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    Strange behavior during probing in 3.3 (solved in 3.4b3)

    Scheduled Pinned Locked Moved Solved
    Beta Firmware
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    • fcwiltundefined
      fcwilt @Th0mpy
      last edited by

      @th0mpy

      I've re-posted your files using the </> tag.

      ; Configuration file for Duet 3 (firmware version 3.3)
      ; executed by the firmware on start-up
      ;
      ; generated by RepRapFirmware Configuration Tool v3.3.1 on Sun Aug 29 2021 21:00:02 GMT-0500 (Central Daylight Time)
      
      ; General preferences
      G90                                                             ; send absolute coordinates...
      M83                                                             ; ...but relative extruder moves
      M550 P"Duet 3"                                                  ; set printer name
      M669 K1                                                         ; select CoreXY mode
      ;M669 K0
      
      
      ; Drives
      M569 P1.1 S0                                                    ; A
      M569 P1.2 S0                                                    ; B
      M569 P1.0 S1                                                    ; Extruder
      
      M569 P0.0 S1                                                    ; Z0
      M569 P0.1 S1                                                    ; Z1
      M569 P0.2 S0                                                    ; Z2
      M569 P0.3 S0                                                    ; Z3
      
      M584 X1.2 Y1.1 Z0.0:0.1:0.2:0.3 E1.0                            ; set drive mapping
      M671 X-60:-60:400:400 Y-60:400:400:-60 S5						; bed leveling coordinates
      M350 X16 Y16 Z16 E16 I1                                         ; configure microstepping with interpolation
      M92 X160.00 Y160.00 Z800.00 E415.00                             ; set steps per mm
      M566 X900.00 Y900.00 Z120.00 E60.00                             ; set maximum instantaneous speed changes (mm/min)
      M203 X60000.00 Y60000.00 Z2000.00 E180.00                       ; set maximum speeds (mm/min)
      M201 X2800.00 Y2800.00 Z250.00 E20.00                           ; set accelerations (mm/s^2)
      M906 X1800 Y1800 Z1800 E500 I30                                 ; set motor currents (mA) and motor idle factor in per cent
      M84 S30                                                         ; Set idle timeout
      
      ; Axis Limits
      M208 X0 Y0 Z0 S1                                                ; set axis minima
      M208 X350 Y350 Z350 S0                                          ; set axis maxima
      
      ; Endstops
      M574 X2 S1 P"!io8.in"                                            ; configure active-high endstop for high end on X via pin io8.in
      M574 Y2 S1 P"!io6.in"                                            ; configure active-high endstop for high end on Y via pin io6.in
      M574 Z1 S2                                                      ; configure Z-probe endstop for low end on Z
      
      ; Z-Probe
      M558 P8 C"io3.in" H30 F1000 T20000                              ; set Z probe type to unmodulated and the dive height + speeds
      G31 P500 X0 Y25 Z0                                              ; set Z probe trigger value, offset and trigger height
      M557 X25:345 Y25:345 P4                                         ; define mesh grid
      
      ; Heaters
      M308 S0 P"1.temp0" Y"thermistor" T100000 B4725 C7.06e-8         ; configure sensor 0 as thermistor on pin temp2
      M950 H0 C"1.out0" T0                                            ; create bed heater output on 1.out0 and map it to sensor 0
      M307 H0 B0 S1.00                                                ; disable bang-bang mode for the bed heater and set PWM limit
      M140 H0                                                         ; map heated bed to heater 0
      M143 H0 S120                                                    ; set temperature limit for heater 0 to 120C
      M308 S1 P"temp0" Y"thermistor" T100000 B4725 C7.06e-8           ; configure sensor 1 as thermistor on pin temp0
      M950 H1 C"out1" T1                                              ; create nozzle heater output on out1 and map it to sensor 1
      M307 H1 B0 S1.00                                                ; disable bang-bang mode for heater  and set PWM limit
      M143 H1 S280                                                    ; set temperature limit for heater 1 to 280C
      ;M308 S2 P"temp1" Y"thermistor" T100000 B4725 C7.06e-8          ; configure sensor 2 as thermistor on pin temp1
      M308 S2 P"temp1" Y"thermistor" T10000 B3940 A"Chamber Temp" 
      ;M950 H2 C"!1.out2" T2                                          ; create chamber heater output on !1.out2 and map it to sensor 2
      ;M307 H2 B0 S1.00                                               ; disable bang-bang mode for the chamber heater and set PWM limit
      ;M141 H2                                                        ; map chamber to heater 2
      ;M143 H2 S280                                                   ; set temperature limit for heater 2 to 280C
      
