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    Duet WIFI Random Skipping Issue

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    Duet Hardware and wiring
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    • dc42undefined
      dc42 administrators
      last edited by

      Which firmware version are you using? Have you tried version 1.20RC1 ?

      Duet WiFi hardware designer and firmware engineer
      Please do not ask me for Duet support via PM or email, use the forum
      http://www.escher3d.com, https://miscsolutions.wordpress.com

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      • totalitarianundefined
        totalitarian
        last edited by

        Still running 1.19, is there anything specific in 1.20RC1 that could address the issue?

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        • dc42undefined
          dc42 administrators
          last edited by

          You should be running at least version 1.19.2 which addresses bugs in 1.19, one of which might possibly account for the strange behaviour. If you are using our MAX31856 thermocouple daughter board, there is another relevant fix in 1.20. In any case, with 1.20 close to release I won't be doing any investigations into possible bugs in earlier series firmware.

          Duet WiFi hardware designer and firmware engineer
          Please do not ask me for Duet support via PM or email, use the forum
          http://www.escher3d.com, https://miscsolutions.wordpress.com

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          • totalitarianundefined
            totalitarian
            last edited by

            Thanks, i'll update later today and report back if I still get this issue

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            • cheeseandhamundefined
              cheeseandham
              last edited by

              Totalitarian,have you found anything?

              My new Duet has been like it since it's been hooked up. Intermittent working, occasionally it drives correctly although I find it doesn't last and will change to this weird crunching after some time.

              • I've changed the loom

              • I've changed the NEMA17 motor it is hooked up to by testing it against my 2 year old (working) Ormerod 2's X-axis (with Duet 0.65 running firmware 1.19)

              • as well I plugged it into the Y-axis on this Ormerod 2 - same symptoms.

              Today I was demonstrating to a friend and he pointed out to me that to him, it looked like it might be heat related, as it works from a "cold" state (not been switched on recently) but doesn't work after it's been on a while.

              We then did further tests by pointing a big household fan at the board when switching it on from cold.Many (unscientific) repeats seem to show that it works a lot longer when a fan is pointing at it, as well as failing after a couple of minutes when the fan is removed.

              • Video of symptoms - https://photos.app.goo.gl/9NyewaadmLwrqx452

              • This is immediately afterwards, after switching off and swapping the X and Y axis cables on the Duet (and nothing else). This shows the X-axis working and the Y-axis crunching https://photos.app.goo.gl/DOma7r8vhHJ3bs5x1

              For information, I was running Firmware 1.19.2, and just in case I upgraded to Firmware Version: 1.20RC4 (2017-12-20) as indicated above, with no change to the behaviour.

              config.g

              ; Configuration file for Duet WiFi (firmware version 1.17 to 1.19)
              ; executed by the firmware on start-up
              ;
              ; generated by RepRapFirmware Configuration Tool on Wed Dec 20 2017 22:03:57 GMT+0000 (GMT Standard Time)
              
              ; General preferences
              M111 S0                            ; Debugging off
              G21                                ; Work in millimetres
              G90                                ; Send absolute coordinates...
              M83                                ; ...but relative extruder moves
              M555 P2                            ; Set firmware compatibility to look like Marlin
              M208 X0 Y0 Z0 S1                   ; Set axis minima
              M208 X240 Y240 Z200 S0             ; Set axis maxima
              
              ; Endstops
              M574 X0 Z0 S0                      ; Set active low endstops
              M574 Y1 S1                         ; Set active high endstops
              M558 P1 X1 Y0 Z1 H5 F120 T6000     ; Set Z probe type to unmodulated, the axes for which it is used and the dive height + speeds
              G31 P600 X0 Y0 Z2.8                ; Set Z probe trigger value, offset and trigger height
              M557 X15:215 Y15:195 S20           ; Define mesh grid
              
