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    inductive Z-probe problem after firmware upgrade

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    • Phaedruxundefined
      Phaedrux Moderator
      last edited by

      What do you have in your homing files?

      @rubinkingma said in inductive Z-probe problem after firmware upgrade:

      ; Z probe
      M558 P5 X0 Y0 Z1 ; Analog Z probe, also used for homing the Z axis
      G31 X 28 Y12 Z0.4 P500 ; Set the probe height and threshold (put your own values here)

      You should remove the old RRF2 commands.

      Z-Bot CoreXY Build | Thingiverse Profile

      rubinkingmaundefined 1 Reply Last reply Reply Quote 0
      • rubinkingmaundefined
        rubinkingma @Th0mpy
        last edited by

        @th0mpy

        Weird, when i dont it complains about "cant enable endstop".

        Th0mpyundefined 1 Reply Last reply Reply Quote 0
        • Th0mpyundefined
          Th0mpy @rubinkingma
          last edited by Th0mpy

          @rubinkingma

          Can you paste in your homeall.g and homez.g?

          Sorry, what board are you using? Just to confirm the pins.

          Usually the team that scores the most points wins the game.

          rubinkingmaundefined 1 Reply Last reply Reply Quote 0
          • rubinkingmaundefined
            rubinkingma @Phaedrux
            last edited by

            @phaedrux

            Thank you for your reply, what part is RRF2 ?
            I got to 3xx firmware today after running 1.19 since 2017

            Used the configurator and while i could have dropped some old stuff in there looking for solutions i'm not at the point where i can see the difference between old and new config.

            1 Reply Last reply Reply Quote 0
            • rubinkingmaundefined
              rubinkingma @Th0mpy
              last edited by

              @th0mpy

              homeall ( I have been dicking around with this for mesh compensation)

              ; homeall.g
              ; called to home all axes
              ;
              ; generated by RepRapFirmware Configuration Tool v3.3.13 on Mon Sep 19 2022 15:01:08 GMT+0200 (Midden-Europese zomertijd)
              ;G91 ; relative positioning
              ;G1 H2 Z5 F6000 ; lift Z relative to current position
              ;G1 H1 X-305 Y-203 F1800 ; move quickly to X or Y endstop and stop there (first pass)
              ;G1 H1 X-305 ; home X axis
              ;G1 H1 Y-203 ; home Y axis
              ;G1 X5 Y5 F6000 ; go back a few mm
              ;G1 H1 X-305 F360 ; move slowly to X axis endstop once more (second pass)
              ;G1 H1 Y-203 ; then move slowly to Y axis endstop
              ;G1 H1 Z-165 F360 ; move Z down stopping at the endstop
              ;G90 ; absolute positioning
              ;G92 Z0 ; set Z position to axis minimum (you may want to adjust this)

              ; Uncomment the following lines to lift Z after probing
              ;G91 ; relative positioning
              ;G1 Z5 F100 ; lift Z relative to current position
              ;G90 ; absolute positioning

              ; homeall.g
              ; called to home all axes
              ;
              ; generated by RepRapFirmware Configuration Tool v3.3.13 on Mon Sep 19 2022 15:01:08 GMT+0200 (Midden-Europese zomertijd)
              G91 ; relative positioning
              G1 H2 Z5 F6000 ; lift Z relative to current position
              G1 H1 X-305 Y-203 F1800 ; move quickly to X or Y endstop and stop there (first pass)
              G1 H2 X5 Y5 F6000 ; go back a few mm
              G1 H1 X-305 F360 ; move slowly to X axis endstop once more (second pass)
              G1 H1 Y-203 ; then move slowly to Y axis endstop
              G1 H1 Z-165 F360 ; move Z down stopping at the endstop
              G1 H2 Z5 F6000
              G90 ; absolute positioning
              G1 X150 Y100 F6000
              G30 ;probe bed

              ; Uncomment the following lines to lift Z after probing
              ;G91 ; relative positioning
              ;G1 Z5 F100 ; lift Z relative to current position
              ;G90 ; absolute positioning

