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    Underextrusion at the Beginning of Print Moves

    Scheduled Pinned Locked Moved
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    • Phaedruxundefined
      Phaedrux Moderator
      last edited by

      Seems like a travel without retraction allowing oozing to produce an under run. What slicer?

      Z-Bot CoreXY Build | Thingiverse Profile

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      • GaRv3undefined
        GaRv3
        last edited by

        Slicer doesn't matter. Same with Slic3r and S3D.
        It does not only happen after travel moves but after a change of direction/speed within a print move too.

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        • Phaedruxundefined
          Phaedrux Moderator
          last edited by

          Can you post your config.g and the results of an M122 diagnostic report run after the problem happens?

          Z-Bot CoreXY Build | Thingiverse Profile

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          • GaRv3undefined
            GaRv3
            last edited by

            Sure. I will do so, as soon as I am back home and have run another test.

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            • GaRv3undefined
              GaRv3
              last edited by

              M122
              === Diagnostics ===
              RepRapFirmware for Duet 2 WiFi/Ethernet version 2.0(RTOS) running on Duet WiFi 1.02 or later
              Board ID: 08DGM-95BLL-N6PSS-6J1F0-3S86R-90TVM
              Used output buffers: 3 of 20 (9 max)
              === RTOS ===
              Static ram: 28380
              Dynamic ram: 95820 of which 0 recycled
              Exception stack ram used: 388
              Never used ram: 6484
              Task NETWORK ready, free stack 396
              Task HEAT blocked, free stack 1256
              Task MAIN running, free stack 3592
              === Platform ===
              Last reset 00:06:20 ago, cause: power up
              Last software reset time unknown, reason: User, spinning module GCodes, available RAM 6460 bytes (slot 2)
              Software reset code 0x0003 HFSR 0x00000000, CFSR 0x00000000, ICSR 0x0041f000, BFAR 0xe000ed38, SP 0xffffffff
              Error status: 0
              Free file entries: 9
              SD card 0 detected, interface speed: 20.0MBytes/sec
              SD card longest block write time: 25.6ms
              MCU temperature: min 24.0, current 29.1, max 29.3
              Supply voltage: min 11.5, current 11.8, max 12.4, under voltage events: 0, over voltage events: 0
              Driver 0: ok, SG min/max 643/1023
              Driver 1: ok, SG min/max 343/1023
              Driver 2: standstill, SG min/max not available
              Driver 3: ok, SG min/max 0/484
              Driver 4: standstill, SG min/max 0/0
              Date/time: 2018-06-18 16:53:04
              Slowest loop: 74.69ms; fastest: 0.07ms
              === Move ===
              Hiccups: 0, StepErrors: 0, LaErrors: 0, FreeDm: 234, MinFreeDm 142, MaxWait: 4024853239ms, Underruns: 0, 0
              Scheduled moves: 466, completed moves: 464
              Bed compensation in use: mesh
              Bed probe heights: 0.000 0.000 0.000 0.000 0.000
              === Heat ===
              Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1
              Heater 0 is on, I-accum = 0.2
              Heater 1 is on, I-accum = 0.3
              === GCodes ===
              Segments left: 0
              Stack records: 2 allocated, 0 in use
              Movement lock held by http
              http is doing "M18 YM122" in state(s) 0
              telnet is idle in state(s) 0
              file is doing "G1 X79.195 Y100.408 E1.0048" in state(s) 0
              serial is idle in state(s) 0
              aux is idle in state(s) 0
              daemon is idle in state(s) 0
              queue is idle in state(s) 0
              autopause is idle in state(s) 0
              Code queue is empty.
              === Network ===
              Slowest loop: 44.85ms; fastest: 0.01ms
              Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
              HTTP sessions: 1 of 8

              • WiFi -
                Network state is running
                WiFi module is connected to access point
                Failed messages: pending 0, notready 0, noresp 0
                WiFi firmware version 1.21
                WiFi MAC address 2c:3a:e8:0b:17:0f
                WiFi Vcc 3.32, reset reason Turned on by main processor
                WiFi flash size 4194304, free heap 12784
                WiFi IP address 192.168.0.70
                WiFi signal strength -43dBm, reconnections 0, sleep mode modem
                Socket states: 0 0 0 0 0 0 0 0
                === Expansion ===
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              • GaRv3undefined
                GaRv3
                last edited by

