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    5bar scara Problem configuring z probe using fsr switch

    Scheduled Pinned Locked Moved Solved
    Duet Hardware and wiring
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    • fcwiltundefined
      fcwilt @gnmrc_
      last edited by

      @gnmrc_

      That is a fascinating machine.

      Please post your most recent config.g file and the various homing files.

      We are overlooking something simple - I think.

      Thanks.

      Frederick

      Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

      gnmrc_undefined 1 Reply Last reply Reply Quote 0
      • gnmrc_undefined
        gnmrc_ @fcwilt
        last edited by

        @fcwilt

        This is the most recent config file: config (1).g
        and this is the most recent homing file:home5barscara (2).g
        (I left commented some workarounds that I tried)

        Thanks for all the help that you are giving me,
        Gianmarco.

        fcwiltundefined 1 Reply Last reply Reply Quote 0
        • fcwiltundefined
          fcwilt @gnmrc_
          last edited by

          @gnmrc_

          Sorry it is taking so long.

          In your homing file at the end you have

          G1 X0 Y0 S2
          

          Why the S2?

          Frederick

          Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

          gnmrc_undefined 1 Reply Last reply Reply Quote 0
          • gnmrc_undefined
            gnmrc_ @fcwilt
            last edited by

            @fcwilt, do not worry about the time I’m not in a hurry.
            I use S2 because it makes me move the arm even if it’s not homed, other h commands would not make it move, I do not know why.

            Gianmarco

            fcwiltundefined 1 Reply Last reply Reply Quote 0
            • fcwiltundefined
              fcwilt @gnmrc_
              last edited by fcwilt

              @gnmrc_ said in Problem configuring z probe using fsr switch:

              @fcwilt, do not worry about the time I’m not in a hurry.
              I use S2 because it makes me move the arm even if it’s not homed, other h commands would not make it move, I do not know why.

              Gianmarco

              What version of firmware are you using?

              This is what the docs says about that for v3 firmware:

              Snnn In RRF3, this parameter is used to set laser power, when switched into Laser mode (see M452); its use for defining move type is deprecated, use 'H' parameter instead. In RRF2.02 and later, when switched into Laser mode (see M452), this parameter sets the laser power. When not switched into Laser mode, and always in firmware 2.01 and earlier, it defines the move type (see the description of the H parameter).

              Also the G1 H1 moves in the homing file, assuming they triggered the endstops, should have marked the axis as homed.

              If that is not happening something is wrong with the code or the endstops (configuration, wiring, etc).

              Frederick

              Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

              gnmrc_undefined 1 Reply Last reply Reply Quote 1
              • Phaedruxundefined
                Phaedrux Moderator
                last edited by

                Can you send M122 in the gcode console and share the results?

                Z-Bot CoreXY Build | Thingiverse Profile

                gnmrc_undefined 1 Reply Last reply Reply Quote 0
                • gnmrc_undefined
                  gnmrc_ @fcwilt
                  last edited by

                  @fcwilt
                  So I’m using RRF3.
                  I’m going to re-test it but when I use the S2 command it gives me a warning message saying obsolete command, but still moves as the old s2 command so ignoring homing not completed.

                  Gianmarco

                  fcwiltundefined 1 Reply Last reply Reply Quote 0
                  • fcwiltundefined
                    fcwilt @gnmrc_
                    last edited by

                    @gnmrc_ said in Problem configuring z probe using fsr switch:

                    @fcwilt
                    So I’m using RRF3.
                    I’m going to re-test it but when I use the S2 command it gives me a warning message saying obsolete command, but still moves as the old s2 command so ignoring homing not completed.

                    Gianmarco

                    Good to know. Often commands and command options, like S2, are deprecated but not yet gone.

                    But it still leaves the question of why the two H1 moves aren't marking the axes as homed.

                    I notice that you specify the movement distance as X200 and Y200.

                    Be aware that if the endstop swtiches are not activated by the time the distance has been moved the axis is not marked as homed.

                    Is 200 long enough to insure the endstop switches are reached?

                    Thanks.

                    Frederick

                    Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

                    gnmrc_undefined 1 Reply Last reply Reply Quote 0
                    • gnmrc_undefined
                      gnmrc_ @fcwilt
                      last edited by

                      @fcwilt Yes endstop are reached with no problems from any arm position.
                      Maybe the movement does not work because it needs to home every axis not only x and y for some reason, this would explain the problem with the movement and why the arm works correctly after a partial homing routine(homing only the arm) and then using g92 to home z and after that everything works as expected.

