Voron 2.4 3MB6 §EB config issues.
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@Titus-A-Duxass so your 3HC is running 3.3 and your 6HC is running 3.4.5 so you're out of sync there.
you also need to update the bootloader on the 3HC. it can be found here https://github.com/Duet3D/Duet3Bootloader/releases/download/2.4/Duet3Bootloader-SAME5x.bin
and instructions https://docs.duet3d.com/en/User_manual/RepRapFirmware/Updating_bootloader -
@jay_s_uk I thought I read somewhere that after v3.3 it does not matter is they are out of sync. I will, nevertheless, update both the 3HC firmware and bootloader.
Thanks, I'll be back.
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@Titus-A-Duxass they definitely need to be in sync as the protocol will change between updates
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@jay_s_uk Okay updates carried out but 3EB firmware is still at 3.3.
M122
=== Diagnostics ===
RepRapFirmware for Duet 3 MB6HC version 3.4.5 (2022-11-30 19:35:23) running on Duet 3 MB6HC v1.01 (standalone mode)
Board ID: 08DJM-9P63L-DJ3T8-6JKDA-3SJ6N-KB7MA
Used output buffers: 3 of 40 (18 max)
=== RTOS ===
Static ram: 152760
Dynamic ram: 97336 of which 184 recycled
Never used RAM 100392, free system stack 208 words
Tasks: NETWORK(ready,30.8%,210) ETHERNET(notifyWait,0.1%,453) HEAT(notifyWait,0.0%,328) Move(notifyWait,0.0%,351) CanReceiv(notifyWait,0.0%,904) CanSender(notifyWait,0.0%,336) CanClock(delaying,0.0%,339) TMC(notifyWait,7.9%,91) MAIN(running,61.1%,925) IDLE(ready,0.1%,30), total 100.0%
Owned mutexes:
=== Platform ===
Last reset 00:02:23 ago, cause: power up
Last software reset at 2022-12-21 10:57, reason: MemoryProtectionFault mmarValid daccViol, GCodes spinning, available RAM 100392, slot 1
Software reset code 0x4163 HFSR 0x00000000 CFSR 0x00000082 ICSR 0x00400804 BFAR 0xffd693d2 SP 0x2041b4f8 Task MAIN Freestk 1670 ok
Stack: 00000002 2042ecfc ffffffff 00000000 00000216 00489385 00488c2e 610f0000 ffffffff 2042c550 20419a84 2042d1ac 00000000 00000001 00000000 00488ee7 2042d1ac fdfc0000 003ff7ff 0048922f 042fffa0 ffffffff ffffffff ffffffff ffffffff ffffffff ffffffff
Error status: 0x00
Step timer max interval 127
MCU temperature: min 34.3, current 41.7, max 41.7
Supply voltage: min 23.9, current 23.9, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes
12V rail voltage: min 12.0, current 12.1, max 12.2, under voltage events: 0
Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
Events: 0 queued, 0 completed
Driver 0: standstill, SG min 0, mspos 8, reads 13222, writes 11 timeouts 0
Driver 1: standstill, SG min 0, mspos 2, reads 13219, writes 14 timeouts 0
Driver 2: standstill, SG min 0, mspos 8, reads 13222, writes 11 timeouts 0
Driver 3: standstill, SG min 0, mspos 2, reads 13220, writes 14 timeouts 0
Driver 4: standstill, SG min 0, mspos 2, reads 13220, writes 14 timeouts 0
Driver 5: standstill, SG min 0, mspos 2, reads 13220, writes 14 timeouts 0
Date/time: 2022-12-21 11:00:12
Slowest loop: 21.07ms; fastest: 0.05ms
=== Storage ===
Free file entries: 10
SD card 0 detected, interface speed: 25.0MBytes/sec
SD card longest read time 3.0ms, write time 0.0ms, max retries 0
=== Move ===
DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
=== MainDDARing ===
Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== AuxDDARing ===
Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== Heat ===
Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
Heater 1 is on, I-accum = 0.0
=== GCodes ===
Segments left: 0
Movement lock held by null
HTTP is idle in state(s) 0
Telnet is idle in state(s) 0
File is idle in state(s) 0
USB is idle in state(s) 0
Aux is idle in state(s) 0
Trigger is idle in state(s) 0
Queue is idle in state(s) 0
LCD is idle in state(s) 0
SBC is idle in state(s) 0
Daemon is idle in state(s) 0
Aux2 is idle in state(s) 0
Autopause is idle in state(s) 0
Code queue is empty
=== CAN ===
Messages queued 1305, received 41, lost 0, boc 0
Longest wait 2ms for reply type 6024, peak Tx sync delay 321, free buffers 50 (min 49), ts 720/719/0
Tx timeouts 0,0,0,0,0,0
=== Network ===
Slowest loop: 18.51ms; fastest: 0.03ms
Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
HTTP sessions: 1 of 8
= Ethernet =
State: active
Error counts: 0 0 0 1 0 0
Socket states: 5 2 2 2 2 0 0 0
=== Multicast handler ===
Responder is inactive, messages received 0, responses 0M122 B1
Diagnostics for board 1:
Duet EXP3HC firmware version 3.3 (2021-06-15 16:12:41)
Bootloader ID: SAME5x bootloader version 2.4 (2021-12-10)
Never used RAM 159104, free system stack 4400 words
Tasks: Move(notifyWait,0.0%,160) HEAT(delaying,0.0%,118) CanAsync(notifyWait,0.0%,69) CanRecv(notifyWait,0.0%,82) CanClock(notifyWait,0.0%,71) TMC(notifyWait,7.2%,63) MAIN(running,91.5%,439) IDLE(ready,0.0%,39) AIN(delaying,1.3%,263), total 100.0%
Last reset 00:02:14 ago, cause: power up
Last software reset data not available
Driver 0: position 0, 1746.2 steps/mm, standstill, reads 60093, writes 16 timeouts 0, SG min/max 0/0, steps req 0 done 0
Driver 1: position 0, 320.0 steps/mm, standstill, reads 60094, writes 16 timeouts 0, SG min/max 0/0, steps req 0 done 0
Driver 2: position 0, 320.0 steps/mm, standstill, reads 60095, writes 16 timeouts 0, SG min/max 0/0, steps req 0 done 0
Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0
Peak sync jitter -1/8, peak Rx sync delay 180, resyncs 0/0, no step interrupt scheduled
VIN: 24.1V, V12: 12.2V
MCU temperature: min 32.7C, current 33.9C, max 33.9C
Ticks since heat task active 80, ADC conversions started 134257, completed 134257, timed out 0, errs 0
Last sensors broadcast 0x00000000 found 0 85 ticks ago, loop time 0
CAN messages queued 36, send timeouts 0, received 1214, lost 0, free buffers 37, min 37, error reg 110064
dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 021.12.2022, 11:01:45 M115 B1
Duet EXP3HC firmware version 3.3 (2021-06-15 16:12:41) -
@Titus-A-Duxass how are you trying to update the 3HC firmware?
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@Titus-A-Duxass so you're uploading the 3HC firmware file to the system tab?
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@jay_s_uk I follow the instructions on that page.
Download the file (Duet2and3firmware-345.zip)
and then upload via the DWC
Upload System Files button. -
@Titus-A-Duxass i don't know why its not updating that way then.
