Duet3D Logo Duet3D
    • Tags
    • Documentation
    • Order
    • Register
    • Login

    Duet3 6CH + 3CH expansion board - Missing steps.

    Scheduled Pinned Locked Moved Solved
    Tuning and tweaking
    12
    153
    8.7k
    Loading More Posts
    • Oldest to Newest
    • Newest to Oldest
    • Most Votes
    Reply
    • Reply as topic
    Log in to reply
    This topic has been deleted. Only users with topic management privileges can see it.
    • deckingmanundefined
      deckingman @evomotors
      last edited by deckingman

      @evomotors said in Duet3 6CH + 3CH expansion board - Missing steps.:

      ........................ I wonder if I have the same issue if E motor is connected to expansion or tool board (both 3.1 and 3.2) and I'm the only one with this issue, it could be related to faulty Duet 3 board?

      I'm beginning to think that way myself - especially as I can run my 6 BMGs on expansion boards without any hiccups and even with an older firmware (providing I use 16x micro-stepping or less).

      But I'm just an end user like you. I suggest you work through the steps that DC42 has asked you to do - he's the one you who will decide if it's a hardware issue and who can authorise a warranty replacement if that is what is required.

      Ian
      https://somei3deas.wordpress.com/
      https://www.youtube.com/@deckingman

      evomotorsundefined 1 Reply Last reply Reply Quote 0
      • evomotorsundefined
        evomotors @deckingman
        last edited by

        @deckingman said in Duet3 6CH + 3CH expansion board - Missing steps.:

        @evomotors said in Duet3 6CH + 3CH expansion board - Missing steps.:

        ........................ I wonder if I have the same issue if E motor is connected to expansion or tool board (both 3.1 and 3.2) and I'm the only one with this issue, it could be related to faulty Duet 3 board?

        I'm beginning to think that way myself - especially as I can run my 6 BMGs on expansion boards without any hiccups and even with an older firmware (providing I use 16x micro-stepping or less).

        But I'm just an end user like you. I suggest you work through the steps that DC42 has asked you to do - he's the one you who will decide if it's a hardware issue and who can authorise a warranty replacement if that is what is required.

        I added another Z axis few days ago and now I don't have free driver on the main board any longer to prove my point.

        Do you think it would work when 3-Z motors connected to Duet3 and 4th Z to Expansion? e.g. (M584 X0.4 Y0.5 Z0.0:0.1:0.2:1.0 E0.1)

        deckingmanundefined 1 Reply Last reply Reply Quote 0
        • jay_s_ukundefined
          jay_s_uk
          last edited by jay_s_uk

          Yes, that would work
          As long as you get your CAN/driver numbers correct

          Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

          1 Reply Last reply Reply Quote 0
          • deckingmanundefined
            deckingman @evomotors
            last edited by

            @evomotors said in Duet3 6CH + 3CH expansion board - Missing steps.:

            @deckingman said in Duet3 6CH + 3CH expansion board - Missing steps.:

            @evomotors said in Duet3 6CH + 3CH expansion board - Missing steps.:

            ........................ I wonder if I have the same issue if E motor is connected to expansion or tool board (both 3.1 and 3.2) and I'm the only one with this issue, it could be related to faulty Duet 3 board?

            I'm beginning to think that way myself - especially as I can run my 6 BMGs on expansion boards without any hiccups and even with an older firmware (providing I use 16x micro-stepping or less).

            But I'm just an end user like you. I suggest you work through the steps that DC42 has asked you to do - he's the one you who will decide if it's a hardware issue and who can authorise a warranty replacement if that is what is required.

            I added another Z axis few days ago and now I don't have free driver on the main board any longer to prove my point.

            Do you think it would work when 3-Z motors connected to Duet3 and 4th Z to Expansion? e.g. (M584 X0.4 Y0.5 Z0.0:0.1:0.2:1.0 E0.1)

            Possibly ..........but you might fall foul of one or other of the following limitations.

            1. Endstop switches and Z probes connected to the main board cannot control motors on an expansion board. This is planned to be fixed in release 3.4.

            2. If you use a Z probe then the Z motors must be connected to the main board. This is planned to be fixed in release 3.4.

