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    Smarteffector problems with 3.11 ( update from 2.04)

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    • fragleundefined
      fragle
      last edited by

      I have found the mistake, there is an optical endstop with some loose contact.
      now it .

      Changed to a news one , and your settings are working.

      But now if i try to run a mesh compensation ( G29), the noozle drives down and then stay around 10mm over the heatplate and stops.

      If i use the old additional Setting for the Z-probe, than the print head crashes into the Heatplate

      31 P100 X0 Y0 Z-0.000 ; Set Z probe trigger value, offset and trigger height
      M557 R150 S20 ; Define mesh grid
      G29 S1 ; Load the heightmap

      jay_s_ukundefined 1 Reply Last reply Reply Quote 0
      • jay_s_ukundefined
        jay_s_uk @fragle
        last edited by

        @fragle can you post your current complete config please. Which delta is it as well?

        Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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        • fragleundefined
          fragle
          last edited by

          It is a Anycubic Predator with a smart effector and default rods

          ; Configuration file for Duet WiFi (firmware version 1.21)
          ; executed by the firmware on start-up
          ;
          ; generated by RepRapFirmware Configuration Tool v2 on Tue Feb 26 2019 21:31:01 GMT+0000 (Greenwich Mean Time)
          
          ; General preferences
          G90                                         				; Send absolute coordinates...
          M83                                         				; ...but relative extruder moves
          
          ; Delta Settings
          M665 L440.000 R227 H430.0 B185.0 						 	; Set delta radius, diagonal rod length, printable radius and homed height
          M666 X0 Y0 Z0 A0.00 B0.00               			     	; Put your endstop adjustments here, or let auto calibration find them
          
          ; Network
          M550 P"Anycubic Predator"                     				; Set machine name
          M551 P""                         							; Set password
          M552 S1
          M552 P192.168.178.10  	                        				; Enable network and acquire dynamic address via DHCP
          M553 P255.255.255.0
          M554 P192.168.178.1
          M586 P0 S1                                  				; Enable HTTP
          M586 P1 S0                                  				; Disable FTP
          M586 P2 S0                                  				; Disable Telnet
          
          ; Drives
          M569 P0 S0                                  				; Drive 0 goes forwards
          M569 P1 S0                                  				; Drive 1 goes forwards
          M569 P2 S0                                  				; Drive 2 goes forwards
          M569 P3 S0                                  				; Drive 3 goes forwards
          M350 X32 Y32 Z32 E16 I1                     				; Configure microstepping with interpolation
          M92 X160.00 Y160.00 Z160.00 E415.00             				; Set steps per mm
          M566 X1000 Y1000 Z1000 E1000    	            			; Set maximum instantaneous speed changes (mm/min)
          M203 X12000.00 Y12000.00 Z12000.00 E10000 					; Set maximum speeds (mm/min)
          M201 X3000.00 Y3000.00 Z3000.00 E3000.00    				; Set accelerations (mm/s^2)
          M906 X1000.00 Y1000.00 Z1000.00 E1000.00 I30 				; Set motor currents (mA) and motor idle factor in per cent
          ;M666 X3 Y0 Z0
          M84 S45                                     				; Set idle timeout
          
          ; Retraction
          M207 S4.0 F5000 R-0.025 T2500 Z0.5							; Firmware retraction
          
          ; Axis Limits
          M208 Z0 S1                                  				; Set minimum Z
          
          ; Endstops
          M574 X1 S1 P"xstop"   ; X min active high endstop switch
          M574 Y1 S1 P"ystop"   ; Y min active high endstop switch
          M574 Z1 S1 P"zstop"   ; Z min active high endstop switch
          M574 U2 S1 P"e0stop"  ; U max active high endstop switch
          
          ; Z-Probe
          M558 P8 H4 F1000 T12000 R0.2 S0.02 A5 C"zprobe.in+zprobe.mod" 
          
