But if the probe always meets the same bed temperature - the variance is constant right?
Thermistor is there to correct the non-constant bed temperatures to keep the same offset between 60 and 90C but I'm using only one

Latest posts made by rudenick
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RE: G32 Dual Z axis constant 0.6mm off-level difference
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RE: G32 Dual Z axis constant 0.6mm off-level difference
@dc42 Hope it is a worthwhile bother. I'm at the wits end with configuring duet for my ender 3 and pinda probe since May.
The Z offset is inconsistent and two Z axis true leveling is inconsistent as well.
- I have replaced the springs with PCABS washers.
- Probe measures at static 60C
- Z rod distances, bed size, probe to nozzle distances are correct.
- Z motor order and cabling is correct.
Please, please help
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RE: G32 Dual Z axis constant 0.6mm off-level difference
Duet software turns out to be very difficult to be made to work despite doing everything like the guides said.
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RE: G32 Dual Z axis constant 0.6mm off-level difference
Yes but as I use 60C always - It's safe dependable value. Using temperature offsets would just add another fail point and would not impact anything that is failing currently
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RE: G32 Dual Z axis constant 0.6mm off-level difference
@Phaedrux I printed a 2cm washers in PCABS and replaced the springs with them. Magnetic bed holds to the bed.
At first it worked but I started to have hardware/connection issues with temperature sensor in pinda probe. I never used temp corretion, I thought it is not available.
I always use 60C temp for homing and printing unless I use PCABS but that's not in the equation/files right now.
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RE: G32 Dual Z axis constant 0.6mm off-level difference
If at least I could home onice:
25/09/2020, 07:54:49 G28 Leadscrew adjustments made: 0.052 -0.048, points used 2, (mean, deviation) before (0.005, 0.029) after (0.000, 0.000) Stopped at height 0.590 mm Stopped at height 0.540 mm Error: Homing failed 25/09/2020, 07:47:56 G28 Leadscrew adjustments made: 0.096 -0.089, points used 2, (mean, deviation) before (0.010, 0.054) after (0.000, 0.000) Stopped at height 0.595 mm Stopped at height 0.515 mm Error: Homing failed 25/09/2020, 07:45:14 G28 Leadscrew adjustments made: 0.164 -0.158, points used 2, (mean, deviation) before (0.014, 0.094) after (0.000, 0.000) Stopped at height 0.647 mm Stopped at height 0.505 mm Error: Homing failed 25/09/2020, 07:42:46 G28 Leadscrew adjustments made: 0.379 -0.333, points used 2, (mean, deviation) before (0.048, 0.209) after (0.000, 0.000) Stopped at height 0.908 mm Stopped at height 0.675 mm
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RE: G32 Dual Z axis constant 0.6mm off-level difference
I also have a trouble with changing Z offset, one week it's 2mm lower and after few prints it goes 2mm up while I'm consistent with the procedure and it is persistent on restarts.