            Link to the full list of limitations is here https://duet3d.dozuki.com/Wiki/Duet_3_firmware_configuration_limitations

            Ian
            https://somei3deas.wordpress.com/
            https://www.youtube.com/@deckingman

            evomotorsundefined 1 Reply Last reply Reply Quote 0
            • evomotorsundefined
              evomotors @deckingman
              last edited by

              @deckingman said in Duet3 6CH + 3CH expansion board - Missing steps.:

              @evomotors said in Duet3 6CH + 3CH expansion board - Missing steps.:

              @deckingman said in Duet3 6CH + 3CH expansion board - Missing steps.:

              @evomotors said in Duet3 6CH + 3CH expansion board - Missing steps.:

              ........................ I wonder if I have the same issue if E motor is connected to expansion or tool board (both 3.1 and 3.2) and I'm the only one with this issue, it could be related to faulty Duet 3 board?

              I'm beginning to think that way myself - especially as I can run my 6 BMGs on expansion boards without any hiccups and even with an older firmware (providing I use 16x micro-stepping or less).

              But I'm just an end user like you. I suggest you work through the steps that DC42 has asked you to do - he's the one you who will decide if it's a hardware issue and who can authorise a warranty replacement if that is what is required.

              I added another Z axis few days ago and now I don't have free driver on the main board any longer to prove my point.

              Do you think it would work when 3-Z motors connected to Duet3 and 4th Z to Expansion? e.g. (M584 X0.4 Y0.5 Z0.0:0.1:0.2:1.0 E0.1)

              Possibly ..........but you might fall foul of one or other of the following limitations.

              1. Endstop switches and Z probes connected to the main board cannot control motors on an expansion board. This is planned to be fixed in release 3.4.

              2. If you use a Z probe then the Z motors must be connected to the main board. This is planned to be fixed in release 3.4.

              Link to the full list of limitations is here https://duet3d.dozuki.com/Wiki/Duet_3_firmware_configuration_limitations

              So looks like I'm stuck... I cannot connect my extruder to main board without changing printer (reverting to 3Z screws).

              1 Reply Last reply Reply Quote 0
              • evomotorsundefined
                evomotors @dc42
                last edited by evomotors

                @dc42

                Can you explain this?

                This is from expansion board diagnostics:
                e8ad254f-3587-413c-86fd-ccd2dfc32735-image.png

                According to it extruder completed all 904822 requested steps, and if I calculate this in mm it would be 904822 / 205 = 4413.77 mm.

                This is job information:
                3c7a38bd-b732-44cb-ac11-2a6983170a2b-image.png
                According to it , the filament usage should be 11375.9 mm.

                And print looks and weights exactly like it 2.5 times lighter.

                So it looks like expansion board is not missing steps, it looks like Duet 3 board is not sending all steps to it.

                1 Reply Last reply Reply Quote 0
                • evomotorsundefined
                  evomotors
                  last edited by

                  Or this is some other "Moves"?

                  1 Reply Last reply Reply Quote 0
                  • dc42undefined
                    dc42 administrators
                    last edited by dc42

                    That figure is moves, not steps. Each move normally has many steps. Try looking at the reported driver 1 position instead. If will have started from 0 when the machine was last powered on or reset.

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                    evomotorsundefined 2 Replies Last reply Reply Quote 0
                    • evomotorsundefined
                      evomotors @dc42
                      last edited by

                      @dc42 said in Duet3 6CH + 3CH expansion board - Missing steps.:

                      That figure is moves, not steps. Each move normally has many steps.

                      But is it possible that Duet3 not sending correct steps to the board?

                      Please work with me on it.

                      1 Reply Last reply Reply Quote 0
                      • evomotorsundefined
                        evomotors @dc42
                        last edited by

                        @dc42 said in Duet3 6CH + 3CH expansion board - Missing steps.:

                        That figure is moves, not steps. Each move normally has many steps. Try looking at the reported driver 1 position instead.

                        Driver 1: position 8664558, 205.0 steps/mm, ok, reads 40377, writes 0 timeouts 0, SG min/max 0/256

                        but 8664558 cannot be steps, this number is huge

                        1 Reply Last reply Reply Quote 0
                        • dc42undefined
                          dc42 administrators
                          last edited by

                          Have you done just one print since powering the printer up?

