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    BLTouch Homing in wrong direction

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    Duet Hardware and wiring
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    • chrisundefined
      chris
      last edited by

      used multimeter to prove continuity between the pins on idc ribbon cable and heater pwm pins

      fcwiltundefined 1 Reply Last reply Reply Quote 1
      • Phaedruxundefined
        Phaedrux Moderator
        last edited by

        I think it may behave like the Duex pwm pin and just needs to be inverted in RRF3.

        So if you still want to use the expansion breakout board, try inverting the servo pin command by adding an exclamation point like this

        ; Z-Probe
        M950 S0 C"!exp.heater7"                         ; create servo pin 0 for BLTouch
        

        Z-Bot CoreXY Build | Thingiverse Profile

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        • chrisundefined
          chris @Phaedrux
          last edited by

          @Phaedrux didn't have dupont connector hence why was using breakout board only on old firmware used H7 not exp.heater7 which is what 3.1.1 set it as M950 S0 C"exp.heater7"

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          • Phaedruxundefined
            Phaedrux Moderator
            last edited by

            If the exclamation point to invert doesn't work, might need to change the pin name

            M950 S0 C"duex.pwm5" also might need to be inverted, but I'm not sure. I've never seen anyone use the breakout board for the BLtouch, so until I get some confirmation we'll just have to experiment.

            Z-Bot CoreXY Build | Thingiverse Profile

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            • chrisundefined
              chris
              last edited by

              seems inverting pin may have worked deploy macros now working

              Phaedruxundefined 1 Reply Last reply Reply Quote 1
              • fcwiltundefined
                fcwilt @chris
                last edited by fcwilt

                @chris said in BLTouch Homing in wrong direction:

                used multimeter to prove continuity between the pins on idc ribbon cable and heater pwm pins

                OK then I think at this point you may just want to try the various other names.

                exp.heater3, exp.8, !duex.e2heat, !duex.pwm1
                exp.heater4, exp.13, !duex.e3heat, !duex.pwm2
                exp.heater5, exp.18, !duex.e4heat, !duex.pwm3
                exp.heater6, exp.23, !duex.e5heat, !duex.pwm4
                exp.heater7, exp.31, !duex.e6heat, !duex.pwm5

                I have the Duex5 board and this is my command M950 S0 C"duex.pwm5"

                Frederick

                Printers: a small Utilmaker style, a small CoreXY and a E3D MS/TC setup. Various hotends. Using Duet 3 hardware running 3.4.6

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                • Phaedruxundefined
                  Phaedrux Moderator @chris
                  last edited by

                  @chris said in BLTouch Homing in wrong direction:

                  seems inverting pin may have worked deploy macros now working

                  That's good.

                  Z-Bot CoreXY Build | Thingiverse Profile

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                  • chrisundefined
                    chris
                    last edited by

                    any advice on how to reduce how close nozzle is to bed currently

                    G31 P25 X46.5 Y0 Z3.6

                    do I change the 3.6mm height?

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                    • Phaedruxundefined
                      Phaedrux Moderator
                      last edited by

                      Follow these steps to measure the trigger height

                      https://duet3d.dozuki.com/Wiki/Test_and_calibrate_the_Z_probe#Section_Calibrate_the_Z_probe_trigger_height

                      Then afterwards when testing your first layer use the baby stepping function to adjust. Then take the amount of baby stepping used and modify the G31 Z value.

                      A larger G31 Z value moves the nozzle and bed closer together. If it's too close, make G31 Z smaller.

                      Z-Bot CoreXY Build | Thingiverse Profile

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                      • chrisundefined
                        chris
                        last edited by

                        so reduce the 3.6 to like 3.4?

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                        • Phaedruxundefined
                          Phaedrux Moderator
                          last edited by

                          bedlevel_nozzle_0.4_200x200-0.3-0.8.stl

                          I'd suggest printing a test pattern like this and adjusting the baby stepping to find out exactly how much to change it.

                          But yeah, 0.2 sounds like a reasonable amount to start with.

                          Z-Bot CoreXY Build | Thingiverse Profile

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