      ; Fans
      M950 F0 C"out7" Q500                                            ; create fan 0 on pin out7 and set its frequency
      M106 P0 S0 H-1                                                  ; set fan 0 value. Thermostatic control is turned off
      M950 F1 C"out8" Q500                                            ; create fan 1 on pin out8 and set its frequency
      M106 P1 S0.5 H1 T45                                             ; set fan 1 value. Thermostatic control is turned on
      
      ; Tools
      M563 P0 D0 H1 F0                                                ; define tool 0
      G10 P0 X0 Y0 Z0                                                 ; set tool 0 axis offsets
      G10 P0 R0 S0                                                    ; set initial tool 0 active and standby temperatures to 0C
      
      ; Custom settings are not defined
      
      ; Miscellaneous
      M501                                                            ; load saved parameters from non-volatile memory
      T0                                                              ; select first tool
      
      
      ; bed.g
      ; called to perform automatic bed compensation via G32
      ;
      ; generated by RepRapFirmware Configuration Tool v3.3.1 on Sun Aug 29 2021 21:00:02 GMT-0500 (Central Daylight Time)
      M561 ; clear any bed transform
      
      
      G30 P0 X25 Y25 Z-99999
      G30 P1 X25 Y350 Z-99999
      G30 P2 X345 Y350 Z-99999
      G30 P3 X345 Y25 S4 Z-99999
      
      ;G29  ; probe the bed and enable compensation
      
      
      

      Printers: a small Utilmaker style, a small CoreXY and a E3D MS/TC setup. Various hotends. Using Duet 3 hardware running 3.4.6

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      • o_lampeundefined
        o_lampe @Th0mpy
        last edited by

        @th0mpy
        I'm sure it's an issue between 6HC and 3HC boards. Either, they don't run on the same firmware or there is a timing issue related to CAN-bus.

        Th0mpyundefined 1 Reply Last reply Reply Quote 0
        • Th0mpyundefined
          Th0mpy @PaulHew
          last edited by

          @paulhew I tried that and no change, The thing to keep in mind is that it also shows this behavior during a mesh probe too so the bed.g file wouldn't matter.

          Usually the team that scores the most points wins the game.

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          • Th0mpyundefined
            Th0mpy @o_lampe
            last edited by

            @o_lampe I double and triple checked the firmware on both. It's updated, and I tried forcing the update as well.

            How would I determine if there's a timing issue? If there is one, what would I do to correct it?

            Usually the team that scores the most points wins the game.

            Th0mpyundefined 1 Reply Last reply Reply Quote 0
            • Th0mpyundefined
              Th0mpy @Th0mpy
              last edited by

              I ran a G32 and ran M122 and M122 B1. It doesn't seem there's a timing issue:

              M122
              === Diagnostics ===
              RepRapFirmware for Duet 3 MB6HC version 3.3 (2021-06-15 21:45:47) running on Duet 3 MB6HC v1.01 or later (SBC mode)
              Board ID: 08DJM-956L2-G43S8-6J9FA-3S86N-1B36F
              Used output buffers: 3 of 40 (13 max)
              === RTOS ===
              Static ram: 150904
              Dynamic ram: 62060 of which 204 recycled
              Never used RAM 141024, free system stack 150 words
              Tasks: SBC(ready,7.3%,328) HEAT(delaying,0.0%,325) Move(notifyWait,0.0%,265) CanReceiv(notifyWait,0.0%,799) CanSender(notifyWait,0.0%,362) CanClock(delaying,0.0%,339) TMC(notifyWait,7.8%,59) MAIN(running,84.6%,922) IDLE(ready,0.2%,29), total 100.0%
              Owned mutexes: HTTP(MAIN)
              === Platform ===
              Last reset 00:09:01 ago, cause: power up
              Last software reset at 2021-09-01 23:20, reason: MemoryProtectionFault iaccViol, GCodes spinning, available RAM 138212, slot 1
              Software reset code 0x4163 HFSR 0x00000000 CFSR 0x00000001 ICSR 0x00400804 BFAR 0x00000000 SP 0x2041b188 Task MAIN Freestk 1665 ok
              Stack: 2042b348 2042b2f0 00000000 00450e65 00000000 00450e75 fffffffe 210f0000 00000000 0000000a 00000000 2042b7f0 20419728 2042dbe4 00000000 00000001 00000000 0047a1d7 2042dbe4 fffc0000 003fffff 0047a51f 00000000 0047a6f7 20429710 ffffffff 2042b348
              Error status: 0x00
              Step timer max interval 127
              MCU temperature: min 39.9, current 40.2, max 40.4
              Supply voltage: min 24.6, current 24.8, max 24.8, under voltage events: 0, over voltage events: 0, power good: yes
              12V rail voltage: min 12.0, current 12.0, max 12.1, under voltage events: 0
              Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
              Driver 0: position 55200, standstill, reads 49529, writes 3 timeouts 0, SG min/max 0/310
              Driver 1: position 55200, standstill, reads 49529, writes 3 timeouts 0, SG min/max 0/264
              Driver 2: position 24000, standstill, reads 49529, writes 3 timeouts 0, SG min/max 0/253
              Driver 3: position 0, standstill, reads 49530, writes 3 timeouts 0, SG min/max 0/301
              Driver 4: position 0, standstill, reads 49533, writes 0 timeouts 0, SG min/max not available
              Driver 5: position 0, standstill, reads 49533, writes 0 timeouts 0, SG min/max not available
              Date/time: 2021-09-02 07:48:41
              Slowest loop: 165.42ms; fastest: 0.04ms
              === Storage ===
              Free file entries: 10
              SD card 0 not detected, interface speed: 37.5MBytes/sec
              SD card longest read time 0.0ms, write time 0.0ms, max retries 0
              === Move ===
              DMs created 125, maxWait 516238ms, bed compensation in use: none, comp offset 0.000
              === MainDDARing ===
              Scheduled moves 23, completed moves 23, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
              === AuxDDARing ===
              Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
              === Heat ===
              Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
              Heater 1 is on, I-accum = 0.0
              === GCodes ===
              Segments left: 0
              Movement lock held by null
              HTTP* is doing "M122" in state(s) 0
              Telnet is idle in state(s) 0
              File is idle in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger* is idle in state(s) 0
              Queue is idle in state(s) 0
              LCD is idle in state(s) 0
              SBC is idle in state(s) 0
              Daemon is idle in state(s) 0
              Aux2 is idle in state(s) 0
              Autopause is idle in state(s) 0
              Code queue is empty.
              === CAN ===
              Messages queued 535, received 453, lost 0, longest wait 1ms for reply type 6013, peak Tx sync delay 164, free buffers 49 (min 46), ts 280/280/0
              Tx timeouts 0,0,0,0,0,0
              === SBC interface ===
              State: 4, failed transfers: 1, checksum errors: 0
              Last transfer: 2ms ago
              RX/TX seq numbers: 18472/18472
              SPI underruns 0, overruns 0
              Disconnects: 0, timeouts: 0, IAP RAM available 0x2c810
              Buffer RX/TX: 0/0-0
              === Duet Control Server ===
              Duet Control Server v3.3.0
              Code buffer space: 4096
              Configured SPI speed: 8000000Hz
              Full transfers per second: 36.15, max wait times: 9.9ms/0.0ms
              Codes per second: 0.84
              Maximum length of RX/TX data transfers: 3292/824
              
              M122 B1
              Diagnostics for board 1:
              Duet EXP3HC firmware version 3.3 (2021-06-15 16:12:41)
              Bootloader ID: not available
              Never used RAM 158872, free system stack 4373 words
              Tasks: Move(notifyWait,0.0%,125) HEAT(delaying,0.0%,104) CanAsync(notifyWait,0.0%,69) CanRecv(notifyWait,0.0%,80) CanClock(notifyWait,0.0%,71) TMC(notifyWait,7.2%,29) MAIN(running,91.4%,338) IDLE(ready,0.0%,39) AIN(delaying,1.3%,263), total 100.0%
              Last reset 00:10:08 ago, cause: power up
              Last software reset data not available
              Driver 0: position 0, 415.0 steps/mm,  standstill, reads 61454, writes 16 timeouts 0, SG min/max 0/0, steps req 0 done 0
              Driver 1: position -1600, 160.0 steps/mm,  standstill, reads 61452, writes 19 timeouts 0, SG min/max 0/237, steps req 329600 done 216085
              Driver 2: position 225600, 160.0 steps/mm,  standstill, reads 61453, writes 19 timeouts 0, SG min/max 0/247, steps req 548800 done 323370
              Moves scheduled 10, completed 10, in progress 0, hiccups 0, step errors 0, maxPrep 43, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0
              Peak sync jitter 0/15, peak Rx sync delay 181, resyncs 0/0, no step interrupt scheduled
              VIN: 25.0V, V12: 12.2V
              MCU temperature: min 19.1C, current 28.6C, max 28.6C
              Ticks since heat task active 173, ADC conversions started 608960, completed 608960, timed out 0, errs 0
              Last sensors broadcast 0x00000001 found 1 178 ticks ago, loop time 0
              CAN messages queued 4741, send timeouts 0, received 5446, lost 0, free buffers 37, min 37, error reg 110000
              dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 414, adv 36852/37076
              