          G31 P100 X0 Y0 Z-0.000                      					; Set Z probe trigger value, offset and trigger height
          M557 R150 S20                               				; Define mesh grid
          G29 S1														; Load the heightmap
          
          ; Heaters
          M308 S0 P"bed_temp" Y"thermistor" T100000 B3950 ; define bed temperature sensor
          M308 S1 P"e0_temp" Y"thermistor" T100000 B4725 C7.06e-8 ; define E0 temperature sensor
          M950 H0 C"bed_heat" T0 ; heater 0 uses the bed_heat pin, sensor 0
          M950 H1 C"e0_heat" T1 ; heater 1 uses the e0_heat pin and sensor 1
          M140 H0 ; the bed heater is heater 0
          
          M143 H0 S130								; Set temperature limit for heater 0 to 120C
          M143 H1 S280								; Set temperature limit for heater 1 to 280C
          
          ; Fans
          M950 F0 C"fan0" Q500                           ; create fan 0 on pin fan0 and set its frequency
          M106 P0 S0 H-1                                 ; set fan 0 value. Thermostatic control is turned off
          M950 F1 C"fan1" Q500                           ; create fan 1 on pin fan1 and set its frequency
          M106 P1 S1 H1 T45                              ; set fan 1 value. Thermostatic control is turned on
          
          ;M106 P0 S0 I0 F100 H-1 C"Print Cooling"     ; Set fan 0 value, PWM signal inversion and frequency. Thermostatic control is turned off
          ;M106 P1 S1 I0 F100 H1 T45 C"Heatsink"       ; Set fan 1 value, PWM signal inversion and frequency. Thermostatic control is turned on
          
          ; Tools
          M563 P0 D0 H1                               				; Define tool 0
          G10 P0 X0 Y0 Z0                             				; Set tool 0 axis offsets
          G10 P0 R0 S0                                				; Set initial tool 0 active and standby temperatures to 0C
          
          ; Automatic saving after power loss is not enabled
          
          ; Custom settings are not configured
          M572 D0 S0.1												; Pressure Advance
          ;M591 D0 P2 C4 S1											; Activate filament sensor
          M404 N1.75 													; Set for print monitor
          M592 D0 A0.07772 B-0.00029 									; Nonlinear extrusion. Set parameters for extruder drive 0
          
          ; Miscellaneous
          M501                                               			; Load saved parameters from non-volatile memory
          
          Phaedruxundefined jay_s_ukundefined 2 Replies Last reply Reply Quote 0
          • Phaedruxundefined
            Phaedrux Moderator @fragle
            last edited by

            @fragle said in Smarteffector problems with 3.11 ( update from 2.04):

            G29 S1

            Don't load the heightmap in config.g. It should only ever be loaded or freshly created after probing the bed with G30 to set Z0.

            What do you have in bed.g and homedelta.g?

            Z-Bot CoreXY Build | Thingiverse Profile

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            • fragleundefined
              fragle
              last edited by

              bed.g

              ; bed.g file for RepRapFirmware, generated by Escher3D calculator
              ; 16 points, 6 factors, probing radius: 160, probe offset (0, 0)
              G28
              G30 P0 X0.00 Y160.00 Z-99999 H0
              G30 P1 X102.85 Y122.57 Z-99999 H0
              G30 P2 X157.57 Y27.78 Z-99999 H0
              G30 P3 X138.56 Y-80.00 Z-99999 H0
              G30 P4 X54.72 Y-150.35 Z-99999 H0
              G30 P5 X-54.72 Y-150.35 Z-99999 H0
              G30 P6 X-138.56 Y-80.00 Z-99999 H0
              G30 P7 X-157.57 Y27.78 Z-99999 H0
              G30 P8 X-102.85 Y122.57 Z-99999 H0
              G30 P9 X0.00 Y80.00 Z-99999 H0
              G30 P10 X69.28 Y40.00 Z-99999 H0
              G30 P11 X69.28 Y-40.00 Z-99999 H0
              G30 P12 X0.00 Y-80.00 Z-99999 H0
              G30 P13 X-69.28 Y-40.00 Z-99999 H0
              G30 P14 X-69.28 Y40.00 Z-99999 H0
              G30 P15 X0 Y0 Z-99999 S6
              