              Home Z

              ; homez.g
              ; called to home the Z axis
              ;
              ; generated by RepRapFirmware Configuration Tool v3.3.13 on Mon Sep 19 2022 15:01:08 GMT+0200 (Midden-Europese zomertijd)
              G91 ; relative positioning
              G1 H2 Z5 F600 ; lift Z relative to current position
              G1 H1 Z-165 F1000 ; move Z down until the endstop is triggered (first pass)
              G1 Z5 F1000 ; go back a few mm
              G1 H1 Z-100 F360 ; move slowly to Z axis endstop once more (second pass)
              G92 Z0 ; set Z position to axis minimum (you may want to adjust this)

              ; Uncomment the following lines to lift Z after probing
              ;G91 ; relative positioning
              ;G1 Z5 F100 ; lift Z relative to current position
              ;G90 ; absolute positioning

              Phaedruxundefined 1 Reply Last reply Reply Quote 0
              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                Ah, nevermind about the old config parts. I see now that it's two separate configs. I've edited your post to make it a bit clearer.

                Can you send M122 and M98 P"config.g" in the console and copy and paste the results here?

                Z-Bot CoreXY Build | Thingiverse Profile

                rubinkingmaundefined Th0mpyundefined 2 Replies Last reply Reply Quote 0
                • rubinkingmaundefined
                  rubinkingma @Phaedrux
                  last edited by

                  @phaedrux

                  M122:

                  M122
                  === Diagnostics ===
                  RepRapFirmware for Duet 2 WiFi/Ethernet version 3.4.2 (2022-09-13 15:11:16) running on Duet WiFi 1.02 or later
                  Board ID: 08DAM-9K9K2-NGNSN-6J9D6-3S46T-TPSRK
                  Used output buffers: 1 of 26 (24 max)
                  === RTOS ===
                  Static ram: 23860
                  Dynamic ram: 74924 of which 40 recycled
                  Never used RAM 13184, free system stack 106 words
                  Tasks: NETWORK(ready,15.2%,237) HEAT(notifyWait,0.0%,333) Move(notifyWait,0.0%,292) MAIN(running,84.8%,442) IDLE(ready,0.0%,30), total 100.0%
                  Owned mutexes: WiFi(NETWORK)
                  === Platform ===
                  Last reset 01:25:43 ago, cause: power up
                  Last software reset at 2022-09-19 20:21, reason: User, GCodes spinning, available RAM 13256, slot 0
                  Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                  Error status: 0x08
                  Aux0 errors 0,0,0
                  Step timer max interval 0
                  MCU temperature: min 40.0, current 40.5, max 43.3
                  Supply voltage: min 24.3, current 24.5, max 24.7, under voltage events: 0, over voltage events: 0, power good: yes
                  Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                  Events: 0 queued, 0 completed
                  Driver 0: standstill, SG min 31
                  Driver 1: standstill, SG min 38
                  Driver 2: standstill, SG min 13
                  Driver 3: standstill, SG min n/a
                  Driver 4: standstill, SG min n/a
                  Driver 5:
                  Driver 6:
                  Driver 7:
                  Driver 8:
                  Driver 9:
                  Driver 10:
                  Driver 11:
                  Date/time: 2022-09-19 21:49:25
                  Cache data hit count 4294967295
                  Slowest loop: 8.64ms; fastest: 0.17ms
                  I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                  === Storage ===
                  Free file entries: 10
                  SD card 0 detected, interface speed: 20.0MBytes/sec
                  SD card longest read time 0.7ms, write time 24.2ms, max retries 0
                  === Move ===
                  DMs created 83, segments created 3, maxWait 1254428ms, bed compensation in use: mesh, comp offset 0.000
                  === MainDDARing ===
                  Scheduled moves 883, completed 883, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                  === AuxDDARing ===
                  Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                  === Heat ===
                  Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                  === GCodes ===
                  Segments left: 0
                  Movement lock held by null
                  HTTP is idle in state(s) 0
                  Telnet is idle in state(s) 0
                  File is idle in state(s) 0
                  USB is idle in state(s) 0
                  Aux is idle in state(s) 0
                  Trigger is idle in state(s) 0
                  Queue is idle in state(s) 0
                  LCD is idle in state(s) 0
                  Daemon is idle in state(s) 0
                  Autopause is idle in state(s) 0
                  Code queue is empty
                  === Network ===
                  Slowest loop: 243.62ms; fastest: 0.07ms
                  Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
                  HTTP sessions: 1 of 8
                  = WiFi =
                  Network state is active
                  WiFi module is connected to access point
                  Failed messages: pending 0, notready 0, noresp 0
                  WiFi firmware version 1.27
                  WiFi MAC address 5c:cf:7f:f7:de:92
                  WiFi Vcc 3.37, reset reason Turned on by main processor
                  WiFi flash size 4194304, free heap 25864
                  WiFi IP address 192.168.1.201
                  WiFi signal strength -77dBm, mode 802.11n, reconnections 0, sleep mode modem
                  Clock register 00002002
                  Socket states: 0 0 0 0 0 0 0 0