you could try turning the machine off, and turning all the dip switches off on the 3HC. This causes the board to request and update the firmware on startup https://docs.duet3d.com/Duet3D_hardware/Duet_3_family/Duet_3_Expansion_3HC#address
can you also check what version of DWC you're running? it shows under general settings -
@jay_s_uk Thanks, that forced it -
21.12.2022, 11:21:12 M115 B1
Duet EXP3HC rev 1.01 or earlier firmware version 3.4.4 (2022-10-14 11:45:56)21.12.2022, 11:22:45 M122 B1
Diagnostics for board 1:
Duet EXP3HC rev 1.01 or earlier firmware version 3.4.4 (2022-10-14 11:45:56)
Bootloader ID: SAME5x bootloader version 2.4 (2021-12-10)
All averaging filters OK
Never used RAM 158932, free system stack 200 words
Tasks: Move(notifyWait,0.0%,160) HEAT(notifyWait,0.0%,108) CanAsync(notifyWait,0.0%,69) CanRecv(notifyWait,0.0%,82) CanClock(notifyWait,0.0%,71) TMC(notifyWait,7.4%,99) MAIN(running,91.2%,441) IDLE(ready,0.0%,40) AIN(delaying,1.3%,263), total 100.0%
Last reset 00:02:06 ago, cause: power up
Last software reset data not available
Driver 0: pos 0, 1746.2 steps/mm,standstill, SG min 0, mspos 2, reads 27429, writes 16 timeouts 0, steps req 0 done 0
Driver 1: pos 0, 320.0 steps/mm,standstill, SG min 0, mspos 2, reads 27430, writes 16 timeouts 0, steps req 0 done 0
Driver 2: pos 0, 320.0 steps/mm,standstill, SG min 0, mspos 2, reads 27430, writes 16 timeouts 0, steps req 0 done 0
Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0
Peak sync jitter -1/8, peak Rx sync delay 178, resyncs 0/0, no step interrupt scheduled
VIN voltage: min 24.1, current 24.2, max 24.2
V12 voltage: min 12.2, current 12.2, max 12.2
MCU temperature: min 32.5C, current 33.8C, max 33.9C
Last sensors broadcast 0x00000000 found 0 173 ticks ago, 0 ordering errs, loop time 0
CAN messages queued 1045, send timeouts 0, received 1146, lost 0, free buffers 37, min 37, error reg 0
dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0M122
=== Diagnostics ===
RepRapFirmware for Duet 3 MB6HC version 3.4.5 (2022-11-30 19:35:23) running on Duet 3 MB6HC v1.01 (standalone mode)
Board ID: 08DJM-9P63L-DJ3T8-6JKDA-3SJ6N-KB7MA
Used output buffers: 3 of 40 (18 max)
=== RTOS ===
Static ram: 152760
Dynamic ram: 97332 of which 184 recycled
Never used RAM 100396, free system stack 202 words
Tasks: NETWORK(ready,31.9%,210) ETHERNET(notifyWait,0.1%,441) HEAT(notifyWait,0.0%,322) Move(notifyWait,0.0%,351) CanReceiv(notifyWait,0.0%,799) CanSender(notifyWait,0.0%,336) CanClock(delaying,0.0%,339) TMC(notifyWait,7.9%,91) MAIN(running,60.0%,925) IDLE(ready,0.1%,30), total 100.0%
Owned mutexes:
=== Platform ===
Last reset 00:02:34 ago, cause: power up
Last software reset details not available
Error status: 0x00
Step timer max interval 126
MCU temperature: min 33.1, current 41.5, max 41.6
Supply voltage: min 23.9, current 23.9, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes
12V rail voltage: min 12.0, current 12.1, max 12.2, under voltage events: 0
Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
Events: 0 queued, 0 completed
Driver 0: standstill, SG min 0, mspos 8, reads 6751, writes 11 timeouts 0
Driver 1: standstill, SG min 0, mspos 2, reads 6748, writes 14 timeouts 0
Driver 2: standstill, SG min 0, mspos 8, reads 6751, writes 11 timeouts 0
Driver 3: standstill, SG min 0, mspos 2, reads 6748, writes 14 timeouts 0
Driver 4: standstill, SG min 0, mspos 2, reads 6748, writes 14 timeouts 0
Driver 5: standstill, SG min 0, mspos 2, reads 6749, writes 14 timeouts 0
Date/time: 2022-12-21 11:23:11
Slowest loop: 21.06ms; fastest: 0.05ms
=== Storage ===
Free file entries: 10
SD card 0 detected, interface speed: 25.0MBytes/sec
SD card longest read time 3.0ms, write time 0.0ms, max retries 0
=== Move ===
DMs created 125, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
=== MainDDARing ===
Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== AuxDDARing ===
Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== Heat ===
Bed heaters 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
Heater 1 is on, I-accum = 0.0
=== GCodes ===
Segments left: 0
Movement lock held by null
HTTP is idle in state(s) 0
Telnet is idle in state(s) 0
File is idle in state(s) 0
USB is idle in state(s) 0
Aux is idle in state(s) 0
Trigger is idle in state(s) 0
Queue is idle in state(s) 0
LCD is idle in state(s) 0
SBC is idle in state(s) 0
Daemon is idle in state(s) 0
Aux2 is idle in state(s) 0
Autopause is idle in state(s) 0
Code queue is empty
=== CAN ===
Messages queued 1401, received 1276, lost 0, boc 0
Longest wait 2ms for reply type 6024, peak Tx sync delay 6, free buffers 50 (min 49), ts 773/772/0
Tx timeouts 0,0,0,0,0,0
=== Network ===
Slowest loop: 17.69ms; fastest: 0.03ms
Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
HTTP sessions: 1 of 8
= Ethernet =
State: active
Error counts: 0 0 0 0 0 0
Socket states: 5 2 2 2 2 0 0 0
=== Multicast handler ===
Responder is inactive, messages received 0, responses 0 -
@Titus-A-Duxass fantastic. now go back to using your printer as you were before and see if you still have issues. there are a few of us (me included) that run v2.4's with RRF
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@Titus-A-Duxass so is it working now or are there still problems?