              homedelta.g

              ; homedelta.g
              ; called to home all towers on a delta printer
              ;
              ; generated by RepRapFirmware Configuration Tool v2 on Tue Feb 26 2019 21:31:01 GMT+0000 (Greenwich Mean Time)
              G91                        ; relative positioning
              G1 H1 X470 Y470 Z470 F1800 ; move all towers to the high end stopping at the endstops (first pass)
              G1 H1 X10 Y10 Z10 F360     ; move all towers up once more (second pass)
              G90                        ; absolute positioning
              
              
              
              
              jay_s_ukundefined 1 Reply Last reply Reply Quote 0
              • jay_s_ukundefined
                jay_s_uk @fragle
                last edited by

                @fragle ok
                Few issues I can see if your config.
                M350 only supports Interpolation of microsteps at x16, so I suggest you change back to x16 and the steps per mm to 80.
                Secondly, your endstop settings are incorrect. You have them set as being on the low end when infact they are on the high end. The correct settings are

                M574 X2 S1 P"xstop"
                M574 Y2 S1 P"ystop"
                M574 Z2 S1 P"zstop"
                

                Your G31 should have z set as -0.1

                Here is my predator config for reference https://github.com/jaysuk/Anycubic-Predator-Duet/tree/SmartEffectorRRF3

                Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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                • jay_s_ukundefined
                  jay_s_uk @fragle
                  last edited by

                  @fragle your homing file is also incorrect as it doesn't move the towers down before trying to home again.
                  This is what it should contain.

                  G91                        ; relative positioning
                  
                  G1 H1 X470 Y470 Z470 F1800 ; move all towers to the high end stopping at the endstops (first pass)
                  G1 X-5 Y-5 Z-5 F1800 H2    ; go down a few mm
                  G1 H1 X10 Y10 Z10 F360     ; move all towers up once more (second pass)
                  G1 Z-5 F6000               ; move down a few mm so that the nozzle can be centred
                  G90                        ; absolute positioning
                  G1 X0 Y0 F6000             ; move X+Y to the centre
                  

                  Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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                  • fragleundefined
                    fragle
                    last edited by

                    I ve adaped my config to your settings, now G32 is working well, but with the mesh compensation i am getting an G29 error Z probe readings are not consistent

                    At G29 the printhead goes down correctly, make some soft touches to the print plate and after around 4 or 5 point he stand still.

                    M557 set mesh parameter said 175 radius and 16 spacing

                    Phaedruxundefined jay_s_ukundefined 2 Replies Last reply Reply Quote 0
                    • fragleundefined
                      fragle
                      last edited by

                      oh i forgot, i have an whambam printplate over the normal print plate

                      1 Reply Last reply Reply Quote 0
                      • Phaedruxundefined
                        Phaedrux Moderator @fragle
                        last edited by

                        @fragle said in Smarteffector problems with 3.11 ( update from 2.04):

                        At G29 the printhead goes down correctly, make some soft touches to the print plate and after around 4 or 5 point he stand still.

                        Might need sensitivity adjusted for the smart effector? Higher probe speed?

                        Z-Bot CoreXY Build | Thingiverse Profile

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                        • jay_s_ukundefined
                          jay_s_uk @fragle
                          last edited by

                          @fragle you've probably got play in your system with the default arms. Try increasing the S value on M558 to something like 0.05

                          Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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                          • fragleundefined
                            fragle
                            last edited by

                            I will try the suggestions today, but i do not thing, that it is an hardware problem, because the system is running on fw 2.04 without any problems.