                          Duet WiFi hardware designer and firmware engineer
                          Please do not ask me for Duet support via PM or email, use the forum
                          http://www.escher3d.com, https://miscsolutions.wordpress.com

                          evomotorsundefined 2 Replies Last reply Reply Quote 0
                          • evomotorsundefined
                            evomotors @dc42
                            last edited by

                            @dc42 said in Duet3 6CH + 3CH expansion board - Missing steps.:

                            Have you done just one print since powering the printer up?

                            No, I did several tests. But let power cycle and try again.

                            1 Reply Last reply Reply Quote 0
                            • evomotorsundefined
                              evomotors @dc42
                              last edited by evomotors

                              @dc42

                              Started fresh with power-cycle.

                              According to job info and gcode file the filament usage should be 2652.10 mm

                              28038d1e-75b9-4683-8959-162af59dbd7d-image.png

                              And according to driver position it extruded only 1418.20

                              d753f327-5d7c-40da-8c29-6a880d4c9b6a-image.png

                              So there is 1233.9 mm discrepancy...

                              Diagnostics for Duet 3

                              M122
                              === Diagnostics ===
                              RepRapFirmware for Duet 3 MB6HC version 3.2 running on Duet 3 MB6HC v1.01 or later (SBC mode)
                              Board ID: 08DJM-956L2-G43S8-6JKDL-3SJ6L-1802G
                              Used output buffers: 1 of 40 (12 max)
                              === RTOS ===
                              Static ram: 149788
                              Dynamic ram: 63168 of which 68 recycled
                              Never used RAM 145808, free system stack 128 words
                              Tasks: Linux(ready,75) HEAT(blocked,296) CanReceiv(blocked,848) CanSender(blocked,337) CanClock(blocked,352) TMC(blocked,19) MAIN(running,720) IDLE(ready,19)
                              Owned mutexes: HTTP(MAIN)
                              === Platform ===
                              Last reset 01:15:28 ago, cause: power up
                              Last software reset at 2021-01-06 22:26, reason: User, none spinning, available RAM 145840, slot 0
                              Software reset code 0x0012 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0x00000000 Task Linu Freestk 0 n/a
                              Error status: 0x00
                              Aux0 errors 0,0,0
                              Aux1 errors 0,0,0
                              MCU temperature: min 38.9, current 39.0, max 39.8
                              Supply voltage: min 24.0, current 24.3, max 24.4, under voltage events: 0, over voltage events: 0, power good: yes
                              12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                              Driver 0: position 0, standstill, reads 18607, writes 2 timeouts 0, SG min/max 0/240
                              Driver 1: position 0, standstill, reads 18607, writes 2 timeouts 0, SG min/max 0/231
                              Driver 2: position 4760, standstill, reads 18607, writes 2 timeouts 0, SG min/max 0/239
                              Driver 3: position 0, standstill, reads 18607, writes 2 timeouts 0, SG min/max 0/254
                              Driver 4: position 0, standstill, reads 18607, writes 2 timeouts 0, SG min/max 0/792
                              Driver 5: position 0, standstill, reads 18606, writes 2 timeouts 0, SG min/max 0/1023
                              Date/time: 2021-01-07 00:26:32
                              Slowest loop: 89.52ms; fastest: 0.04ms
                              === Storage ===
                              Free file entries: 10
                              SD card 0 not detected, interface speed: 37.5MBytes/sec
                              SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                              === Move ===
                              DMs created 125, maxWait 131ms, bed compensation in use: none, comp offset 0.000
                              === MainDDARing ===
                              Scheduled moves 95097, completed moves 95097, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                              === AuxDDARing ===
                              Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                              === Heat ===
                              Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                              Heater 0 is on, I-accum = 0.3
                              Heater 1 is on, I-accum = 0.3
                              === GCodes ===
                              Segments left: 0
                              Movement lock held by null
                              HTTP* is doing "M122" in state(s) 0
                              Telnet is idle in state(s) 0
                              File* is idle in state(s) 0
                              USB is idle in state(s) 0
                              Aux is idle in state(s) 0
                              Trigger* is idle in state(s) 0
                              Queue* is idle in state(s) 0
                              LCD is idle in state(s) 0
                              SBC is idle in state(s) 0
                              Daemon is idle in state(s) 0
                              Aux2 is idle in state(s) 0
                              Autopause is idle in state(s) 0
                              Code queue is empty.
                              === CAN ===
                              Messages queued 89455, send timeouts 0, received 242, lost 0, longest wait 20ms for reply type 6024, free buffers 48
                              === SBC interface ===
                              State: 4, failed transfers: 0
                              Last transfer: 1ms ago
                              RX/TX seq numbers: 28721/28721
                              SPI underruns 0, overruns 0
                              Number of disconnects: 0, IAP RAM available 0x2c8a8
                              Buffer RX/TX: 0/0-0
                              === Duet Control Server ===
                              Duet Control Server v3.2.0
                              Code buffer space: 4096
                              Configured SPI speed: 8000000 Hz
                              Full transfers per second: 51.22
                              Maximum length of RX/TX data transfers: 2584/1324
                              

