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    Error: bad Command XXX W/RRF 3.2 and leveling issue

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    • martin7404undefined
      martin7404
      last edited by martin7404

      I am one of the other 2 that are running the same printer design
      What was the version you ran before update to 3.2.
      I updated while changing Z steppers and have the same thing with the back left low and front right high but within 0.15 , so I thought it is something with the magnet base and spring steel sheet. Later I will roll back to 3.0 and try.
      One more thing for now I am runing G29 with 6*6 grid every print and there is some variaton map to map.

      Muldex IDEX Duet2+Duex5
      Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
      Sapphire Pro with Duet2, with closed-loop motors
      custom high temp E3D tool changer with Duet2+Duex

      3DPrintingWorldundefined 1 Reply Last reply Reply Quote 0
      • 3DPrintingWorldundefined
        3DPrintingWorld @martin7404
        last edited by

        @martin7404 Hey Martin, I didn't realize you were having a issue as well. I was on 3.1.1, Gui is still on it and is not having the same issue. We double checked our config's but could not find any differences that would matter. I just tried reverting back to 3.1.1, I still get the error but not the fan issue, and its still not homing properly. Maybe updating the firmware is just a coincidence as I was making some other changes at the same time.

        Strange that your map is not repeating. I've done trigger testes where I move the probe 200mm in each direction and back before probes and it repeats within .001-.01. I don't understand how I can use three points to level, then do a trigger height on each point and it says the deviation is only .005, but its actually closer to .25mm.

        martin7404undefined 1 Reply Last reply Reply Quote 0
        • 3DPrintingWorldundefined
          3DPrintingWorld @Veti
          last edited by

          @Veti said in Error: bad Command XXX W/RRF 3.2 and leveling issue:

          post m122 output

          I just reverted to 3.1.1 to see what happens and the fan no longer turns on at startup but I still get the alarms. The bed is still not leveling properly so I assume that is unrelated.

          === Diagnostics ===
          RepRapFirmware for Duet 2 WiFi/Ethernet version 3.1.1 running on Duet WiFi 1.02 or later + DueX5
          Board ID: 08DGM-9T6BU-FG3SJ-6J1FA-3SN6J-1VYRG
          Used output buffers: 3 of 24 (18 max)
          === RTOS ===
          Static ram: 27980
          Dynamic ram: 96468 of which 44 recycled
          Exception stack ram used: 344
          Never used ram: 6236
          Tasks: NETWORK(ready,348) HEAT(blocked,1224) DUEX(suspended,160) MAIN(running,1880) IDLE(ready,80)
          Owned mutexes: WiFi(NETWORK)
          === Platform ===
          Last reset 00:08:07 ago, cause: software
          Last software reset time unknown, reason: User, spinning module GCodes, available RAM 6316 bytes (slot 1)
          Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task MAIN
          Error status: 0
          MCU temperature: min 38.7, current 39.2, max 39.9
          Supply voltage: min 24.0, current 24.2, max 24.4, under voltage events: 0, over voltage events: 0, power good: yes
          Driver 0: standstill, SG min/max not available
          Driver 1: standstill, SG min/max not available
          Driver 2: standstill, SG min/max not available
          Driver 3: standstill, SG min/max not available
          Driver 4: standstill, SG min/max not available
          Driver 5: standstill, SG min/max not available
          Driver 6: standstill, SG min/max not available
          Driver 7: standstill, SG min/max not available
          Driver 8: standstill, SG min/max not available
          Driver 9: standstill, SG min/max not available
          Date/time: 2021-02-07 11:43:46
          Cache data hit count 826594182
          Slowest loop: 9.38ms; fastest: 0.14ms
          I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0
          === Storage ===
          Free file entries: 10
          SD card 0 detected, interface speed: 20.0MBytes/sec
          SD card longest read time 3.8ms, write time 0.0ms, max retries 0
          === Move ===
          Hiccups: 0(0), FreeDm: 169, MinFreeDm: 169, MaxWait: 0ms
          Bed compensation in use: none, comp offset 0.000
          === MainDDARing ===
          Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
          === AuxDDARing ===
          Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1
          === Heat ===
          Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
          === GCodes ===
          Segments left: 0
          Movement lock held by null
          HTTP is idle in state(s) 0
          Telnet is idle in state(s) 0
          File is idle in state(s) 0
          USB is idle in state(s) 0
          Aux is idle in state(s) 0
          Trigger is idle in state(s) 0
          Queue is idle in state(s) 0
          Daemon is idle in state(s) 0
          Autopause is idle in state(s) 0
          Code queue is empty.
          === Network ===
          Slowest loop: 16.53ms; fastest: 0.00ms
          Responder states: HTTP(2) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions
          HTTP sessions: 1 of 8

