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    Z-Axis not homing

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    • Phaedruxundefined
      Phaedrux Moderator
      last edited by

      Swap the plug to the ZA port and put the jumpers on the ZB port and try again.

      Z-Bot CoreXY Build | Thingiverse Profile

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      • rickypilnikundefined
        rickypilnik
        last edited by

        Same as before. Z - Axis still not moving.

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        • Phaedruxundefined
          Phaedrux Moderator
          last edited by Phaedrux

          And just to eliminate the homing files, If you send M564 S0 H0 to allow unhomed axis movement are you able to get the z motor to move by using the jogging buttons?

          And does it still produce the short to ground error message?

          Z-Bot CoreXY Build | Thingiverse Profile

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          • Phaedruxundefined
            Phaedrux Moderator
            last edited by

            Can you also send M122 in the console and post the response?

            Z-Bot CoreXY Build | Thingiverse Profile

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            • rickypilnikundefined
              rickypilnik
              last edited by

              No I can't move the Z-axis, but x and y are fine even with the message of short to drivers from before.

              m122
              === Diagnostics ===
              RepRapFirmware for Duet 2 Maestro version 3.1.1 running on Duet Maestro 1.0
              Board ID: 08DJM-9X66L-LG3SN-6JKDL-3S06Q-K8X6P
              Used output buffers: 3 of 24 (10 max)
              === RTOS ===
              Static ram: 21924
              Dynamic ram: 92804 of which 52 recycled
              Exception stack ram used: 392
              Never used ram: 15900
              Tasks: NETWORK(ready,472) HEAT(blocked,1324) MAIN(running,1996) IDLE(ready,84)
              Owned mutexes:
              === Platform ===
              Last reset 00:01:06 ago, cause: power up
              Last software reset at 2020-05-20 19:20, reason: User, spinning module GCodes, available RAM 16096 bytes (slot 3)
              Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0400f000 BFAR 0xe000ed38 SP 0xffffffff Task MAIN
              Error status: 0
              MCU temperature: min 32.7, current 35.3, max 35.5
              Supply voltage: min 0.0, current 15.4, max 15.7, under voltage events: 0, over voltage events: 0, power good: yes
              Driver 0: standstill, read errors 0, write errors 0, ifcount 9, reads 2644, timeouts 0
              Driver 1: standstill, read errors 0, write errors 0, ifcount 9, reads 2644, timeouts 0
              Driver 2: short-to-ground, read errors 0, write errors 0, ifcount 9, reads 2644, timeouts 0
              Driver 3: standstill, read errors 0, write errors 0, ifcount 7, reads 2646, timeouts 0
              Driver 4: standstill, read errors 0, write errors 0, ifcount 6, reads 2647, timeouts 0
              Driver 5: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 2653
              Driver 6: ok, read errors 0, write errors 0, ifcount 0, reads 0, timeouts 2652
              Date/time: 2020-05-20 19:32:27
              Slowest loop: 10.29ms; fastest: 0.12ms
              I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
              === Storage ===
              Free file entries: 9
              SD card 0 detected, interface speed: 15.0MBytes/sec
              SD card longest read time 2.6ms, write time 0.0ms, max retries 0
              === Move ===
              Hiccups: 0(0), FreeDm: 168, MinFreeDm: 168, MaxWait: 26403ms
              Bed compensation in use: none, comp offset 0.000
              === MainDDARing ===
              Scheduled moves: 14, completed moves: 13, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: 3
              === AuxDDARing ===
              Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
              === Heat ===
              Bed heaters = 0 -1, chamberHeaters = -1 -1
              === GCodes ===
              Segments left: 0
              Movement lock held by HTTP
              HTTP is idle in state(s) 1 8, running macro
              Telnet is idle in state(s) 0
              File is idle in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger is idle in state(s) 0
              Queue is idle in state(s) 0
              LCD is idle in state(s) 0
              Daemon is idle in state(s) 0
              Autopause is idle in state(s) 0
              Code queue is empty.
              === Network ===
              Slowest loop: 129.03ms; fastest: 0.02ms
              Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
              HTTP sessions: 1 of 8
              Interface state active, link 100Mbps full duplex

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              • Phaedruxundefined
                Phaedrux Moderator @rickypilnik
                last edited by

                @rickypilnik said in Z-Axis not homing:

                Supply voltage: min 0.0, current 15.4, max 15.7, under voltage events: 0, over voltage events: 0, power good: yes

                Does 15v sound correct for your power supply?

                @rickypilnik said in Z-Axis not homing:

                No I can't move the Z-axis, but x and y are fine even with the message of short to drivers from before.

                The short to ground message was only for driver 2, correct?

                Z-Bot CoreXY Build | Thingiverse Profile

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                • rickypilnikundefined
                  rickypilnik
                  last edited by

                  Yes 15V sounds correct and the message is
                  " Error: short-to-ground reported by driver(s) 2 "

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                  • Phaedruxundefined
                    Phaedrux Moderator
                    last edited by

                    Alright, I think we've established that the Z driver has failed unfortunately. Please hang on while I confer with DC42 in case he has any further ideas.

                    When and where did you purchase your Duet 3?

                    Z-Bot CoreXY Build | Thingiverse Profile

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                    • rickypilnikundefined
                      rickypilnik
                      last edited by

                      On the 5th May 2020, from E3D Online, and it's a Maestro

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                      • Phaedruxundefined
                        Phaedrux Moderator
                        last edited by

                        Ah yes, sorry, Maestro.

                        Z-Bot CoreXY Build | Thingiverse Profile

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                        • Phaedruxundefined
                          Phaedrux Moderator @rickypilnik
                          last edited by

                          @rickypilnik said in Z-Axis not homing:

                          (changed all motor currents to 1875mA (max is 2.5A)

                          I think the reason I assumed it was a Duet 3 was because of this statement on motor current.

                          These motors may not be well suited to the Maestro as it's drivers are rated for 1.4a peak. The Duet wifi is 2.4a and the Duet3 6.3.

                          You'd have to run the drivers at full power to get close to 60% of the rated max for the motors. This will require actively cooling the driver chips.

                          If you send M906 in the console, what does it report back with?

                          Z-Bot CoreXY Build | Thingiverse Profile

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                          • rickypilnikundefined
                            rickypilnik @Phaedrux
                            last edited by rickypilnik

                            @Phaedrux That is quite unfortunate to hear, but if I switch it to a duet 2 wifi you reckon things should be ok?

                            As in it should stop shorting to ground if I use a lower motor current on a different printer, say a CR-10 with motors that max out at 1.5A anyways.

                            Motor current (mA) - X:1875, Y:1875, Z:1875, E:1875, idle factor 30%

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                            • Phaedruxundefined
                              Phaedrux Moderator
                              last edited by

                              Yes a Duet2Wifi/Ethernet would be a much better match for those motors.

                              Z-Bot CoreXY Build | Thingiverse Profile

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                              • rickypilnikundefined
                                rickypilnik
                                last edited by

                                So after all that, having switched boards around I think I found the underlying problem of this all......... A badly crimped factory connector on the Velleman..........AGHH
                                Anyway thanks for all your help you helped solve problems I wasn't even aware of yet!

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                                • Phaedruxundefined
                                  Phaedrux Moderator
                                  last edited by

                                  Glad you got it figured out and the driver hasn't failed.

                                  Z-Bot CoreXY Build | Thingiverse Profile

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