                              Diagnostics for board 1

                              M122 B1
                              Diagnostics for board 1:
                              Duet EXP3HC firmware version 3.2 (2021-01-05)
                              Bootloader ID: not available
                              Never used RAM 154848, free system stack 156 words
                              HEAT 90 CanAsync 94 CanRecv 84 TMC 30 MAIN 287 AIN 257
                              Last reset 01:06:25 ago, cause: power up
                              Last software reset data not available
                              Driver 0: position 0, 80.0 steps/mm,  standstill, reads 48117, writes 0 timeouts 0, SG min/max not available
                              Driver 1: position 290732, 205.0 steps/mm,  standstill, reads 48116, writes 0 timeouts 0, SG min/max 0/698
                              Driver 2: position 0, 80.0 steps/mm,  standstill, reads 48115, writes 0 timeouts 0, SG min/max not available
                              Moves scheduled 74262, completed 74262, in progress 0, hiccups 144
                              No step interrupt scheduled
                              VIN: 24.7V, V12: 12.3V
                              MCU temperature: min 43.8C, current 44.0C, max 44.2C
                              Ticks since heat task active 138, ADC conversions started 3985880, completed 3985879, timed out 0
                              Last sensors broadcast 0x00000000 found 0 141 ticks ago, loop time 0
                              CAN messages queued 22, send timeouts 0, received 15281, lost 0, free buffers 36
                              

                              config.g

                              ; Configuration file for Duet 3 (firmware version 3)
                              ; executed by the firmware on start-up
                              ;
                              ; generated by RepRapFirmware Configuration Tool v3.1.4 on Sat Aug 01 2020 21:20:25 GMT-0400 (Eastern Daylight Time)
                              
                              ; General preferences
                              G90                                                ; send absolute coordinates...
                              M83                                                ; ...but relative extruder moves
                              M550 P"Duet 3"                                     ; set printer name
                              M669 K1                                            ; select CoreXY mode
                              
                              ; Drives
                              ; Dnnn 0=constant off time, 1=random off time, 2=spread cycle, 3=stealthChop or stealthChop2
                              
                              M569 P0.0 S1 D2                                    ; Z1 physical drive goes forwards, spread cycle
                              M569 P0.1 S1 D2                                    ; Z2 physical drive goes forwards, spread cycle
                              M569 P0.2 S1 D2                                    ; Z3 physical drive goes forwards, spread cycle
                              M569 P0.3 S1 D2                                    ; Z4 physical drive goes backwards, spread cycle
                              M569 P0.4 S1 D2                                    ; X  physical drive goes forwards, spread cycle
                              M569 P0.5 S1 D2                                    ; Y  physical drive goes forwards, spread cycle
                              M569 P1.1 S1 D2                                    ; E0 physical drive goes forwards, spread cycle
                              
                              ; set drive mappings            
                              M584 X0.4 Y0.5 Z0.0:0.1:0.2:0.3 E1.1      
                              
                              ; leadscrews at rear left, front middle, rear right
                              M671 X14.891:14.891:567.309:567.309 Y-44.113:466.887:466.887:-44.113 S20
                              
                              ; configure microstepping with interpolation                
                              M350 X16 Y16 Z1 E8 I1
                                     