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                            • fragleundefined
                              fragle
                              last edited by

                              small update

                              if i use G32, than i am getting

                              Calibrated 8 factors using 16 points, (mean, deviation) before (-0.004, 0.067) after (-0.000, 0.053)
                              Repeating calibration because deviation is too high (0.053mm)
                              too many auto calibration attempts

                              jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                              • jay_s_ukundefined
                                jay_s_uk @fragle
                                last edited by

                                @fragle so change the S value to 0.06 (or even slightly higher)
                                Currently, any value above 0.05 (originally 0.02) will cause it to fail.
                                Its due to the sloppy eyes they use on the rods on the predator.

                                Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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                                • fragleundefined
                                  fragle
                                  last edited by

                                  G32 is now successful after the second run

                                  I have set the sensitivtiy to 10 for the smart effector, but i am wondering, why the display of the Z probe switches to "1000" around every third contact to the print plate.

                                  The other 2 hits, there was no "1000" release on the display ( even tough the nozzle hits the plate and withdraw correct.

                                  jay_s_ukundefined 1 Reply Last reply Reply Quote 0
                                  • jay_s_ukundefined
                                    jay_s_uk @fragle
                                    last edited by

                                    @fragle DWC generally doesn't catch up enough to fully display every probe. If it works, don't worth about it.

                                    Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

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                                    • fragleundefined
                                      fragle
                                      last edited by

                                      I have crosschecked the predator with my old 2.04 settings, everything is working fine.

                                      Back to 3.1.1

                                      Now i can run G32 and G29 without error.

                                      I i try to print something i use as start script
                                      G28
                                      G32

                                      During the G32 from the gcode i am getting always an
                                      Error: Z Probe already triggered at atrt of probing mode

                                      I have reset the sensififity to 131:131 ( default setting)

                                      i ve tried some configs starting from here https://duet3d.dozuki.com/Wiki/Test_and_calibrate_the_Z_probe to some hints in the forum, but nothing worked.

                                      dc42undefined 1 Reply Last reply Reply Quote 0
                                      • dc42undefined
                                        dc42 administrators @fragle
                                        last edited by dc42

                                        @fragle said in Smarteffector problems with 3.11 ( update from 2.04):

                                        Error: Z Probe already triggered at atrt of probing mode

                                        There are a few possible reasons for this:

                                        1. The Smart Effector is triggering when it shouldn't. If this is happening, you will see the green LED on the effector flashing. But if you are sure that it works under RRF 2.05.1, that can't be the problem.
                                        2. Vibration or deceleration after the positioning move is causing the effector to trigger. If it's vibration, reducing the sensitivity will help. If it's deceleration after the positioning move, increase the M558 R parameter.
                                        3. The effector output wire is picking up interference from an adjacent stepper motor wire. If that is the cause, and you are using probe type 5 in M558, increasing the G50 P parameter may help.

                                        Are you using exactly the same parameter values (except for the ones where the command format has changed) in 3.1.1 as in 2.04, in your M558, M201, M203, M566, M906 and M569 commands in config.g?

                                        Duet WiFi hardware designer and firmware engineer
                                        Please do not ask me for Duet support via PM or email, use the forum
                                        http://www.escher3d.com, https://miscsolutions.wordpress.com

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                                        • fragleundefined
                                          fragle
                                          last edited by

                                          small update:

                                          I ve upgraded to firmware 3.2 an now i can print, but i have to adjust the Printhead at printing with 0,2mm babysteps.

                                          If i try to calibrate the Z Probe as described here https://duet3d.dozuki.com/Wiki/Test_and_calibrate_the_Z_probe i am getting -0,01 . Nothing change if i will change the z value to 0,2

                                          Phaedruxundefined 1 Reply Last reply Reply Quote 0
                                          • Phaedruxundefined
                                            Phaedrux Moderator @fragle
                                            last edited by

                                            @fragle said in Smarteffector problems with 3.11 ( update from 2.04):

                                            i am getting -0,01

                                            It should be slightly negative because it's pressing into the bed. Why do you want to use 0.2?

                                            Z-Bot CoreXY Build | Thingiverse Profile

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