          • WiFi -
            Network state is active
            WiFi module is connected to access point
            Failed messages: pending 0, notready 0, noresp 0
            WiFi firmware version 1.23
            WiFi MAC address 60:01:94:2e:09:23
            WiFi Vcc 3.39, reset reason Unknown
            WiFi flash size 4194304, free heap 23088
            WiFi signal strength -54dBm, reconnections 0, sleep mode modem
            Socket states: 4 0 0 0 0 0 0 0
            === Filament sensors ===
            Extruder 0: pos 145.20, errs: frame 0 parity 0 ovrun 0 pol 0 ovdue 0
            Extruder 1: no data received
            === DueX ===
            Read count 1, 0.12 reads/min
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          • 3DPrintingWorldundefined
            3DPrintingWorld
            last edited by

            This is bed.g, I do three points as close as I can to the beds connection points. I have also tried four corners and three points closer to center but results are similar.

            G30 P0 X200 Y285 Z-99999   ; Probe Middle
            G30 P1 X15 Y15 Z-99999     ; Probe Left
            G30 P2 X324 Y15 Z-99999 S3 ; Probe Right
            
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            • 3DPrintingWorldundefined
              3DPrintingWorld
              last edited by

              The important bits of the config for auto leveling. Drives are called out in the same order and their physical location, from left to right.

              Identical locations work for another user and had worked previously for me.

              Drives:

              M569 P5 S0                                      ; Z left physical drive 5 goes backwards 0
              M569 P6 S0                                      ; Z center physical drive 6 goes backwards
              M569 P7 S1                                      ; Z right physical drive 7 goes forwards 1
              

              Mapping

              M584 X0 Y1:2 U3 Z5:6:7 E4:8                     ; set drive mapping
              

              Bed Connection Locations

              M671 X-20.6:200:420.6 Y14.3:333.3:14.3 S5       ; Locations left, center, right 
              
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              • 3DPrintingWorldundefined
                3DPrintingWorld
                last edited by

                ; Drives
                M569 P0 S0                                      ; X physical drive 0 goes backwards
                M569 P1 S0                                      ; Y right physical drive 1 goes forwards
                M569 P2 S1                                      ; Y left physical drive 8 goes backwards
                M569 P3 S1                                      ; U physical drive 2 goes backwards
                M569 P4 S0                                      ; E1 physical drive 3 goes forwards
                M569 P5 S0                                      ; Z left physical drive 5 goes backwards 0
                M569 P6 S0                                      ; Z center physical drive 6 goes backwards
                M569 P7 S1                                      ; Z right physical drive 7 goes forwards 1
                M569 P8 S0                                      ; E2 physical drive 4 goes forwards
                
                M584 X0 Y1:2 U3 Z5:6:7 E4:8                     ; set drive mapping
                
                M350 X16 U16 Y16 Z16 E16:16 I1                                                        ; configure microstepping with interpolation
                M92 X100.00 U100.00 Y100.00:100.00 Z1096:1096:1096 E415.00:655.00                   ; set steps per mm (1760nimble)
                M566 X1000.00 U1000.00 Y1000.00:1000.00 Z80.00:80.00:80.00 E100.00:300.00                   ; set maximum instantaneous speed changes (mm/min)(Nimble 40)
                M203 X12000.00 U12000.00 Y12000.00:12000.00 Z2000.00:2000.00:2000.00 E4200.00:4200.00 ; set maximum speeds (mm/min)
                M201 X800.00 U800.00 Y800.00:800.00 Z35.00:35.00:35.00 E600.00:600.00                ; set accelerations (mm/s^2)(500)(Nimble 120)
                M906 X700 U700 Y700:700 Z200:200:200 E800:600 I30                                     ; set motor currents (mA) and motor idle factor in per cent(Nimble 500)
                M84 S30                                                                               ; Set idle timeout
                
                ; Axis Limits
                M208 X-21.4 Y0 U33 Z0 S1                        ; set axis min was (-18 BMG)16.7_X-14.4 Y0 U40 Z0 S1
                M208 X344 U415.7 Y334 Z300 S0                     ; set axis max Y WAS 339_X350 U422.7 Y334 Z300 S0
                
                M669 K0 Y1:-1:0:1				                ; select Markforged Kinematics Y to react with X and U
                
                ; Endstops 
                M574 X1 S1 P"xstop"                             ;X axis active high endstop switch
                M574 Y2 S1 P"ystop+zstop"                       ; Y Double max active high endstop switch
                M574 U2 S1 P"duex.e2stop"                            ;U axis active high endstop switch
                M574 Z1 S2 						; Define Z to use Probe. Home to Min.
                
