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Bl touch problems

Scheduled Pinned Locked Moved
Tuning and tweaking
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  • undefined
    Phaedrux Moderator
    last edited by 13 Jun 2019, 01:15

    Re check the wiring.

    Does the probe respond to deploy and retract commands?

    Z-Bot CoreXY Build | Thingiverse Profile

    undefined 1 Reply Last reply 13 Jun 2019, 01:20 Reply Quote 0
    • undefined
      kmhudgins @Phaedrux
      last edited by 13 Jun 2019, 01:20

      @phaedrux yes it responds to both

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      • undefined
        kmhudgins
        last edited by 13 Jun 2019, 01:22

        here is my config.g

        ; General preferences
        G90 ; Send absolute coordinates...
        M83 ; ...but relative extruder moves

        ; Network
        M550 P"Ender3ProMaestro" ; Set machine name
        M552 P0.0.0.0 S1 ; Enable network and acquire dynamic address via DHCP
        M586 P0 S1 ; Enable HTTP
        M586 P1 S0 ; Disable FTP
        M586 P2 S0 ; Disable Telnet

        ; Drives
        M569 P0 S0 ; Physical drive 0 goes backwards
        M569 P1 S0 ; Physical drive 1 goes backwards
        M569 P2 S1 ; Physical drive 2 goes forwards
        M569 P3 S0 ; Physical drive 3 goes backwards
        M350 X16 Y16 Z16 E128 I1 ; Configure microstepping with interpolation
        M92 X80.00 Y80.00 Z4000.00 E741.00 ; Set steps per mm
        M566 X600.00 Y600.00 Z60.00 E300.00 ; Set maximum instantaneous speed changes (mm/min)
        M203 X9000.00 Y9000.00 Z600.00 E6000.00 ; Set maximum speeds (mm/min)
        M201 X500.00 Y500.00 Z120.00 E5000.00 ; Set accelerations (mm/s^2)
        M906 X800.00 Y800.00 Z800.00 E900.00 I30 ; Set motor currents (mA) and motor idle factor in per cent
        M84 S30 ; Set idle timeout

        ; Axis Limits
        M208 X0 Y0 Z0 S1 ; Set axis minima
        M208 X230 Y230 Z260 S0 ; Set axis maxima

        ; Endstops
        M574 X1 Y1 S1 ; Set active high endstops

        ; Z-Probe
        M574 Z1 S2 ; Set endstops controlled by probe
        M558 P9 H5 F120 T6000 ; Set Z probe type to bltouch and the dive height + speeds
        G31 P500 X0 Y0 Z2.5 ; Set Z probe trigger value, offset and trigger height
        M557 X10:220 Y10:220 S20 ; Define mesh grid

        ; Heaters
        M307 H0 B0 S1.00 ; Disable bang-bang mode for the bed heater and set PWM limit
        M305 P0 T98801 B4185 R2200 ; Set thermistor + ADC parameters for heater 0
        M143 H0 S120 ; Set temperature limit for heater 0 to 120C
        M305 P1 T98801 B4185 R2200 ; Set thermistor + ADC parameters for heater 1
        M143 H1 S280 ; Set temperature limit for heater 1 to 280C

        ; Fans
        M106 P0 S0 I0 F20 H1 T45 ; Set fan 0 value, PWM signal inversion and frequency. Thermostatic control is turned on
        M106 P1 S0 I0 F20 H1 T45 ; Set fan 1 value, PWM signal inversion and frequency. Thermostatic control is turned on
        M106 P2 S0 I0 F20 H1:0 T45 ; Set fan 2 value, PWM signal inversion and frequency. Thermostatic control is turned on

        ; Tools
        M563 P0 S"Hotend" D0 H1 ; Define tool 0
        G10 P0 X0 Y0 Z0 ; Set tool 0 axis offsets
        G10 P0 R0 S0 ; Set initial tool 0 active and standby temperatures to 0C

        ; Automatic power saving
        M911 S21 R23 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; Set voltage thresholds and actions to run on power loss

        ; Custom settings
        M918 P1 E4 ; Enable 12864 LCD with 1 menu item per encoder click

        ; Miscellaneous
        M501 ; Load saved parameters from non-volatile memory

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        • undefined
          kmhudgins
          last edited by 13 Jun 2019, 01:45

          i think i got it working but im not sure how good of a fix it is.
          sense the proble is ready 1000 i set the trigger vallue to 1001 at the moment. this allows me to get some movement.

          1 Reply Last reply Reply Quote 0
          • undefined
            Phaedrux Moderator
            last edited by 13 Jun 2019, 01:47

            How exactly do you have it wired? It sounds like the signal is being inverted or that it needs to be inverted.

            Z-Bot CoreXY Build | Thingiverse Profile

            1 Reply Last reply Reply Quote 0
            • undefined
              kmhudgins
              last edited by 13 Jun 2019, 01:52

              0_1560390698810_c7f6eb0d-9074-4381-bc0a-842d3b8deb69-image.png

              1 Reply Last reply Reply Quote 0
              • undefined
                kmhudgins
                last edited by 13 Jun 2019, 01:55

                I used the connectors that came with the board. unfortunate I could not find a 5 pin connector so i used a 2 pin and a 3 pin and cut the plastic guides that interfered off.