                              ; set steps per mm
                              ;M92 X160.00 Y160.00 Z200.00 E172
                              M92 X160.00 Y160.00 Z200.00 E205
                              
                              ; set maximum instantaneous speed changes  (jerk) (mm/min)      	   
                              M566 X500.00 Y500.00 Z50.00 E3000.00  
                              
                              ; set maximum speeds (mm/min)     
                              M203 X30000.00 Y30000.00 Z1200.00 E180000.00
                              
                              ; set accelerations (mm/s^2)
                              M201 X10000.00 Y10000.00 Z100.00 E5000.00
                              
                              ; set motor currents (mA) and motor idle factor in percent                          
                              M906 X1500 Y1500 Z1500 E1300 I80  
                              
                              ; Set idle timeout
                              M84 S30                                            
                              
                              ; Axis Limits
                              M208 X0 Y0 Z0 S1                                   	; set axis minima
                              M208 X515 Y515 Z540 S0                             	; set axis maxima
                              
                              ; Endstops
                              M574 X1 S1 P"io1.in"								; configure active-high endstop for low end on X via pin io1.in
                              M574 Y1 S1 P"io0.in"                               	; configure active-high endstop for low end on Y via pin io0.in
                              M574 Z1 S2                                         	; configure Z-probe endstop for low end on Z
                              
                              ; Z-Probe
                              M950 S0 C"io4.out"                            		; create servo pin 0 for BLTouch
                              M558 P9 C"!io4.in" H10 A5 R0.2 S0.005 F100 T10000   ; set Z probe type to bltouch(P9),the dive height(H), number of repeats(A), recovery time(R), speed(F dive and T travel)
                              ;M558 P8 C"^io4.in" H30 F600 T6000             		; set Z probe type to switch and the dive height + speeds
                              
                              G31 P500 X43.00 Y-24 Z1.82					   		; set Z probe trigger value, offset and trigger height
                              ;G31 P1000 X0 Y0 Z0                         	   	; set Z probe trigger value, offset and trigger height
                              M557 X40:480 Y40:450 S55:51.2                       ; define mesh grid
                              
                              ; Heaters
                              M308 S0 P"temp0" Y"thermistor" T100000 B4138       	; configure sensor 0 as thermistor on pin temp0
                              M950 H0 C"out0" T0                                 	; create bed heater output on out0 and map it to sensor 0
                              M307 H0 B0 S1.00                                   	; disable bang-bang mode for the bed heater and set PWM limit
                              M140 H0                                            	; map heated bed to heater 0
                              M143 H0 S105                                       	; set temperature limit for heater 0 to 100C
                              
                              M308 S1 P"temp1" Y"thermistor" T100000 B4138   		; configure sensor 1 as thermistor on pin temp1
                              M950 H1 C"out1" T1                             		; create nozzle heater output on out1 and map it to sensor 1
                              M307 H1 B0 S1.00                                   	; disable bang-bang mode for heater  and set PWM limit
                              
                              ; Fans
                              M950 F0 C"out7" Q500                               	; create fan 0 on pin out7 and set its frequency
                              M106 P0 C"PART COOLING" S0 H-1                     	; set fan 0 name and value. Thermostatic control is turned off
                              M950 F1 C"out8" Q500                               	; create fan 1 on pin out8 and set its frequency
                              M106 P1 C"AQUA" S1 H1 T45                          	; set fan 1 name and value. Thermostatic control is turned on
                              
                              ; Tools
                              M563 P0 S"Hotend" D0 H1 F0                   	   	; define tool 0
                              G10 P0 X-3 Y24 Z0                                   ; set tool 0 axis offsets
                              G10 P0 R0 S0                                       	; set initial tool 0 active and standby temperatures to 0C
                                                               
                              
                              ; set voltage thresholds and actions to run on power loss
                              M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" 
                              
                              ; select first tool
                              T0													                                                 
                              
                              ; Print and travel acceleration
                              ;M204 P6000 T4000								   
                              
                              ; fix for BLTouch self-test at startup 
                              ;M280 P0 S60 ; BLtouch - toggle switch mode
                              ;G4 P1000 ; wait 1 second
                              ;M280 P0 S120 ; BLtouch toggle self-test
                              
                              ; pressure advance								    							   	   
                              M572 D0 S0.046
                              
                              ; Firmware retraction
                              M207 D0 S0.8 F900 Z0.1 R0
                              
                              ; Dynamic acceleration. Cancel ringing at 27.59Hz
                              M593 F27.59
                              
                              ; Use config override
                              M501
                              
                              
                              dc42undefined 1 Reply Last reply Reply Quote 0
                              • evomotorsundefined
                                evomotors
                                last edited by

                                @dc42

                                I tried to connect XY to expansion board and E to Duet3, now X and Y missing steps... So it has to be something wrong...