                ; Configuration file for Duet WiFi (firmware version 1.20 or newer)
                ; executed by the firmware on start-up
                ;
                ; generated by RepRapFirmware Configuration Tool on Fri Feb 02 2018 20:19:38 GMT+0100

                ; General preferences
                M111 S0 ; Debugging off
                G21 ; Work in millimetres
                G90 ; Send absolute coordinates...
                M83 ; ...but relative extruder moves
                M555 P2 ; Set firmware compatibility to look like Marlin
                ; Automatic saving after power loss is not enabled

                M667 S0 ; Select CoreXY mode: Cartesian
                M208 X-45 Y-15 Z0 U0 V0 S1 ; Set axis minima
                M208 X215 Y210 Z230 U230 V230 S0 ; Set axis maxima

                ; Endstops
                M574 X1 Y1 Z1 U1 V1 S1 ; Set active high endstops
                M558 P4 B1 H4 F120 T6000 I1 ; Set Z probe type to switch and the dive height + speeds (inversed)
                G31 P600 X-26 Y-40 Z2.700 ; Set Z probe trigger value, offset and trigger height
                M557 X40:160 Y40:160 S40 ; Define mesh grid

                ; Map Drives
                M584 X0 Y1 Z2:4 U2 V4 E3 ; X:0, Y:1, Z:2+4, E:3, U(Z1):2, V(Z2):4

                ;Stall Detection
                M915 X S23 F0 R1 ; Stall detection for X axis
                M915 Y S23 F0 R1 ; Stall detection for Y axis
                M915 Z S-10 F0 R1 ; Stall detection for Z axis
                M915 U S-10 F0 R1 ; Stall detection for Z axis 1 (U)
                M915 V S-10 F0 R1 ; Stall detection for Z axis 2 (V)

                ; Drives
                M569 P0 S1 ; Drive 0 (X) goes forwards
                M569 P1 S1 ; Drive 1 (Y) goes forwards
                M569 P2 S0 ; Drive 2 (Z1/U) goes backwards
                M569 P3 S1 ; Drive 3 (E) goes forwards
                M569 P4 S0 ; Drive 4 (Z2/V) goes backwards

                M350 X16 Y16 Z16 U16 V16 E16 I1 ; Configure microstepping (interpolated)
                M92 X100 Y100 Z400 U400 V400 E100 ; Set steps per mm (interpoloated)
                M566 X600 Y600 Z18 U18 V18 E300 ; Set maximum instantaneous speed changes (mm/min) (Jerk) (A8 Default)
                M201 X2000 Y2000 Z100 U100 V100 E10000 ; Set MAX accelerations (mm/s^2) (A8 Default)
                M203 X24000 Y24000 Z480 U480 V480 E3000 ; Set maximum speeds (feedrate) (mm/min) (A8 Default)
                M204 P400 T1000 ; Set accelerations for print and travel moves (mm/s^2)
                M906 X900 Y900 Z900 U900 V900 E900 I30 ; Set motor currents (mA) and motor idle factor in per cent
                M84 S60 ; Set idle timeout

                ; Pressure Advance
                ;M572 D0 S0.010 ; Set pressure advance

                ; Firmware Retraction
                ;M207 S4.0 F2400 Z0.04 ; Set retraction distance (mm), speed (mm/min) and Z-Hop

                ; Heaters
                ;M301 H0 S1.00 P10 I0.1 D200 T0.4 W180 B30 ; Use PID on bed heater (may require further tuning)
                M305 P0 T100000 B4138 C0 R4700 ; Set thermistor + ADC parameters for heater 0
                M143 H0 S120 ; Set temperature limit for heater 0 to 120C
                M305 P1 T100000 B4138 C0 R4700 ; Set thermistor + ADC parameters for heater 1
                M143 H1 S280 ; Set temperature limit for heater 1 to 280C

                ; Tools
                M563 P0 D0 H1 ; Define tool 0
                G10 P0 X0 Y0 Z0 U0 V0 ; Set tool 0 axis offsets
                G10 P0 R0 S0 ; Set initial tool 0 active and standby temperatures to 0C

                ; Network
                M550 PAnet A8 Test ; Set machine name
                ;M551 Pxxx ; Set password
                M552 S1 ; Enable network
                M587 S"xxx" P"xxx" I192.168.0.70 ; Configure access point.
                M586 P0 S1 ; Enable HTTP
                M586 P1 S1 ; Enable FTP
                M586 P2 S0 ; Disable Telnet

