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    First print after upgrading to Duet3d WiFi

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    • dc42undefined
      dc42 administrators
      last edited by

      It looks like you got quite bad ringing because the amplitude is dying down very slowly. Check the tightness of the belt that controls the axis perpendicular to the face that exhibits the riging.

      You could try the dynamic acceleration adjustment feature in firmware 2.02RC6, see https://duet3d.dozuki.com/Wiki/Gcode#Section_M593_Configure_Dynamic_Acceleration_Adjustment.

      Duet WiFi hardware designer and firmware engineer
      Please do not ask me for Duet support via PM or email, use the forum
      http://www.escher3d.com, https://miscsolutions.wordpress.com

      briskspiritundefined 1 Reply Last reply Reply Quote 0
      • briskspiritundefined
        briskspirit @dc42
        last edited by briskspirit

        @dc42 Both axis are with tight belts for sure, new pulleys and etc... And I don't hear any resonance or other audible problems. Both axis has almost the same ringing problem so I am lost with that problem... Something is flexing too much? Maybe could be the plastic carriage on LM8SUU bearings? I just can't understand what can be so wrong even at 30mm/s to give such a big ringing on both axis..

        Or could it be because my belts might be overtightened ? (Sounds like a guitar strings)

        Danalundefined 1 Reply Last reply Reply Quote 0
        • dc42undefined
          dc42 administrators
          last edited by

          What stepper motors are you using, and what motor currents have you set?

          Duet WiFi hardware designer and firmware engineer
          Please do not ask me for Duet support via PM or email, use the forum
          http://www.escher3d.com, https://miscsolutions.wordpress.com

          briskspiritundefined 1 Reply Last reply Reply Quote 0
          • briskspiritundefined
            briskspirit @dc42
            last edited by briskspirit

            @dc42

            X axis: nema 17 40mm 0.9deg stepper with current set at 80%, Y axis nema 17 40mm 1.8deg high impedance stepper with current set at 80%

            M906 X1064 Y680 Z1200 E714:714 I30 ;

            Full config:

            ; Configuration file for Duet WiFi
            ; executed by the firmware on start-up
            
            ; General preferences
            M111 S0 ; Debug off
            G21; Work in millimetres
            G90 ; Send absolute coordinates...
            M83 ; ...but relative extruder moves
            M555 P1 ; Set firmware compatibility to look like RepRapFirmare (P2 for Marlin)
            M575 P1 B57600 S1 ; Set auxiliary serial port baud rate and require checksum (for PanelDue)
            
            ; Network
            M550 PQIDIPro ; Set machine name
            M552 S1 ; Enable network
            M587 S" " P" " I192.168.1.201 J192.168.1.1 K255.255.255.0 ; Configure access point and IP addresses. You can delete this line once connected
            M586 P0 S1 ; Enable HTTP
            M586 P1 S0 ; Disable FTP
            M586 P2 S0 ; Disable Telnet
            
            ; Drives
            M569 P0 S1 ; Drive 0 goes forwards
            M569 P1 S1 ; Drive 1 goes forwards
            M569 P2 S0 ; Drive 2 goes backwards(Z drive)
            M569 P3 S1 ; Drive 3 goes forwards(Tool 0)
            M569 P4 S0 ; Drive 4 goes backwards(Tool 1)
            
            M350 X16 Y16 Z16 E16:16 I1 S2 ; Configure microstepping without interpolation and Spread Cycle enabled
            ;16T pulleys
            M92 X200 Y100 ; Set steps per mm for X(is 0.9deg stepper) Y(is 1.8deg stepper)
            ;T8*2 lead screw
            M92 Z1600 ; Set steps per mm for Z
            ;TODO: will be changed to geared 2.75:1 extruder with Bondtech gears and Nema 17 slim stepper
            M92 E99:99 ; Set steps per mm for extruders E0 and E1 (Different for PLA and PETG??)
            