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RE: G32 Dual Z axis constant 0.6mm off-level difference
Full config.g
; General preferences G90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"Ender1" ; set printer name ; Network ;M552 S0 ; disable network ; Drives M569 P0 S0 D3 ;T0.1:0.1:0.02:0.02 ; physical drive 0 goes backwards using TMC220x driver timings M569 P1 S0 D3 ;T0.1:0.1:0.02:0.02 ; physical drive 1 goes backwards using TMC220x driver timings M569 P2 S1 D3 ;T0.1:0.1:0.02:0.02 ; physical drive 2 goes forwards using TMC220x driver timings M569 P3 S0 ;T0.1:0.1:0.02:0.02 ; physical drive 3 goes backwards using TMC220x driver timings M569 P4 S1 D3 ;T0.1:0.1:0.02:0.02 ; physical drive 3 goes backwards using TMC220x driver timings ;M569 P0 S0 ; physical drive 0 goes forwards using default driver timings ;M569 P1 S0 ; physical drive 1 goes forwards using default driver timings ;M569 P2 S1 ; physical drive 2 goes forwards using default driver timings ;M569 P3 S0 ; physical drive 3 goes forwards using default driver timings M584 X0 Y1 Z2:4 E3 ; set drive mapping M350 X16 Y16 Z16 E32 I1 ; configure microstepping with interpolation M92 X80.00 Y80.00 Z400 E194.68 ; set steps per mm 210.00 without m350 M566 X1200.00 Y1200.00 Z24.00 E300.00 ; set maximum instantaneous speed changes (mm/min) M203 X9000.00 Y9000.00 Z180.00 E6000.00 ; set maximum speeds (mm/min) M201 X500.00 Y500.00 Z100.00 E5000.00 ; set accelerations (mm/s^2) M906 X800 Y800 Z800 E1000 I30 ; set motor currents (mA) M572 D0 S0.42 ; set pressure advance for direct drive M84 S30 ; Set idle timeout ;dual z axis limits ;TO BE CORRECTED M671 X-30:260 Y115:115 S1 ; leadscrews at left (connected to Z) and right (connected to E1) of X axis ;M208 X45:195 Y30:185 ; X carriage moves from -5 to 205, Y bed goes from 0 to 200 ; Axis Limits M208 X0 Y0 Z0 S1 ; set axis minima M208 X252 Y230 Z230 S0 ; set axis maxima ; Endstops M574 X1 S1 P"xstop" ; configure active-high endstop for low end on X via pin xstop M574 Y1 S1 P"ystop" ; configure active-high endstop for low end on Y via pin ystop M574 Z1 S1 P"zstop" ; configure active-high endstop for low end on Z via pin zstop ; Z-Probe PINDA M558 P5 C"probe" H3 F120 T6000 A20 S0.005 ; PINDA ;M308 S2 P"e1temp" A"PINDA" Y"thermistor" T100000 B3950 ; PINDA TEMP OK G31 P100 X-35 Y-4 ;Z0.540 M557 Y20:220 X19:215 P9 ; define mesh grid OK ; Heaters M140 H0 ; remap heated bed to heater 0 M308 S0 P"bedtemp" Y"thermistor" T100000 B4092 ; configure sensor 0 as thermistor on pin bedtemp M950 H0 C"bed" T0 ; create bed heater output on bed and map it toensor 0 M143 H0 S110 ; set temperature limit for heater 0 to 150C M307 H0 A149.8 C505.7 D0.3 S1.0 V0.0 B0 ; disable bang-bang mode for the nozzle heater and set PWM limit, update auto bed tuning M303 H0 S90 M308 S1 P"e0temp" Y"thermistor" T100000 B4092 ; configure sensor 1 as thermistor on pin e0temp M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1 M143 H1 S265 ; set temperature limit for heater 1 to 275C M307 H1 A348.1 C142.2 D5.1 S1.0 V0.0 B0 ; disable bang-bang mode for the nozzle heater and set PWM limit, update auto bed tuning M303 H1 S260 ; Fans M950 F0 C"fan0" Q500 ; create fan 0 on pin fan0 and set its frequency M106 P0 S0 H-1 ; set fan 0 value. Thermostatic control is turned off M950 F1 C"e1heat" Q500 ; create fan 1 on pin e1heat and set its frequency M106 P1 H1 T40 S255 ; set fan 1 value. Speed is set to 255. Thermostatic control is off ; Tools M563 P0 D0 H1 F0 ; define tool 0 ;G10 P0 X0 Y-13 Z-0.80 ; set tool 0 axis offsets G10 P0 X0 Y-13 Z0 ; set tool 0 axis offsets G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C ; Custom settings are not defined ; Miscellaneous T0 ; select first tool
full homeall.g