How did two drivers on the 6HC come to be faulty?
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@dc42 No it still has issues.
X and Y home as should.
Z motors along to 0X0Y and then hangs until it times out, you can here some motors running.I bought the board knowing that the two drivers are kaputt, I suspect that there are more failures on the board.
So I either have to find another board or strip it out and fit a BTT Manta M8P that I have. This is not something that I want to do as a it means replacing all the connectors.
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@Titus-A-Duxass can you try downgrading the mainboard to 3.4.4?
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@jay_s_uk Wait - my mistake! The Z is homing, it's just going extremely slow! Should be done about Tuesday.
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@Titus-A-Duxass said in Voron 2.4 3MB6 §EB config issues.:
M574 Z1 S2 ; configure Z-probe endstop for low end on Z
You should remove that line. Endstop mode S2 is used only when the Z probe is used to home axes other than Z.
Please post your homeall.g and homez.g files.
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@jay_s_uk Oops!
21.12.2022, 11:34:07 G28 Z
Error: Probe was not triggered during probing move
Error: Probe was not triggered during probing moveThis happened with the Z at about +100mm
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@dc42
; homeall.g
; called to home all axes
;
; generated by RepRapFirmware Configuration Tool v3.3.15 on Sun Dec 18 2022 17:39:32 GMT+0100 (Mitteleuropäische Normalzeit)
G91 ; relative positioning
G1 H2 Z5 F6000 ; lift Z relative to current position
G1 H1 X295 Y295 F1800 ; move quickly to X or Y endstop and stop there (first pass)
G1 H1 X295 ; home X axis
G1 H1 Y295 ; home Y axis
G1 X-5 Y-5 F6000 ; go back a few mm
G1 H1 X295 F360 ; move slowly to X axis endstop once more (second pass)
G1 H1 Y295 ; then move slowly to Y axis endstop
G90 ; absolute positioning
G1 X40 Y15 F6000 ; go to first bed probe point and home Z
G30 ; home Z by probing the bed; Uncomment the following lines to lift Z after probing
;G91 ; relative positioning
;G1 Z5 F100 ; lift Z relative to current position
;G90 ; absolute positioning; homez.g
; called to home the Z axis
;
; generated by RepRapFirmware Configuration Tool v3.3.15 on Sun Dec 18 2022 17:39:32 GMT+0100 (Mitteleuropäische Normalzeit)
G91 ; relative positioning
G1 H2 Z5 F6000 ; lift Z relative to current position
G90 ; absolute positioning
G1 X40 Y15 F6000 ; go to first probe point
G30 ; home Z by probing the bed; Uncomment the following lines to lift Z after probing
;G91 ; relative positioning
;G1 Z5 F100 ; lift Z relative to current position
;G90 ; absolute positioning -
@Titus-A-Duxass can you post your config as well just so we can see your probe settings?
btw, what probe arrangement are you using? -
Okay, I switch it off and manually lowered Z, it now homes. I think there maybe a time out issue.