            ; Axis kinematics
            M566 X1200 Y1200 Z12 E2400:2400 ; Set maximum instantaneous speed changes (mm/min)
            ;TODO: change max speed after changing extruders (https://reprapfirmware.org)
            M203 X12000 Y12000 Z600 E12000:12000 ; Set maximum speeds (mm/min) # Max speed before torque drop for X - 15354, Y - 11046
            M201 X1000 Y1000 Z50 E1000:1000 ; Set accelerations (mm/s^2) # Max accel for X by calculator 2820, for Y - 2155(estimate as I don't know exact weight)
            
            ; Steppers currents
            M906 X1064 Y680 Z1200 E714:714 I30 ; Set motor currents (mA) and motor idle factor in per cent
            M84 S30 ; Set idle timeout
            
            ; Axis Limits
            M208 X0 Y0 Z0 S1 ; Set axis minima
            M208 X264.5 Y154 Z169 S0 ; Set axis maxima
            ;M579 X1.001895478 Y1.004419446; Scale axis (Correction factors based on measurment of printed models)
            
            
            ; Endstops
            M574 X2 S0 ; Set active low endstop for X
            M574 Y2 S0 ; Set active low endstop for Y
            M574 Z2 S0 ; Set active low endstop for Z
            
            ; Z-Probe
            M558 P0 H5 F120 T12000 ; Disable Z probe but set dive height, probe speed and travel speed
            M557 X15:249.5 Y15:139 S20 ; Define mesh grid
            
            ; Heaters
            ;Bed
            M307 H0 A297.5 C982.3 D0.7 B0 S1.00 ; Disable bang-bang mode for the bed heater and set PWM limit
            M305 P0 T100000 B3950 C0 R4700 ; Set thermistor + ADC parameters for heater 0
            M143 H0 S110 ; Set temperature limit for heater 0 to 110C
            
            ;Extruders
            M307 H1 A561.2 C153.0 D9.6 B0 S1.00 ; Disable bang-bang mode for the bed heater and set PWM limit
            M305 P1 T100000 B3950 C0 R4700 ; Set thermistor + ADC parameters for heater 1
            M143 H1 S310 ; Set temperature limit for heater 1 to 310C (All Metal hotend)
            
            M307 H2 A797.2 C207.2 D8.1 B0 S1.00 ; Disable bang-bang mode for the bed heater and set PWM limit
            M305 P2 T100000 B3950 C0 R4700  ; Set thermistor + ADC parameters for heater 2
            M143 H2 S260 ; Set temperature limit for heater 2 to 260C
            
            ; Fans
            ; Part cooling
            M106 P0 S0 L0 I0 F100 H-1 ; Set fan 0 value, PWM signal inversion and frequency. Thermostatic control is turned off
            
            ; Cooling block fans
            M106 P1 S1 I0 F25000 H1:2 T45 ; Set fan 1 value, PWM signal inversion and frequency. Thermostatic control is turned on
            M106 P2 S1 I0 F25000 H1:2 T45 ; Set fan 2 value, PWM signal inversion and frequency. Thermostatic control is turned on
            
            ; Tools
            M563 P0 D0 H1 ; Define tool 0
            G10 P0 X0 Y0 Z0 ; Set tool 0 axis offsets
            G10 P0 R0 S0 ; Set initial tool 0 active and standby temperatures to 0C
            M563 P1 D1 H2 ; Define tool 1
            G10 P1 X-34 Y0 Z0 ; Set tool 1 axis offsets
            G10 P1 R0 S0 ; Set initial tool 1 active and standby temperatures to 0C
            
            ; Automatic power saving
            M911 S20 R22 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; Set voltage thresholds and actions to run on power loss
            
            ; Custom settings
            
            ; Miscellaneous
            M501 ; Load saved parameters from non-volatile memory
            

            override:

            M572 D0 S0.120
            
            dc42undefined 1 Reply Last reply Reply Quote 0
            • briskspiritundefined
              briskspirit
              last edited by

              @dc42 any ideas where to dig? Please!