G91 ; relative positioning G1 H2 Z5 F6000 ; lift Z relative to current position M190 S60 ; set temp to 60 G1 H1 X-240 Y-240 F3000 ; move quickly to X and Y axis endstops and stop there (first pass) G1 H2 X5 Y5 F6000 ; go back a few mm G1 H1 X-240 Y-240 F240 ; move slowly to X and Y axis endstops once more (second pass) G1 H2 Z5 F6000 ; lift Z relative to current position G1 X160 Y115 F3000 ; put head over the centre of the bed, or wherever you want to probe G30 F240 ; lower head, stop when probe triggered and set Z to trigger height G90 ; back to absolute mode G1 H2 X0 Y0 Z20 F6000 ; Go to home position G32 G31 Z0.498 ;Z0.540 ;G29 S1 G28 Z
full bed.g
G30 P0 X20 Y115 Z-99999 ; probe near a leadscrew, half way along Y axis G30 P1 X190 Y115 Z-99999 S2 ; probe near a leadscrew and calibrate 2 motors G28 Z G90 ; absolute mode G1 Z5 G1 X40 Y115 F6000 ; put head over the mid left corner G1 Z0 G91 ; relative mode G1 H2 Z5 F6000 ; raise head 4mm to ensure it is above the Z probe trigger height G90 ; back to absolute mode G30 S-1; lower head, stop when probe triggered and report the value G90 ; absolute mode G1 Z5 M564 S0 G1 X250 Y115 F6000 ; put head over the mid right corner M564 S1 G91 ; relative mode G1 H2 Z5 F6000 ; raise head 4mm to ensure it is above the Z probe trigger height G90 ; back to absolute mode G30 S-1; lower head, stop when probe triggered and report the value
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RE: G32 Dual Z axis constant 0.6mm off-level difference
@Phaedrux said in G32 Dual Z axis constant 0.6mm off-level difference:
You should set the trigger height in config.g and leave it there. You haven't posted your config so I don't know what your trigger height is set there, but if it's different than 0.540 then you're going to have some problems.
I started getting fine leveling results precisely because I moved it from config.g so G32 works without it. How do I get better measurements with Z offset in there? (they were scattered and inconsistent. I got the motors in the right order.
At least now they get more even but still I need to home it few times
25/09/2020, 07:54:49 G28 Leadscrew adjustments made: 0.052 -0.048, points used 2, (mean, deviation) before (0.005, 0.029) after (0.000, 0.000) Stopped at height 0.590 mm Stopped at height 0.540 mm Error: Homing failed 25/09/2020, 07:47:56 G28 Leadscrew adjustments made: 0.096 -0.089, points used 2, (mean, deviation) before (0.010, 0.054) after (0.000, 0.000) Stopped at height 0.595 mm Stopped at height 0.515 mm Error: Homing failed 25/09/2020, 07:45:14 G28 Leadscrew adjustments made: 0.164 -0.158, points used 2, (mean, deviation) before (0.014, 0.094) after (0.000, 0.000) Stopped at height 0.647 mm Stopped at height 0.505 mm Error: Homing failed
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RE: G32 Dual Z axis constant 0.6mm off-level difference
After I push emergency stop and run homeall.g
G91 ; relative positioning G1 H2 Z5 F6000 ; lift Z relative to current position M190 S60 ; set temp to 60 G1 H1 X-240 Y-240 F3000 ; move quickly to X and Y axis endstops and stop there (first pass) G1 H2 X5 Y5 F6000 ; go back a few mm G1 H1 X-240 Y-240 F240 ; move slowly to X and Y axis endstops once more (second pass) G1 H2 Z5 F6000 ; lift Z relative to current position G1 X160 Y115 F3000 ; put head over the centre of the bed, or wherever you want to probe G30 F240 ; lower head, stop when probe triggered and set Z to trigger height G90 ; back to absolute mode G1 H2 X0 Y0 Z20 F6000 ; Go to home position G32 G31 Z0.540 G29 S1 G28 Z
I get fine results:
G28 Stopped at height 0.815 mm Stopped at height 0.690 mm Leadscrew adjustments made: 0.139 -0.349, points used 2, (mean, deviation) before (-0.088, 0.143) after (-0.000, 0.000) Stopped at height 0.730 mm Stopped at height 0.770 mm
But it is ridiculous. Limiting use.