              Usually the team that scores the most points wins the game.

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              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                That is rather strange. Can you try adding M400 between your G30 commands in bed.g and see if that makes a difference?

                Z-Bot CoreXY Build | Thingiverse Profile

                Th0mpyundefined 1 Reply Last reply Reply Quote 0
                • Th0mpyundefined
                  Th0mpy @Phaedrux
                  last edited by Th0mpy

                  @phaedrux Unfortunately that made no difference. Still drops Z in the during Y moves.

                  One interesting thing... If I put an R0.5 in the M558 command it does not move Z until .5 seconds after it started moving. If I up that to R1 it completes the Y move then probes (it takes just about a second to move from point to point). This tells me that when it's traveling along the Y axis it's also trying to probe Z. Not sure why in the X axis it doesn't do this.

                  Usually the team that scores the most points wins the game.

                  Th0mpyundefined 1 Reply Last reply Reply Quote 0
                  • Th0mpyundefined
                    Th0mpy @Th0mpy
                    last edited by

                    So, I just changed the axis maximums to 300 and the bed.g to a 300 on the Y axis as well. That fixed it. I don't know why, and I'm attempting to play with it to see what exactly happened. I'll report back if I can determine what is going wrong.

                    Usually the team that scores the most points wins the game.

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                    • Th0mpyundefined
                      Th0mpy
                      last edited by

                      Ok so I think it's an issue with the probe offset. The maximum being 350, the probe could not hit that. The maximum should be 375 and the bed.g should be 350. If I'm figuring this correctly. IMHO could the 3hc be throwing an error that we don't see, which could cause the movement to be complete?

                      Usually the team that scores the most points wins the game.

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                      • Phaedruxundefined
                        Phaedrux Moderator
                        last edited by

                        Would you be able to test this in standalone mode?

                        https://duet3d.dozuki.com/Wiki/Getting_Started_With_Duet_3#Section_Running_in_standalone_mode

                        Z-Bot CoreXY Build | Thingiverse Profile

                        Th0mpyundefined 2 Replies Last reply Reply Quote 0
                        • Th0mpyundefined
                          Th0mpy @Phaedrux
                          last edited by

                          @phaedrux I will see if I can tonight.

                          Usually the team that scores the most points wins the game.

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                          • Th0mpyundefined
                            Th0mpy @Phaedrux
                            last edited by

                            @phaedrux Using the exact same config file in standalone mode. It behaves the same. Side note I was able to fix it on a G32 but not a G29. It may not be an issue because it does not have as far to go, but I feel it could still give false readings. I'll keep playing.

                            Usually the team that scores the most points wins the game.

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                            • Phaedruxundefined
                              Phaedrux Moderator
                              last edited by

                              While you're in standalone mode would you be able to test 3.4 beta 3 as well? Simply because it would be easiest to go back and forth while in standalone mode.

                              https://github.com/Duet3D/RepRapFirmware/releases/tag/3.4.0beta3

                              Z-Bot CoreXY Build | Thingiverse Profile

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                              • Th0mpyundefined
                                Th0mpy
                                last edited by Th0mpy

                                @phaedrux Ok yeah, that took care of it. All is working! Does that mean you know what the issue is? 🙂

                                UPDATE: I hooked it back up to the Pi and updated to the unstable branch. We're still looking good!

                                Usually the team that scores the most points wins the game.

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                                • Phaedruxundefined
                                  Phaedrux Moderator
                                  last edited by

                                  Glad that's fixed it. Please keep up with the 3.4 releases as they come on the way to the final release just to confirm that it stays fixed.

                                  Z-Bot CoreXY Build | Thingiverse Profile

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