; Configuration file for Duet 3 MB 6HC (firmware version 3.3)
; executed by the firmware on start-up
;
; generated by RepRapFirmware Configuration Tool v3.3.15 on Sun Dec 18 2022 17:39:32 GMT+0100 (Mitteleuropäische Normalzeit); General preferences
G90 ; send absolute coordinates...
M83 ; ...but relative extruder moves
M550 P"voron" ; set printer name
M669 K1 ; select CoreXY mode; Wait a moment for the CAN expansion boards to start
G4 S2; Network
M552 P0.0.0.0 S1 ; enable network and acquire dynamic address via DHCP
M586 P0 S1 ; enable HTTP
M586 P1 S0 ; disable FTP
M586 P2 S0 ; disable Telnet; Drives
M584 X1.1 Y1.2 Z0.1:0.5:0.3:0.4 E1.0 ; set drive mappingM569 P1.1 S0 ; A motor goes forwards
M569 P1.2 S0 ; B motor goes forwardsM569 P0.1 S1 ; FL goes forwards
M569 P0.5 S0 ; RL goes backwards
M569 P0.3 S0 ; RR goes forwards
M569 P0.4 S1 ; FR goes backwardsM569 P1.0 S0 ; Extruder goes backwards
M350 Z64 I0 ; configure microstepping without interpolation
M350 X64 Y64 E64 I1 ; configure microstepping with interpolation
M92 X320.00 Y320.00 Z400.00 E1746.16 ; set steps per mm
M566 X900.00 Y900.00 Z60.00 E120.00 ; set maximum instantaneous speed changes (mm/min)
M203 X60000.00 Y60000.00 Z18000.00 E1200.00 ; set maximum speeds (mm/min)
M201 X6000.00 Y6000.00 Z4000.00 E250.00 ; set accelerations (mm/s^2)
M906 X1500 Y1500 Z1200 E400 I30 ; set motor currents (mA) and motor idle factor in per cent
M84 S10 ; Set idle timeout; Axis Limits
M208 X0 Y0 Z0 S1 ; set axis minima
M208 X290 Y290 Z250 S0 ; set axis maxima; Endstops
M574 X2 S1 P"^io1.in" ; configure switch-type (e.g. microswitch) endstop for high end on X via pin ^io1.in
M574 Y2 S1 P"^io2.in" ; configure switch-type (e.g. microswitch) endstop for high end on Y via pin ^io2.in; Z-Probe
M558 P5 C"^io3.in" H5 F120 T6000 ; set Z probe type to switch and the dive height + speeds
G31 P500 X0 Y25 Z2.5 ; set Z probe trigger value, offset and trigger height
M557 X40:260 Y40:260 S20 ; define mesh grid; Heaters
M308 S0 P"temp0" Y"thermistor" T100000 B4092 ; configure sensor 0 as thermistor on pin temp0
M950 H0 C"out0" T0 ; create bed heater output on out0 and map it to sensor 0
M307 H0 B1 S1.00 ; enable bang-bang mode for the bed heater and set PWM limit
M140 H0 ; map heated bed to heater 0
M143 H0 S120 ; set temperature limit for heater 0 to 120C
M308 S1 P"temp1" Y"thermistor" T100000 B4725 C7.06e-8 ; configure sensor 1 as thermistor on pin temp1
M950 H1 C"out1" T1 ; create nozzle heater output on out1 and map it to sensor 1
M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
M143 H1 S280 ; set temperature limit for heater 1 to 280C; Fans
M950 F0 C"out7" Q500 ; create fan 0 on pin out7 and set its frequency
M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned off
M950 F1 C"out8" Q500 ; create fan 1 on pin out8 and set its frequency
M106 P1 S0 H1 T45 ; set fan 1 value. Thermostatic control is turned on; Tools
M563 P0 S"Revo" D0 H1 F0:1 ; define tool 0
G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C; Custom settings
M584 Z0.1:0.5:0.3:0.4; Miscellaneous
M501 ; load saved parameters from non-volatile memory
T0 ; select first tool