              ; Drives
              M569 P0 S0                         ; Drive 0 goes backwards
              M569 P1 S1                         ; Drive 1 goes forwards
              M569 P2 S1                         ; Drive 2 goes forwards
              M569 P3 S1                         ; Drive 3 goes forwards
              M569 P4 S1                         ; Drive 4 goes forwards
              M350 X16 Y16 Z16 E16:16 I0         ; Configure microstepping without interpolation
              M92 X87.489 Y87.489 Z4000 E420:420 ; Set steps per mm
              M566 X300 Y900 Z12 E120:120        ; Set maximum instantaneous speed changes (mm/min)
              M203 X6000 Y6000 Z180 E1200:1200   ; Set maximum speeds (mm/min)
              M201 X500 Y20 Z250 E250:250        ; Set accelerations (mm/s^2)
              M906 X800 Y1000 Z800 E800:800 I30  ; Set motor currents (mA) and motor idle factor in per cent
              M84 S30                            ; Set idle timeout
              
              ; Heaters
              M305 P0 T10000 B3988 C0 R4700      ; Set thermistor + ADC parameters for heater 0
              M143 H0 S120                       ; Set temperature limit for heater 0 to 120C
              M305 P1 T100000 B4138 C0 R4700     ; Set thermistor + ADC parameters for heater 1
              M143 H1 S260                       ; Set temperature limit for heater 1 to 260C
              M305 P2 T100000 B4138 C0 R4700     ; Set thermistor + ADC parameters for heater 2
              M143 H2 S260                       ; Set temperature limit for heater 2 to 260C
              
              ; Tools
              M563 P0 D0 H1                      ; Define tool 0
              G10 P0 X0 Y0 Z0                    ; Set tool 0 axis offsets
              G10 P0 R0 S0                       ; Set initial tool 0 active and standby temperatures to 0C
              M563 P1 D1 H2                      ; Define tool 1
              G10 P1 X10 Y0 Z0                   ; Set tool 1 axis offsets
              G10 P1 R0 S0                       ; Set initial tool 1 active and standby temperatures to 0C
              
              ; Network
              M550 PMy RepRapPro Ormerod 2       ; Set machine name
              M552 S1                            ; Enable network
              ;*** Access point is configured manually via M587 by the user
              M586 P0 S1                         ; Enable HTTP
              M586 P1 S1                         ; Enable FTP
              M586 P2 S0                         ; Disable Telnet
              
              ; Fans
              M106 P0 S0 I0 F500 H-1             ; Set fan 0 value, PWM signal inversion and frequency. Thermostatic control is turned off
              M106 P1 S1 I0 F500 H1:2 T45        ; Set fan 1 value, PWM signal inversion and frequency. Thermostatic control is turned on
              M106 P2 S1 I0 F500 H1:2 T45        ; Set fan 2 value, PWM signal inversion and frequency. Thermostatic control is turned on
              
              ; Custom settings are not configured
              
              

              So, is this a known issue? Is there supposed to be a fan over some part of the board that I'm not aware of? (it is mounted in the open, so there is no airflow issue) or is this something I should be contacting Duet3D about?

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              • dc42undefined
                dc42 administrators
                last edited by

                I've just replied to your similar post on the RepRapForum. If you suspect that a particular motor output his at fault, try substituting the E1 motor output instead, and use the M584 command to assign the E1 driver (driver 4) to the axis concerned. The M584 command must come before some other commands including M906 and M350.

                Duet WiFi hardware designer and firmware engineer
                Please do not ask me for Duet support via PM or email, use the forum
                http://www.escher3d.com, https://miscsolutions.wordpress.com

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                • totalitarianundefined
                  totalitarian
                  last edited by

                  cheeseandham doing as dc42 mentioned fixed the issue for me. It must be a faulty driver. dc42 how do we go about getting it replaced under warranty?

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                  • dc42undefined
                    dc42 administrators
                    last edited by

                    Email your supplier. If you bought it from duet3d.com then the address is info at duet3d dot com.

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

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                    • cheeseandhamundefined
                      cheeseandham
                      last edited by

                      Right, now Christmas is out of the way!

                      I used the M584 command to assign the E1 driver (driver 4) to the X axis as instructed above.
                      Everything works fine and I commissioned and could print a Marvin.

                      Moving the loom back to the X axis, and unfortunately it does the same thing as before (works for 0-4 minutes then crunch & fail)

                      I wouldn't mind so much if I hadn't bought the DuetWifi specifically for dual extrusion 🙂

                      Therefore I'll report this to my supplier.

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                      • cheeseandhamundefined
                        cheeseandham
                        last edited by

                        Sorted out / solved.

                        I'll just say Think3DPrint3D have great customer service. 😄

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