                                dc42undefined 1 Reply Last reply Reply Quote 0
                                • dc42undefined
                                  dc42 administrators @evomotors
                                  last edited by

                                  @evomotors said in Duet3 6CH + 3CH expansion board - Missing steps.:

                                  @dc42

                                  I tried to connect XY to expansion board and E to Duet3, now X and Y missing steps... So it has to be something wrong...

                                  Are you sure they are missing steps? Has there been a layer shift?

                                  Duet WiFi hardware designer and firmware engineer
                                  Please do not ask me for Duet support via PM or email, use the forum
                                  http://www.escher3d.com, https://miscsolutions.wordpress.com

                                  1 Reply Last reply Reply Quote 0
                                  • dc42undefined
                                    dc42 administrators @evomotors
                                    last edited by

                                    @evomotors said in Duet3 6CH + 3CH expansion board - Missing steps.:

                                    So there is 1233.9 mm discrepancy...

                                    Please provide the GCode file you are printing, and I will run it on my bench system, using the config.g file you have already posted.

                                    Duet WiFi hardware designer and firmware engineer
                                    Please do not ask me for Duet support via PM or email, use the forum
                                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                                    evomotorsundefined 2 Replies Last reply Reply Quote 0
                                    • evomotorsundefined
                                      evomotors @dc42
                                      last edited by

                                      @dc42
                                      No, It is likely a layer shifts on every layer when I wired YX motors to the expansion board.

                                      So any motor connected to expansion board is under powered for some reason in my setup.

                                      1 Reply Last reply Reply Quote 0
                                      • evomotorsundefined
                                        evomotors @dc42
                                        last edited by

                                        @dc42 said in Duet3 6CH + 3CH expansion board - Missing steps.:

                                        @evomotors said in Duet3 6CH + 3CH expansion board - Missing steps.:

                                        So there is 1233.9 mm discrepancy...

                                        Please provide the GCode file you are printing, and I will run it on my bench system, using the config.g file you have already posted.

                                        To save time I tried just a simple cookie cutter from thingiverse bun.gcode

                                        But I think you are right and the issue could be with motor stalling, but it's not stalling because of the bed motor or mechanical issue as when I switched XY to the EXP3HC, XY started stalling. So there is something wrong with drivers current adjustments.

                                        I have exactly the same issue with tool board. I had to use E motor driver on Duet 3 instead of Tool-Board as I had exactly the same issue.

                                        deckingmanundefined 1 Reply Last reply Reply Quote 0
                                        • deckingmanundefined
                                          deckingman @evomotors
                                          last edited by

                                          @evomotors Just a suggestion - if you run M122 B1 during a print do all the voltages look good? No under voltage events or anything like that? It sounds a bit like power supply issue (to the expansion board) but I'd have thought that would show up as under voltage.

                                          Ian
                                          https://somei3deas.wordpress.com/
                                          https://www.youtube.com/@deckingman

                                          evomotorsundefined 1 Reply Last reply Reply Quote 0
                                          • evomotorsundefined
                                            evomotors @deckingman
                                            last edited by

                                            @deckingman said in Duet3 6CH + 3CH expansion board - Missing steps.:

                                            @evomotors Just a suggestion - if you run M122 B1 during a print do all the voltages look good? No under voltage events or anything like that? It sounds a bit like power supply issue (to the expansion board) but I'd have thought that would show up as under voltage.

                                            M122 B1 always showing up something like this, never under voltage.

                                            VIN: 24.7V, V12: 12.3V
                                            
                                            1 Reply Last reply Reply Quote 0
                                            • First post
                                              Last post
                                            Unless otherwise noted, all forum content is licensed under CC-BY-SA