                ; Fans
                M106 P0 S0 I0 F500 H-1 ; Set fan 0 value, PWM signal inversion and frequency. Thermostatic control is turned off
                M106 P1 S1 I0 F500 H1 T45 ; Set fan 1 value, PWM signal inversion and frequency. Thermostatic control is turned on
                M106 P2 S1 I0 F500 H1 T45 ; Set fan 2 value, PWM signal inversion and frequency. Thermostatic control is turned on

                ; CPU Temperature Calibration
                M912 P0 S-16.5

                ; Load saved Settings
                M501 ; Load config-override.g

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                • GaRv3undefined
                  GaRv3
                  last edited by

                  It seems linke the extruder starts extruding filament a little too late.
                  Nobody else faced this problem before?

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                  • Phaedruxundefined
                    Phaedrux Moderator
                    last edited by

                    Try setting your motor current to 85% of max minimum and retry.

                    Z-Bot CoreXY Build | Thingiverse Profile

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                    • Phaedruxundefined
                      Phaedrux Moderator @Phaedrux
                      last edited by

                      @phaedrux what is the extruder?

                      It totally goes away if you revert to a previous firmware version?

                      Z-Bot CoreXY Build | Thingiverse Profile

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                      • GaRv3undefined
                        GaRv3
                        last edited by

                        The motor runs at 900mA which is the current it is rated at.
                        I have not tried reverting to an older firmware version. I am not sure how to do this safely.

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                        • Danalundefined
                          Danal @GaRv3
                          last edited by Danal

                          @garv3 said in Underextrusion at the Beginning of Print Moves:

                          I am not sure how to do this safely.

                          Get whatever version you wish from Github. Follow the normal upload, etc. Depending on exact versions, slight tweaks to configuration may be needed.

                          If you somehow get "painted into a corner", follow the fallback procedures here:

                          https://duet3d.dozuki.com/Wiki/Installing_and_Updating_Firmware

                          Fallback #3 will ALWAYS work, and can be used to install any release after 1.19. In fact, if you have doubt about "mixed versions" or similar, starting with a blank/formatted card and fallback #3 will ensure everything is in sync. I've done it before, just for "mental comfort".

                          Delta / Kossel printer fanatic

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                          • Phaedruxundefined
                            Phaedrux Moderator
                            last edited by

                            900ma seems low to me for rated current. Can you post a link to the motor specs?

                            Z-Bot CoreXY Build | Thingiverse Profile

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                            • GaRv3undefined
                              GaRv3
                              last edited by

                              https://www.gearbest.com/3d-printer-parts/pp_540282.html?vip=4266359&gclid=CjwKCAjw9qfZBRA5EiwAiq0AbXsG7eVHXuESAoNW6fhbcCEcmuNcOI2yTYnp016b9ylPt-luT8IzGhoC6pwQAvD_BwE

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                              • Phaedruxundefined
                                Phaedrux Moderator
                                last edited by

                                Main Features:

                                • Step angle: 1.8 degree
                                • Number of phases: 2
                                • Voltage: 3.96V
                                • Current: 0.9A
                                • Resistance: 4.4 ohm
                                • Holding torque: 0.34 Nm

                                In this case 900mA might be too high for this motor, try 765 instead which would be 85% of rated.

                                Running the motor at max current could explain the behaviour seen here if it's overheating. Does the motor feel hot to the touch?

                                Z-Bot CoreXY Build | Thingiverse Profile

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                                • GaRv3undefined
                                  GaRv3
                                  last edited by GaRv3

                                  During long prints they get warm but not really hot. I set them to 765mA now.

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                                  • GaRv3undefined
                                    GaRv3
                                    last edited by

                                    Lowering the current unfortunately didn't change anything.

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                                    • Phaedruxundefined
                                      Phaedrux Moderator
                                      last edited by

                                      Can you post some pictures of your slicer settings?

                                      Z-Bot CoreXY Build | Thingiverse Profile

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                                      • Phaedruxundefined
                                        Phaedrux Moderator
                                        last edited by

                                        Also, what type of extruder is it? 4mm of retraction may be too much. It really looks like retraction under runs.

                                        Z-Bot CoreXY Build | Thingiverse Profile

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