                      Let me know what you think.

                      Thanks,
                      Gianmarco

                      fcwiltundefined 1 Reply Last reply Reply Quote 0
                      • fcwiltundefined
                        fcwilt @gnmrc_
                        last edited by

                        @gnmrc_

                        Here are the last three lines from the most recent homing code:

                        G90
                        G1 X0 Y0 F300 S2 ;move hotend to the center
                        G30

                        As I recall you said the S2 (which should be H2 according to the docs) is needed.

                        But if the previous two G1 H1 commands worked the X and Y axis should be homed and the S2 (H2) should not be needed.

                        Now the G30 is the probing command and it is not going to work since it needs the Z axis to be homed.

                        And there is nothing in your homing file that tries to home the Z axis.

                        To help clarify something try this, please:

                        • remove the S2 from the last G1 command
                        • remove the G30 command
                        • test homing now

                        Yes, I know that Z axis will not be homed but I am not worried about that.

                        What worries me is the need for the S2.

                        Thanks.

                        Frederick

                        Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

                        gnmrc_undefined 1 Reply Last reply Reply Quote 0
                        • gnmrc_undefined
                          gnmrc_ @fcwilt
                          last edited by

                          @fcwilt I’ve done as you said, this is the error I get:
                          G0/G1: insufficient axes homed

                          fcwiltundefined 1 Reply Last reply Reply Quote 0
                          • gnmrc_undefined
                            gnmrc_ @Phaedrux
                            last edited by

                            @Phaedrux this is what I get from m122:

                            m122
                            === Diagnostics ===
                            RepRapFirmware for Duet 2 WiFi/Ethernet version 3.4.5 (2022-11-30 19:36:12) running on Duet WiFi 1.02 or later
                            Board ID: 0JD0M-9P6M2-NWNS0-7JKDD-3SN6S-1U0BJ
                            Used output buffers: 1 of 26 (11 max)
                            === RTOS ===
                            Static ram: 23836
                            Dynamic ram: 74172 of which 68 recycled
                            Never used RAM 14004, free system stack 184 words
                            Tasks: NETWORK(ready,13.4%,242) HEAT(notifyWait,0.0%,333) Move(notifyWait,0.0%,363) MAIN(running,84.1%,446) IDLE(ready,2.5%,30), total 100.0%
                            Owned mutexes:
                            === Platform ===
                            Last reset 00:00:37 ago, cause: power up
                            Last software reset at 2023-10-19 21:58, reason: User, GCodes spinning, available RAM 13692, slot 2
                            Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
                            Error status: 0x00
                            Step timer max interval 0
                            MCU temperature: min 29.8, current 33.2, max 33.4
                            Supply voltage: min 12.5, current 12.5, max 12.6, under voltage events: 0, over voltage events: 0, power good: yes
                            Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                            Events: 0 queued, 0 completed
                            Driver 0: standstill, SG min n/a
                            Driver 1: standstill, SG min n/a
                            Driver 2: standstill, SG min n/a
                            Driver 3: standstill, SG min n/a
                            Driver 4: standstill, SG min n/a
                            Driver 5:
                            Driver 6:
                            Driver 7:
                            Driver 8:
                            Driver 9:
                            Driver 10:
                            Driver 11:
                            Date/time: 2023-10-24 17:39:02
                            Cache data hit count 1374063136
                            Slowest loop: 6.81ms; fastest: 0.18ms
                            I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
                            === Storage ===
                            Free file entries: 10
                            SD card 0 detected, interface speed: 20.0MBytes/sec
                            SD card longest read time 2.4ms, write time 0.0ms, max retries 0
                            === Move ===
                            DMs created 83, segments created 0, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                            === MainDDARing ===
                            Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                            === AuxDDARing ===
                            Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                            === Heat ===
                            Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
                            === GCodes ===
                            Segments left: 0
                            Movement lock held by null
                            HTTP is idle in state(s) 0
                            Telnet is idle in state(s) 0
                            File is idle in state(s) 0
                            USB is idle in state(s) 0
                            Aux is idle in state(s) 0
                            Trigger is idle in state(s) 0
                            Queue is idle in state(s) 0
                            LCD is idle in state(s) 0
                            Daemon is idle in state(s) 0
                            Autopause is idle in state(s) 0
                            Code queue is empty
                            === Network ===
                            Slowest loop: 15.77ms; fastest: 0.00ms
                            Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
                            HTTP sessions: 1 of 8
                            = WiFi =
                            Network state is active
                            WiFi module is connected to access point
                            Failed messages: pending 0, notready 0, noresp 0
                            WiFi firmware version 1.23
                            WiFi MAC address 98💿ac:20:cb:ca
                            WiFi Vcc 3.37, reset reason Turned on by main processor
                            WiFi flash size 4194304, free heap 25824
                            WiFi IP address 192.168.178.109
                            WiFi signal strength -54dBm, mode none, reconnections 0, sleep mode modem
                            Clock register ffffffff
                            Socket states: 0 0 0 0 0 0 0 0

