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    Stepper motor lost torque

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    My Duet controlled machine
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    • dc42undefined
      dc42 administrators @oliverracing
      last edited by

      The Duet WiFi/Ethernet doesn't normally need any cooling unless you run the motors at 2A or higher.

      Duet WiFi hardware designer and firmware engineer
      Please do not ask me for Duet support via PM or email, use the forum
      http://www.escher3d.com, https://miscsolutions.wordpress.com

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      • oliverracingundefined
        oliverracing
        last edited by oliverracing

        I Know and chips stayed cool enough to touch during a long print, I just went with better safe than sorry approach as the duet is in the heated build chamber. I plan on moving outside when I get a chance but that'll involve lengthening all the wires so been putting it off.

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        • oliverracingundefined
          oliverracing
          last edited by

          So this is turning out to be interesting....

          -swapped stepper, still got the issue
          -new wiring, still got the issue
          -swapped to e1, still go the issue

          No idea where to go from here! ☹

          deckingmanundefined 1 Reply Last reply Reply Quote 0
          • deckingmanundefined
            deckingman @oliverracing
            last edited by

            @oliverracing If the motor sits there clicking away but nothing else happens and it isn't the motor, or the wiring, or the motor driver then it must be something wrong with the extruder itself. What extruder is it?

            Ian
            https://somei3deas.wordpress.com/
            https://www.youtube.com/@deckingman

            oliverracingundefined 1 Reply Last reply Reply Quote 0
            • oliverracingundefined
              oliverracing @deckingman
              last edited by

              @deckingman That was my thought - I checked it out of the extruder too but it can barely turn the extruder drive gear when held in my hand (direct on the output shaft). I've tried upping the current to 1500ma and that changes the clicking to a louder clicking but still struggles to turn the drive gear in my hand

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              • A Former User?
                A Former User
                last edited by

                if the motor driver is active its hard to turn the motor shaft, if the driver is not active it should spin relatively freely if not mechanically loaded somehow.

                oliverracingundefined 1 Reply Last reply Reply Quote 0
                • oliverracingundefined
                  oliverracing @A Former User
                  last edited by

                  @bearer yeah I know, when active it feels a little stiff (I know this normally feels a lot harder to turn than this) and almost rough but completely smooth when off for both. Tearing my hair out at the moment as no idea what's going on.

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                  • A Former User?
                    A Former User
                    last edited by

                    So if you disconnect the motor is it the same? If you disconnect and short out the coils is it the same? Sounds like something is shorted, and those two should help point towards bad wiring or bad drivers.

                    oliverracingundefined 1 Reply Last reply Reply Quote 0
                    • oliverracingundefined
                      oliverracing @A Former User
                      last edited by

                      @bearer nope, when disconnected the motor spins freely but when powered it's got such low holding torque I can turn the Shaft by hand with much lower amount of force to normal

                      dc42undefined deckingmanundefined 2 Replies Last reply Reply Quote 0
                      • dc42undefined
                        dc42 administrators @oliverracing
                        last edited by

                        @oliverracing said in Stepper motor lost torque:

                        @bearer nope, when disconnected the motor spins freely but when powered it's got such low holding torque I can turn the Shaft by hand with much lower amount of force to normal

                        What current are you running the motor at? Can you provide a link to the data sheet?

                        Send M906 without parameters to check that the current is what you think it is. Also M913 to check that it is at 100%.

                        Duet WiFi hardware designer and firmware engineer
                        Please do not ask me for Duet support via PM or email, use the forum
                        http://www.escher3d.com, https://miscsolutions.wordpress.com

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                        • oliverracingundefined
                          oliverracing
                          last edited by

                          I'm running the motor at 900ma - and have been for ~2 years, Tried M906 to set the current up to 1500ma just to check if that made any difference (definitely added torque, just not much). I'll try M906 and M913 to check tonight - at work at the moment so hold fire on this.

                          As for specs of motor - they are the basic ones that originally came on the Tevo Tarantula that my printer once was based on. I have also tried a similar spec motor fresh from the box and this shows the same issue making me think it's unlikely to be a motor issue. I've made a fresh wire, so making that unlikely and tested the new and old (in that order) on the E1 driver and that had the same issue.

                          Can't work out how to link so here are the specs...
                          Drive Shaft - - - - - - - - - - - - - - - - - - - - - - - - - - - - 4.5mm
                          Step Angle - - - - - - - - - - - - - - - - - - - - - - - - - - - - 1.8°
                          Step Angle Accuracy - - - - - - - - - - - - - - - - - - - - 1.8 ° ± 5%
                          Holding torque - - - - - - - - - - - - - - - - - - - - - - - - 420mN.m(I=1.5A)
                          Rated Current/Phase - - - - - - - - - - - - - - - - - - - 1.5A
                          Phase Resistance - - - - - - - - - - - - - - - - - - - - - - 1.6±10%
                          Voltage - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - 2.4V
                          Inductance - - - - - - - - - - - - - - - - - - - - - - - - - - - 3.8mH±20%
                          Positioning Torque - - - - - - - - - - - - - - - - - - - - - 18mN.m REF.
                          Maximum load starting frequency - - - - - - - - - 1400pps
                          Maximum no-load operating frequency - - - - - 8000pps
                          Moment of inertia - - - - - - - - - - - - - - - - - - - - - - 57gcm
                          Ambient temperature - - - - - - - - - - - - - - - - - - _ -20 ~ 50

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                          • deckingmanundefined
                            deckingman @oliverracing
                            last edited by

                            @oliverracing said in Stepper motor lost torque:

                            @bearer nope, when disconnected the motor spins freely but when powered it's got such low holding torque I can turn the Shaft by hand with much lower amount of force to normal

                            To recap, this was working fine but the fault suddenly started without you making any changes to the configuration files.

