Awesome, Thank you!

Latest posts made by Mylespol
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Duet3D Filament Monitor Rotating Magnet Version STLs?
Hey, just curious are there STLs CAD or a drawing anywhere for the newest revision of the magnet filament sensor housing (the one with the SLA printed housing) I found the dev one thats linked on YouMagine but couldn't find the current design.
Thanks!
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RE: Maestro Steppers not working
I can't say that I see any, would pictures of the board be helpful?
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RE: Maestro Steppers not working
@nhof
Sadly no change, still free spinning@dc42
From switching to 2.02 the M122 command returnsM122
=== Diagnostics ===
RepRapFirmware for Duet 2 Maestro version 2.02(RTOS) running on Duet Maestro 1.0
Board ID: 08DGM-95762-FD3TD-6JKD4-3S86N-1T8VD
Used output buffers: 1 of 20 (9 max)
=== RTOS ===
Static ram: 19476
Dynamic ram: 92848 of which 0 recycled
Exception stack ram used: 200
Never used ram: 18548
Tasks: NETWORK(ready,672) HEAT(blocked,1260) MAIN(running,3940) IDLE(ready,204)
Owned mutexes:
=== Platform ===
Last reset 00:00:25 ago, cause: software
Last software reset at 2019-04-18 21:14, reason: User, spinning module GCodes, available RAM 23916 bytes (slot 2)
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x04432000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
Error status: 0
Free file entries: 10
SD card 0 detected, interface speed: 15.0MBytes/sec
SD card longest block write time: 0.0ms, max retries 0
MCU temperature: min 44.4, current 44.7, max 45.0
Supply voltage: min 0.0, current 12.1, max 12.1, under voltage events: 0, over voltage events: 0, power good: yes
Driver 0: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 442
Driver 1: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 442
Driver 2: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 441
Driver 3: standstill, read errors 0, write errors 1, ifcount 13, reads 434, timeouts 0
Driver 4: standstill, read errors 0, write errors 1, ifcount 13, reads 434, timeouts 0
Driver 5: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 441
Driver 6: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 441
Date/time: 2019-04-19 12:46:54
Slowest loop: 2.99ms; fastest: 0.06ms
I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0
=== Move ===
Hiccups: 0, StepErrors: 0, LaErrors: 0, FreeDm: 240, MinFreeDm: 240, MaxWait: 0ms, Underruns: 0, 0
Scheduled moves: 0, completed moves: 0
Bed compensation in use: none
Bed probe heights: 0.000 0.000 0.000 0.000 0.000
=== Heat ===
Bed heaters = 0, chamberHeaters = -1 -1
=== GCodes ===
Segments left: 0
Stack records: 1 allocated, 0 in use
Movement lock held by null
http is idle in state(s) 0
telnet is idle in state(s) 0
file is idle in state(s) 0
serial is idle in state(s) 0
aux is idle in state(s) 0
daemon is idle in state(s) 0
queue is idle in state(s) 0
lcd is idle in state(s) 0
autopause is idle in state(s) 0
Code queue is empty.
=== Network ===
Slowest loop: 5.24ms; fastest: 0.03ms
Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
HTTP sessions: 1 of 8
Interface state 5, link 100Mbps full duplexSo sadly I'm guessing something managed to kill drivers 0-2?
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Maestro Steppers not working
Hey, first I'll mention this is my first post so I'm sorry if I miss anything.
So I was in the process of converting a CR-10 to use a Duet Maestro + BLtouch and thermocouple. I had everything working and decided I should update the firmware (from I believe an early version of 2.0) to the latest. After the update, I couldn't get any of the motors to power. When homing or anything I could still freely move the motors with my hand. I have checked all my connectors to no avail. In addition, all the lights are on when the board is receiving power. I've tried M122 M906 and see nothing abnormal (ill add those below with config). I've also tried different firmware configs without all the other additions to see if they were causing it. Lastly, I see no visible damage to the board.
Note: one oddity is that when I switched a motor and map it to E1 the motor receives enough power to resist being turned by hand.
