@Phaedrux Motors are cold to the touch
Motors model number is:
JK42HS40-1704-13A
@Phaedrux Motors are cold to the touch
Motors model number is:
JK42HS40-1704-13A
@Bewaren M98
P"config.g"
HTTP is enabled on port 80
FTP is disabled
TELNET is disabled
@Phaedrux said in Duet2 Firmware Upgrade Issue:
M122
M122
=== Diagnostics ===
RepRapFirmware for Duet 2 WiFi/Ethernet version 3.5.1 (2024-04-19 14:40:46) running on Duet Ethernet 1.02 or later
Board ID: 08DGM-917DA-G4MSD-6JKDA-3SN6Q-TST39
Used output buffers: 1 of 26 (14 max)
=== RTOS ===
Static ram: 23256
Dynamic ram: 67932 of which 0 recycled
Never used RAM 21956, free system stack 184 words
Tasks: NETWORK(1,ready,27.9%,220) HEAT(3,nWait 5,0.0%,330) Move(4,nWait 5,0.0%,359) MAIN(1,running,72.0%,761) IDLE(0,ready,0.1%,29), total 100.0%
Owned mutexes:
=== Platform ===
Last reset 00:27:25 ago, cause: software
Last software reset at 2024-04-19 22:48, reason: User, Gcodes spinning, available RAM 21812, slot 0
Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0041f000 BFAR 0xe000ed38 SP 0x00000000 Task MAIN Freestk 0 n/a
Error status: 0x00
Aux0 errors 0,0,0
MCU temperature: min 35.4, current 36.7, max 37.3
Supply voltage: min 24.2, current 24.3, max 24.3, under voltage events: 0, over voltage events: 0, power good: yes
Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
Events: 0 queued, 0 completed
Driver 0: standstill, SG min n/a
Driver 1: standstill, SG min n/a
Driver 2: standstill, SG min n/a
Driver 3: standstill, SG min n/a
Driver 4: standstill, SG min n/a
Driver 5:
Driver 6:
Driver 7:
Driver 8:
Driver 9:
Driver 10:
Driver 11:
Date/time: 2024-04-19 23:15:40
Cache data hit count 4294967295
Slowest loop: 15.20ms; fastest: 0.18ms
I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
=== Storage ===
Free file entries: 10
SD card 0 detected, interface speed: 20.0MBytes/sec
SD card longest read time 13.0ms, write time 0.0ms, max retries 0
=== Move ===
DMs created 83, segments created 0, maxWait 0ms, bed compensation in use: none, height map offset 0.000, max steps late 0, min interval 0, bad calcs 0, ebfmin 0.00, ebfmax 0.00
no step interrupt scheduled
Moves shaped first try 0, on retry 0, too short 0, wrong shape 0, maybepossible 0
=== DDARing 0 ===
Scheduled moves 0, completed 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
=== Heat ===
Bed heaters 0 -1 -1 -1, chamber heaters -1 -1 -1 -1, ordering errs 0
=== GCodes ===
Movement locks held by null
HTTP is idle in state(s) 0
Telnet is idle in state(s) 0
File is idle in state(s) 0
USB is idle in state(s) 0
Aux is idle in state(s) 0
Trigger is idle in state(s) 0
Queue is idle in state(s) 0
LCD is idle in state(s) 0
Daemon is idle in state(s) 0
Autopause is idle in state(s) 0
Q0 segments left 0
Code queue 0 is empty
=== Network ===
Slowest loop: 6.92ms; fastest: 0.01ms
Responder states: HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0)
HTTP sessions: 1 of 8
Interface state active, link 100Mbps full duplex
Socket states: 5 2 2 2 2 2
M98 "config.g"
Error: M98: No P or R parameter
Nema 17 Specs:
Motor Type: Bipolar Stepper.
Step Angle: 1.8°
Holding Torque: 26Ncm(36.8oz.in)
Rated Current/phase: 0.4A.
Phase Resistance: 30ohms.
Inductance: 37mH+/-20%(1KHz)
Config.g:
config (1).g
@Phaedrux Alright I've checked all the wiring is correct and I've updated the firmware. Both motors are moving the correct direction now but when the axis are homing I'm now getting a issue with Driver 2
'Warning: Driver 2 warning: phase A may be disconnected, phase B may be disconnected'
There's nothing grounding on the board and I can't figure out what else it could be, the motors maybe?
@Phaedrux How do I go about updating the DWC Files?
Evening all
I've recently gotten back into 3D Printing and decided to build a new printer out of parts laying around. I have a Duet2 that I'm planning on using for the control board, however when I've tried to upgrade it to the latest firmware I'm getting this error:
M997: Firmware binary "0:/firmware/Duet2CombinedFirmware.bin" is not valid for this electronics
This is the board and firmware I'm running. When I try to install my RepRap firmware onto it it's displaying the above error message.
The main reason I'm trying to update it is because I'm getting this error message when trying to move the motors (One will move at a time, but both can't at the same time) (CoreXY Build)
Any support would be great!
@infiniteloop I'll try that shortly and let you know how it goes!
@infiniteloop Yeah I've checked them and can't seem to see any issue, however now that the print head is slight away from the base plate I am not getting any fluctuations in the temperature, could it be due to interference from the base plate or possibly grounding?
@droftarts I've started another print and it fluctuated a lot to start with while doing the outer perimeters of the print, however now it has stabilised while doing the internals of the base layer I'm rather confused now
(From 13:58 onwards is the start of print 2
@droftarts I've checked over all my wiring, replaced the thermistor and made some adjustments and I am now getting this I'm starting to think it may be a faulty smart effector or control board