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                  • Th0mpyundefined
                    Th0mpy @Phaedrux
                    last edited by

                    @phaedrux

                    I see the issue.

                    In the homez.g file change this:

                    G91 ; relative positioning
                    G1 H2 Z5 F600 ; lift Z relative to current position
                    G1 H1 Z-165 F1000 ; move Z down until the endstop is triggered (first pass)
                    G1 Z5 F1000 ; go back a few mm
                    G1 H1 Z-100 F360 ; move slowly to Z axis endstop once more (second pass)
                    G92 Z0 ; set Z position to axis minimum (you may want to adjust this)
                    

                    to this

                    G1 X150 Y150 F6000
                    G91 ; relative positioning
                    G1 H2 Z5 F600 ; lift Z relative to current position
                    G90
                    G30
                    

                    Usually the team that scores the most points wins the game.

                    1 Reply Last reply Reply Quote 0
                    • Phaedruxundefined
                      Phaedrux Moderator @rubinkingma
                      last edited by

                      Your homez.g file is still looking for an endstop. It needs to be changed to use G30 instead of a G1 H1 Z move in order to use the probe.

                      Your homeall.g is using both an endstop move AND a G30 to probe.

                      Here are the corrected files

                      ; homeall.g
                      ; called to home all axes
                      ;
                      ; generated by RepRapFirmware Configuration Tool v3.3.13 on Mon Sep 19 2022 15:01:08 GMT+0200 (Midden-Europese zomertijd)
                      G91 ; relative positioning
                      G1 H2 Z5 F6000 ; lift Z relative to current position
                      G1 H1 X-305 Y-203 F1800 ; move quickly to X or Y endstop and stop there (first pass)
                      G1 H2 X5 Y5 F6000 ; go back a few mm
                      G1 H1 X-305 F360 ; move slowly to X axis endstop once more (second pass)
                      G1 H1 Y-203 ; then move slowly to Y axis endstop
                      G90 ; absolute positioning
                      G1 X150 Y100 F6000
                      G30 ;probe bed
                      
                      ; homez.g
                      ; called to home the Z axis
                      ;
                      ; generated by RepRapFirmware Configuration Tool v3.3.13 on Mon Sep 19 2022 15:01:08 GMT+0200 (Midden-Europese zomertijd)
                      G90 ; absolute positioning
                      G1 X150 Y100 F6000
                      G30 ;probe bed
                      

                      Z-Bot CoreXY Build | Thingiverse Profile

                      Th0mpyundefined 1 Reply Last reply Reply Quote 0
                      • Th0mpyundefined
                        Th0mpy @Phaedrux
                        last edited by Th0mpy

                        @phaedrux
                        Stop replying so fast 🙂

                        But you're right, I missed the homeall.g error.

                        Usually the team that scores the most points wins the game.

                        1 Reply Last reply Reply Quote 1
                        • rubinkingmaundefined
                          rubinkingma
                          last edited by

                          Thanks to you both!

                          So it works now, this or next week ill start printing again and see what else i can find to complain about.

                          This used to be my "quick and dirty" machine, and after a few years almost the only machine i use.

                          I never took the time to really make it print nicely because i had a E3D volcano on it with a 0.8 Nozzle.

                          Now with all these cool changes i want to dial it in with a 0.6 nozzle and make it a really nice machine.

                          Its a core XY "hypercube" remix with hiwin rails for the bed.
                          It should be able to make very nice prints if i just spend some time with it

                          Th0mpyundefined 1 Reply Last reply Reply Quote 1
                          • Th0mpyundefined
                            Th0mpy @rubinkingma
                            last edited by

                            @rubinkingma

                            Excellent! Happy Printing!

                            Usually the team that scores the most points wins the game.

                            1 Reply Last reply Reply Quote 0
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