Results of M122:
M122
=== Diagnostics ===
RepRapFirmware for Duet 2 Maestro version 2.03beta3 running on Duet Maestro 1.0
Board ID: 08DGM-95762-FD3TD-6JKD4-3S86N-1T8VD
Used output buffers: 3 of 20 (17 max)
=== RTOS ===
Static ram: 19592
Dynamic ram: 87292 of which 0 recycled
Exception stack ram used: 208
Never used ram: 23980
Tasks: NETWORK(ready,660) HEAT(blocked,1232) MAIN(running,3920) IDLE(ready,204)
Owned mutexes:
=== Platform ===
Last reset 00:01:15 ago, cause: software
Last software reset at 2019-04-18 21:14, reason: User, spinning module GCodes, available RAM 23916 bytes (slot 2)
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x04432000 BFAR 0xe000ed38 SP 0xffffffff Task 0x4e49414d
Error status: 0
Free file entries: 10
SD card 0 detected, interface speed: 15.0MBytes/sec
SD card longest block write time: 0.0ms, max retries 0
MCU temperature: min 46.7, current 47.4, max 47.5
Supply voltage: min 12.1, current 12.1, max 12.1, under voltage events: 0, over voltage events: 0, power good: yes
Driver 0: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 1126
Driver 1: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 1126
Driver 2: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 1127
Driver 3: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 1127
Driver 4: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 1127
Driver 5: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 1126
Driver 6: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 1126
Date/time: 2019-04-18 21:15:34
Slowest loop: 2.30ms; fastest: 0.07ms
I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0
=== Move ===
Hiccups: 0, FreeDm: 169, MinFreeDm: 169, MaxWait: 0ms
Bed compensation in use: none
Bed probe heights: 0.000 0.000 0.000 0.000 0.000
=== MainDDARing ===
Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0
=== AuxDDARing ===
Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0
=== Heat ===
Bed heaters = 0, chamberHeaters = -1 -1
=== GCodes ===
Segments left: 0, aux move: no
Stack records: 1 allocated, 0 in use
Movement lock held by null
http is idle in state(s) 0
telnet is idle in state(s) 0
file is idle in state(s) 0
serial is idle in state(s) 0
aux is idle in state(s) 0
daemon is idle in state(s) 0
queue is idle in state(s) 0
lcd is idle in state(s) 0
autopause is idle in state(s) 0
Code queue is empty.
=== Network ===
Slowest loop: 9.60ms; fastest: 0.03ms
Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0) Telnet(0)
HTTP sessions: 1 of 8
Interface state 5, link 100Mbps full duplexM906 results:
Motor current (mA) - X:1000, Y:1000, Z:1000, E:1000:1000:1000:1000, idle factor 30%Config.g:
; Configuration file for Duet Maestro (firmware version 1.21)
; executed by the firmware on start-up
;
; generated by RepRapFirmware Configuration Tool v2 on Sat Apr 06 2019 22:11:37 GMT-0400 (Eastern Daylight Time); General preferences
G90 ; Send absolute coordinates...
M83 ; ...but relative extruder moves; Network
M550 P"My Printer" ; Set machine name
M552 P0.0.0.0 S1 ; Enable network and acquire dynamic address via DHCP
M586 P0 S1 ; Enable HTTP
M586 P1 S0 ; Disable FTP
M586 P2 S0 ; Disable Telnet; Drives
M569 P0 S1 ; Drive 0 goes forwards
M569 P1 S1 ; Drive 1 goes forwards
M569 P2 S1 ; Drive 2 goes forwards
M569 P3 S1 ; Drive 3 goes forwards
M350 X16 Y16 Z16 E16 I1 ; Configure microstepping with interpolation
M92 X80.00 Y80.00 Z4000.00 E420.00 ; Set steps per mm
M566 X900.00 Y900.00 Z12.00 E120.00 ; Set maximum instantaneous speed changes (mm/min)
M203 X6000.00 Y6000.00 Z180.00 E1200.00 ; Set maximum speeds (mm/min)
M201 X500.00 Y500.00 Z20.00 E250.00 ; Set accelerations (mm/s^2)
M906 X1000 Y1000 Z1000 E1000 I30 ; Set motor currents (mA) and motor idle factor in per cent
M84 S30 ; Set idle timeout; Axis Limits
M208 X0 Y0 Z0 S1 ; Set axis minima
M208 X300 Y300 Z400 S0 ; Set axis maxima; Endstops
M574 Z1 S0 ; Set active low and disabled endstops
M574 X1 Y1 S1 ; Set active high endstops; Z-Probe
M558 P64 H5 F100 T2000 ; Set Z probe type to bltouch and the dive height + speeds
G31 X0 Y30 Z0 P25 ; Set Z probe trigger value, offset and trigger height
;M557 X15:300 Y35:300 S20 ; Define mesh grid; Heaters
M305 P0 T100000 B4138 R2200 ; Set thermistor + ADC parameters for heater 0
M143 H0 S120 ; Set temperature limit for heater 0 to 120C
M305 P1 X150 T"K" ; Configure thermocouple for heater 1
M143 H1 S300 ; Set temperature limit for heater 1 to 300C; Fans
M106 P0 S0.3 I0 F500 H T45 ; Set fan 0 value, PWM signal inversion and frequency. Thermostatic control is turned on
M106 P1 S1 I0 F500 H1 T45 ; Set fan 1 value, PWM signal inversion and frequency. Thermostatic control is turned on; Tools
M563 P0 D0 H1 ; Define tool 0
G10 P0 X0 Y0 Z0 ; Set tool 0 axis offsets
G10 P0 R0 S0 ; Set initial tool 0 active and standby temperatures to 0C; Automatic saving after power loss is not enabled
; Custom settings are not configured
Thanks!