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                            • fcwiltundefined
                              fcwilt @gnmrc_
                              last edited by

                              @gnmrc_ said in Problem configuring z probe using fsr switch:

                              @fcwilt I’ve done as you said, this is the error I get:
                              G0/G1: insufficient axes homed

                              I should have asked - exactly what are you/it doing when this message appears - during the homing file execution?

                              Thanks.

                              Frederick

                              Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

                              gnmrc_undefined 1 Reply Last reply Reply Quote 0
                              • gnmrc_undefined
                                gnmrc_ @fcwilt
                                last edited by gnmrc_

                                @fcwilt It’does nothing the arm stays in his homed position

                                Gianmarco

                                fcwiltundefined 1 Reply Last reply Reply Quote 0
                                • fcwiltundefined
                                  fcwilt @gnmrc_
                                  last edited by

                                  @gnmrc_ said in Problem configuring z probe using fsr switch:

                                  @fcwilt It’does nothing it stops the movement.

                                  When does that happen?

                                  When trying to execute the homing file?

                                  After that?

                                  Frederick

                                  Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

                                  gnmrc_undefined 1 Reply Last reply Reply Quote 0
                                  • Phaedruxundefined
                                    Phaedrux Moderator
                                    last edited by

                                    I assume you're working from this?

                                    https://docs.duet3d.com/en/User_manual/Machine_configuration/Configuration_five_bar_parallel_scara

                                    Z-Bot CoreXY Build | Thingiverse Profile

                                    gnmrc_undefined 1 Reply Last reply Reply Quote 1
                                    • gnmrc_undefined
                                      gnmrc_ @fcwilt
                                      last edited by

                                      @fcwilt, no the arm homes itself, then when it should do the x0 y0 move it stops

                                      fcwiltundefined 1 Reply Last reply Reply Quote 0
                                      • gnmrc_undefined
                                        gnmrc_ @Phaedrux
                                        last edited by

                                        @Phaedrux yes, I’m using that and I used some other forum post from 2019 I think.

                                        1 Reply Last reply Reply Quote 0
                                        • fcwiltundefined
                                          fcwilt @gnmrc_
                                          last edited by

                                          @gnmrc_ said in Problem configuring z probe using fsr switch:

                                          Try to be more precise - I am not there seeing what you are seeing - need to help fill in the gaps of my knowledge. Thanks.

                                          no the arm homes itself, then when it should do the x0 y0 move it stops

                                          Are you referring to the move to X=0 Y=0 at the end of the homing file?

                                          That is when you get the error message about un-homed axes?

                                          Correct?

                                          IF that is what is happening then the G1 H1 moves are NOT homing the axes. If they were being homed the move to X=0 Y=0 would work.

                                          When a homing move fails, that is it reaches the end of the specified travel (in your case 200) without activating the endstop switch, there is no error message - it just stops moving and the axis is still not homed.

                                          So remove the move to X=0 Y=0 (if it is still there), re-boot the machine and click on the HomeAll button in the DWC Dashboard.

                                          Once the movement in both axes stops. check if the X and Y home buttons have changed to indicate they are homed.

                                          Thanks.

                                          Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

                                          gnmrc_undefined 1 Reply Last reply Reply Quote 0
                                          • gnmrc_undefined
                                            gnmrc_ @fcwilt
                                            last edited by

                                            @fcwilt yes exactly, the machine stops before the x=0 y=0 move in the homing file, but I see from the board’s leds that my endstop gets triggered,I even tested with m119 ,and the arms stops when touching their relative endstops so I do not think this is the case.
                                            Also if I only do the G1 H1 X and G1 H1 Y moves in the homing file when it ends my x and y axis results as homed.

                                            Gianmarco

                                            fcwiltundefined 1 Reply Last reply Reply Quote 0
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