                            What you are describing (i.e. you can easily turn the motor by hand, even when the holding current is set to 1500mA) indicates that only one pair of coils is being energised. I can only think of three possible reasons for that. 1) The motor itself is faulty but you say you've tried another. 2) There wiring is faulty but you say you've replaced it all. 3)The driver is faulty but you say you've tried another driver.

                            One thing occurs to me but I don't know if it is possible, is that the stepper developed a fault which took out the driver chip. You then tried that motor on another driver but because of the fault, it instantly took out that driver chip too. @dc42 will know if that's possible.

                            If not, then it only leaves highly improbably scenarios. 1) The stepper you replaced it with is also faulty. 2) The wiring you replaced is also faulty. 3) The driver you swapped with is also faulty.

                            It's easy enough to test a stepper motor to see if both coils are healthy - just do an internet search which will reveal a number of methods depending on what tools you have available. Once you have established that you have healthy stepper motor, connect it to a known healthy driver - such as one of the axis drivers. If it doesn't work, then it has to be the wiring between the stepper and the driver. If it does work, then it has to be a faulty driver (or two).

                            Ian
                            https://somei3deas.wordpress.com/
                            https://www.youtube.com/@deckingman

                            oliverracingundefined 1 Reply Last reply Reply Quote 0
                            • oliverracingundefined
                              oliverracing @deckingman
                              last edited by oliverracing

                              @deckingman Spot on and and thank you for putting it far more elegantly than I ever could! I'll go though in that order to try and work out what's going on.

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                              • oliverracingundefined
                                oliverracing
                                last edited by oliverracing

                                Damn

                                That didn't end well (the short to ground warnings). Pop and burning smell with this warning in DWC. Had previously checked M906 - came back with E900:900 and M913 with returned 100%. Unplugged and replugged all connectors to do with extruder to check and tried a 1mm extrude and pop.

                                For reference the e0 driver now has a little hole in it

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                                • oliverracingundefined
                                  oliverracing
                                  last edited by

                                  Just looking for a replacement chip, is it a TMC2660-PA-T or TMC2660-PA that I need to be a direct swap and is it just a case of removing the old chip and soldering the new one on?

                                  dc42undefined 1 Reply Last reply Reply Quote 0
                                  • Vetiundefined
                                    Veti
                                    last edited by

                                    before you do any chip replacement you need to go on a hunt for what was causing the problem.

                                    start by checking the resistance of each phase of the stepper that you had connected.

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                                    • dc42undefined
                                      dc42 administrators @oliverracing
                                      last edited by

                                      @oliverracing said in Stepper motor lost torque:

                                      Just looking for a replacement chip, is it a TMC2660-PA-T or TMC2660-PA that I need to be a direct swap and is it just a case of removing the old chip and soldering the new one on?

                                      Yes that's the one. I think the -T suffix just means that it is supplied on a reel. But before you replace it, how old is your Duet? If the driver failure wasn't your fault, replacement is covered by the warranty.

                                      Duet WiFi hardware designer and firmware engineer
                                      Please do not ask me for Duet support via PM or email, use the forum
                                      http://www.escher3d.com, https://miscsolutions.wordpress.com

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                                      • oliverracingundefined
                                        oliverracing
                                        last edited by

                                        Yeah, I'm gonna do a proper debug this weekend as thought I had but must have missed something. The TMC2660 chips had a 3 week lead time so got a few ordered anyway ~£5 each so hardly a issue if they're not the original cause but one will need replacing anyway as it has a hole in it where the magic smoke came out!

                                        Not sure the age of the board, I've had it nearly 6 months and it was used before I got it, the previous owner had given up with 3d printing but not due to board issues but will ask him anyway if it might still be in warranty, I suspect not as he'd given up for a fairly long time.

                                        I got the board free so I might just invest in a new board if there's nothing wrong with the steppers and the rest of the wiring as massively prefer it over the stock board on the Tevo.

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                                        • Phaedruxundefined
                                          Phaedrux Moderator
                                          last edited by

                                          There will be a PCB revision on the board itself, that may give an indication as to its age.

                                          Z-Bot CoreXY Build | Thingiverse Profile

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                                          • oliverracingundefined
                                            oliverracing
                                            last edited by

                                            So....

                                            I am officially an idiot. The stepper I did my testing with the pin-out is different to the original one - making this the likely cause of the pop and smoke I'd have thought.

                                            I reckon wiring was the cause of the original loss of torque as a quick resistance check shows high resistance on on of the 4 wires.

                                            I'll replace the drivers and go from there! Any other bits I might need to change?

                                            Thanks for all the help, I'm sure I'll be back here when this fix doesn't work but fingers are crossed!

                                            dc42undefined 1 Reply Last reply Reply Quote 0
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