructions. I've completed them and now I'm able to start the heaters as expected. Here's the result of M122, just for a sanity check. Does everything look right now?

                                      M122
                                      === Diagnostics ===
                                      RepRapFirmware for Duet 3 MB6HC version 3.4.0 (2022-03-15 18:57:24) running on Duet 3 MB6HC v1.01 or later (SBC mode)
                                      Board ID: 08DJM-956BA-NA3TN-6J9F6-3SN6N-TB8UU
                                      Used output buffers: 1 of 40 (13 max)
                                      === RTOS ===
                                      Static ram: 151000
                                      Dynamic ram: 65728 of which 424 recycled
                                      Never used RAM 133520, free system stack 216 words
                                      Tasks: SBC(ready,0.6%,487) HEAT(notifyWait,0.0%,321) Move(notifyWait,0.0%,352) CanReceiv(notifyWait,0.0%,944) CanSender(notifyWait,0.0%,374) CanClock(delaying,0.0%,333) TMC(notifyWait,7.8%,92) MAIN(running,91.6%,923) IDLE(ready,0.0%,30), total 100.0%
                                      Owned mutexes: HTTP(MAIN)
                                      === Platform ===
                                      Last reset 00:03:06 ago, cause: software
                                      Last software reset at 2022-05-14 14:47, reason: User, none spinning, available RAM 133520, slot 0
                                      Software reset code 0x0012 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0x00000000 Task SBC Freestk 0 n/a
                                      Error status: 0x00
                                      Aux0 errors 0,0,0
                                      Step timer max interval 131
                                      MCU temperature: min 43.0, current 43.1, max 43.2
                                      Supply voltage: min 23.8, current 23.9, max 23.9, under voltage events: 0, over voltage events: 0, power good: yes
                                      12V rail voltage: min 12.0, current 12.0, max 12.0, under voltage events: 0
                                      Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                                      Events: 0 queued, 0 completed
                                      Driver 0: standstill, SG min n/a, mspos 8, reads 23991, writes 0 timeouts 0
                                      Driver 1: standstill, SG min n/a, mspos 8, reads 23991, writes 0 timeouts 0
                                      Driver 2: standstill, SG min n/a, mspos 8, reads 23991, writes 0 timeouts 0
                                      Driver 3: standstill, SG min n/a, mspos 8, reads 23991, writes 0 timeouts 0
                                      Driver 4: standstill, SG min n/a, mspos 8, reads 23991, writes 0 timeouts 0
                                      Driver 5: standstill, SG min n/a, mspos 8, reads 23991, writes 0 timeouts 0
                                      Date/time: 2022-05-14 14:50:30
                                      Slowest loop: 1.05ms; fastest: 0.05ms
                                      === Storage ===
                                      Free file entries: 10
                                      SD card 0 not detected, interface speed: 37.5MBytes/sec
                                      SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                                      === Move ===
                                      DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                                      === MainDDARing ===
                                      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                      === AuxDDARing ===
                                      Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                      === Heat ===
                                      Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                                      === GCodes ===
                                      Segments left: 0
                                      Movement lock held by null
                                      HTTP* is doing "M122" in state(s) 0
                                      Telnet is idle in state(s) 0
                                      File is idle in state(s) 0
                                      USB is idle in state(s) 0
                                      Aux is idle in state(s) 0
                                      Trigger* is idle in state(s) 0
                                      Queue is idle in state(s) 0
                                      LCD is idle in state(s) 0
                                      SBC is idle in state(s) 0
                                      Daemon is idle in state(s) 0
                                      Aux2 is idle in state(s) 0
                                      Autopause is idle in state(s) 0
                                      Code queue is empty
                                      === CAN ===
                                      Messages queued 39, received 0, lost 0, boc 0
                                      Longest wait 0ms for reply type 0, peak Tx sync delay 0, free buffers 50 (min 50), ts 22/0/0
                                      Tx timeouts 0,0,22,0,0,17 last cancelled message type 30 dest 127
                                      === SBC interface ===
                                      Transfer state: 4, failed transfers: 0, checksum errors: 0
                                      RX/TX seq numbers: 7579/7579
                                      SPI underruns 0, overruns 0
                                      State: 5, disconnects: 0, timeouts: 0, IAP RAM available 0x2b880
                                      Buffer RX/TX: 0/0-0, open files: 0
                                      === Duet Control Server ===
                                      Duet Control Server v3.4.0
                                      Code buffer space: 4096
                                      Configured SPI speed: 8000000Hz, TfrRdy pin glitches: 0
                                      Full transfers per second: 39.59, max time between full transfers: 31.1ms, max pin wait times: 26.2ms/0.1ms
                                      Codes per second: 0.24
                                      Maximum length of RX/TX data transfers: 3108/820
                                      
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                                      • TechButterflyundefined TechButterfly has marked this topic as solved
                                      • Phaedruxundefined
                                        Phaedrux Moderator
                                        last edited by

                                        Yes that looks good now. You're versions match.

                                        Z-Bot CoreXY Build | Thingiverse Profile

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