                1 Reply Last reply Reply Quote 0
                • undefined
                  kmhudgins
                  last edited by 13 Jun 2019, 02:01

                  0_1560391262726_unnamed.jpg
                  here is the actual wiring

                  1 Reply Last reply Reply Quote 0
                  • undefined
                    Phaedrux Moderator
                    last edited by 13 Jun 2019, 02:42

                    That looks right.

                    What version of BLTouch is it?

                    I'd still double check the wires and crimps themselves to make sure they aren't damaged and that all electrical connections are actually being made.

                    Z-Bot CoreXY Build | Thingiverse Profile

                    1 Reply Last reply Reply Quote 0
                    • undefined
                      kmhudgins
                      last edited by 13 Jun 2019, 02:43

                      the bl touch is v3

                      1 Reply Last reply Reply Quote 0
                      • undefined
                        Phaedrux Moderator
                        last edited by 13 Jun 2019, 02:46

                        I have a V3 BlTouch that I hope to be connecting to a Duet Maestro in the next couple days once I have some parts printed. Though I don't think there is anything compatibility wise that should be stopping it from working.

                        Most likely it's a wiring issue of some kind, or a small configuration oversight.

                        Maybe take a break from it and come back at it with fresh eyes. Start from the top.

                        Z-Bot CoreXY Build | Thingiverse Profile

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                        • undefined
                          kmhudgins
                          last edited by 13 Jun 2019, 02:47

                          thank you for the help. I am going to re do the crimp connections and see where that gets me.

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                          • undefined
                            kmhudgins
                            last edited by 13 Jun 2019, 03:00

                            0_1560394654839_bc85cb07-df98-4a9d-8944-7a8ff5dd36a0-image.png
                            i figured out part of the issue. the white and black connectors near the bltouch came untouched. now my z-probe is ready. im not sure if anything on this could be usefull but now i can actually run the home however when i trigger the bltouch it the z axis does not stop.

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                            • undefined
                              Phaedrux Moderator
                              last edited by 13 Jun 2019, 03:44

                              If it's not stopping, that would indicate there's still an issue with the wiring, probably the white wire.

                              Z-Bot CoreXY Build | Thingiverse Profile

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                              • undefined
                                PaulHew
                                last edited by 13 Jun 2019, 07:31

                                Is that a direct run from the BL to the Maestro in regards to the wiring?
                                Do you have any joins in the wires? If you do make sure they are solid and if you have changed colours make sure they correspond correctly at the Maestro end.

                                Also unplug the tiny connector on the back of the BL Touch carefully and plug back in again, it might not be seated correctly, its fiddly!

                                Your code for the Z-Probe is the same as mine.

                                Also as Phaedrux has guided me before the height of the BL Touch needs to be correct.
                                Turn power off, wind down the Z axis slowly so the nozzle touches the bed.
                                Measure from bed to bottom of the CASE of the BL touch, it should be about 8mm. Not the probe tip.
                                I printed a tool from thingiverse to help me as using a mirror as a bed makes seeing things harder!

                                RailCore II - Duet Mini + 1LC, Voron V0.1 - Duet Mini
                                Voron 2.4 disassembled..... Waiting for the RailCore Mini....

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                                • undefined
                                  lodger
                                  last edited by lodger 13 Jun 2019, 13:13

                                  Your G31 in your config says " G31 P500 X0 Y0 " . Your need measure your off sets ,

                                  Just thinking is the BL TOUCH flashing red. mine does it now and then and i have to power up and down the printer... when she is flashing it shows triggered .

                                  undefined undefined 2 Replies Last reply 13 Jun 2019, 19:11 Reply Quote 0
                                  • undefined
                                    PaulHew @lodger
                                    last edited by 13 Jun 2019, 19:11

                                    @lodger He does have an offset
                                    G31 P500 X0 Y0 Z2.5
                                    I had a double take also.

                                    RailCore II - Duet Mini + 1LC, Voron V0.1 - Duet Mini
                                    Voron 2.4 disassembled..... Waiting for the RailCore Mini....

                                    undefined 1 Reply Last reply 13 Jun 2019, 19:22 Reply Quote 0
                                    • undefined
                                      Phaedrux Moderator @PaulHew
                                      last edited by 13 Jun 2019, 19:22

                                      @paulhew said in Bl touch problems:

                                      X0 Y0

                                      He'll also need the X and Y offset.

                                      Z-Bot CoreXY Build | Thingiverse Profile

                                      undefined 1 Reply Last reply 13 Jun 2019, 21:53 Reply Quote 0
                                      • undefined
                                        lodger @Phaedrux
                                        last edited by 13 Jun 2019, 21:53

                                        @phaedrux If your unsure of this point us to how you have mounted it .IE what mount you printed out so we can help...

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                                        • undefined
                                          kmhudgins
                                          last edited by 14 Jun 2019, 02:33

                                          so i figured out the issue my connectors near the bl touch came undone i need to heat shrink the connectors so that this does not happen before. at the moment it is running. as fare as actual offsets I have a general idea of what they or for this particular mount but i plan on printing a diffrent one out as well as design a blower attachment for the nactua quite fans i am using to replace the stock fans.
                                          if anyone has any suggestions an a good mounting system i would take suggestions. I am currently looking at the hero me mounts but not set on them.
                                          thank you for all the help.

                                          undefined 1 Reply Last reply 14 Jun 2019, 03:05 Reply Quote 0
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