              1 Reply Last reply Reply Quote 0
              • Danalundefined
                Danal @briskspirit
                last edited by Danal

                @briskspirit said in First print after upgrading to Duet3d WiFi:

                Or could it be because my belts might be overtightened ? (Sounds like a guitar strings)

                I don't know if being too tight causes ringing per se... but it does cause all kinds of other bad things.

                "Tight, but not too tight." Yeah, what a load of... anyway... "Guitar string" is definitely too tight. IMNSHO.

                Delta / Kossel printer fanatic

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                • dc42undefined
                  dc42 administrators @briskspirit
                  last edited by dc42

                  @briskspirit said in First print after upgrading to Duet3d WiFi:

                  X axis: nema 17 40mm 0.9deg stepper with current set at 80%, Y axis nema 17 40mm 1.8deg high impedance stepper with current set at 80%
                  ...
                  ; Steppers currents

                  M906 X1064 Y680 Z1200 E714:714 I30 ; Set motor currents (mA) and motor idle factor in per cent

                  Which motors, exactly? Are you using 12V or 24V power? Your Y axis motor in particular almost certainly needs 24V power, and even then the maximum speed before it loses torque and becomes noisy is likely to be quite low.

                  Duet WiFi hardware designer and firmware engineer
                  Please do not ask me for Duet support via PM or email, use the forum
                  http://www.escher3d.com, https://miscsolutions.wordpress.com

                  briskspiritundefined 2 Replies Last reply Reply Quote 0
                  • briskspiritundefined
                    briskspirit @dc42
                    last edited by

                    @dc42 24V power supply, max speed and acceleration was calculated from your online tools

                    X stepper JK42HM34-1334
                    Y stepper 42HB34F08AB-10

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                    • briskspiritundefined
                      briskspirit @dc42
                      last edited by

                      @dc42 I saw your answer in topic https://forum.duet3d.com/topic/8223/extruder-smoothness/2

                      I am using 1.8deg steppers on both extruders with steps per mm = ~100. (X16 microstepping, I1)
                      Maybe this is what is going on too?
                      I have two pancake motors with 0.9deg, but they are short/less powerful (waiting for gears to come)

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                      • dc42undefined
                        dc42 administrators
                        last edited by

                        Is the ringing pattern worse on the X face of the cube, or on the Y face? Whichever face is worse, it's probably the other axis that is ringing.

                        Duet WiFi hardware designer and firmware engineer
                        Please do not ask me for Duet support via PM or email, use the forum
                        http://www.escher3d.com, https://miscsolutions.wordpress.com

                        briskspiritundefined 1 Reply Last reply Reply Quote 0
                        • briskspiritundefined
                          briskspirit @dc42
                          last edited by

                          @dc42 Both axis has that ringing with same period but amplitude is worser on the Y face(so X is ringing with more amplitude)

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                          • briskspiritundefined
                            briskspirit
                            last edited by

                            What can cause almost the same ringing?

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                            • briskspiritundefined
                              briskspirit
                              last edited by

                              So I was a bit angry and furious and crashed my printer )) Some 8mm rods got bent and etc... Long story short: rebuilt my printer with new rods, installed dampers for Y and Z, tightened everything and now at 42mm/s speed I am getting very minimal ringing with very small amplitude(can see barely but can't feel by nail). So rebuilding helped or dampers 🙂

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                              • dc42undefined
                                dc42 administrators
                                last edited by

                                I'm glad you solved it.

                                The major cause of low-frequency ringing on a well-built machine is likely to be the interaction of the elasticity of the belts and the moving mass. That's why it's generally helpful to keep the moving mass as low as possible.

                                Duet WiFi hardware designer and firmware engineer
                                Please do not ask me for Duet support via PM or email, use the forum
                                http://www.escher3d.com, https://miscsolutions.wordpress.com

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