                ; Filament Sensor
                M591 D0 P3 C"e0stop" S1 R70:130 L24.8 E3.0 ; Duet3D rotating magnet sensor for extruder drive 0 is connected to E0 endstop input, enabled, sensitivity 24.8mm.rev, 70% to 130% tolerance, 3mm detection length
                M591 D1 P3 C"e1stop" S0 R70:130 L24.8 E3.0 ; Duet3D rotating magnet sensor for extruder drive 0 is connected to E0 endstop input, enabled, sensitivity 24.8mm.rev, 70% to 130% tolerance, 3mm detection length
                
                M591 D0 ; display filament sensor parameters for extruder drive 0
                M591 D1 ; display filament sensor parameters for extruder drive 0
                
                ; Z-Probe
                M671 X-20.6:200:420.6 Y14.3:333.3:14.3 S5       ; Locations left, center, right 
                M950 S0 C"duex.e6heat"                          ; create servo pin 0 for BLTouch
                M558 P9 C"zprobe.in" H5 F120 T5000   ; set Z probe type to bltouch and the dive height + speeds (WAS 9000)
                G31 P25 X-29 Y0 Z1.37                             ; set Z probe trigger value, offset and trigger height(lower number farther away)1.54build 1.44glass 
                M557 X10:360 Y10:290 S20                        ; probe from X=10 to 390, Y=10 to 290mm with a mesh spacing of 20mm
                
                ; Heaters
                M308 S0 P"bedtemp" Y"thermistor" T100000 B4534 C9.565227e-8      ; configure sensor 0 as thermistor on pin bedtemp
                M950 H0 C"bedheat" T0                                            ; create bed heater output on bedheat and map it to sensor 0
                M143 H0 S120                                                     ; set temperature limit for heater 0 to 120C
                M307 H0 B0 S1.00                                                 ; disable bang-bang mode for the bed heater and set PWM limit
                M140 H0                                                          ; map heated bed to heater 0
                M308 S1 P"e0temp" Y"thermistor" T500000 B4723 C1.196220e-7 R4700 ; configure sensor 1 as thermistor on pin e0temp
                M950 H1 C"e0heat" T1                                             ; create nozzle heater output on e0heat and map it to sensor 1
                M143 H1 S280                                                     ; set temperature limit for heater 1 to 280C
                M307 H1 B0 S1.00                                                 ; disable bang-bang mode for heater  and set PWM limit
                M308 S2 P"e1temp" Y"thermistor" T500000 B4723 C1.196220e-7 R4700 ; configure sensor 2 as thermistor on pin e1temp
                M950 H2 C"e1heat" T2                                             ; create nozzle heater output on e1heat and map it to sensor 2
                M143 H2 S280                                                     ; set temperature limit for heater 2 to 280C
                M307 H2 B0 S1.01                                                 ; disable bang-bang mode for heater  and set PWM limit
                
                ; Fans
                M950 F0 C"fan0" Q500                             ; create fan 0 on pin fan0 and set its frequency
                M106 P0 S0 H-1                                   ; set fan 0 value. Thermostatic control is turned off
                M950 F1 C"fan1" Q500                             ; create fan 1 on pin fan1 and set its frequency
                M106 P1 S1 H1 T45                                ; set fan 1 value. Thermostatic control is turned on
                M950 F2 C"duex.fan4" Q500                             ; create fan 2 on pin fan2 and set its frequency
                M106 P2 S0 H-1                                   ; set fan 2 value. Thermostatic control is turned off
                M950 F3 C"duex.fan8" Q500                        ; create fan 3 on pin duex.fan8 and set its frequency
                M106 P3 S1 H2 T45                                ; set fan 3 value. Thermostatic control is turned on
                
                ; LEDs
                M950 F4 C"duex.fan6" ;Q500                       ; create LED 4 on pin duex.fan6 and set its frequency
                M106 P4 S255 H-1                                 ; set LED 4 value. Thermostatic control is turned OFF
                M950 F5 C"duex.fan7" ;Q500                       ; create LED 5 on pin duex.fan7 and set its frequency
                M106 P5 S255 H-1                                 ; set LED 5 value. Thermostatic control is turned OFF
                
                ; Tools
                M563 P0 D0 H1 F0 S"Left"                      ; define tool 0 Left 
                G10 P0 X0 Y0 Z0                               ; set tool 0 axis offsets y was .45
                G10 P0 R0 S0                                     ; set initial tool 0 active and standby temperatures to 0C
                
                M563 P1 D1 H2 X3 F2 S"Right"                        ; define tool 1 Right
                G10 P1 X0 Y-1.45 Z0                                  ; set tool 1 axis offsets (.5BMG)
                G10 P1 R0 S0                                     ; set initial tool 1 active and standby temperatures to 0C
                
                M563 P2 D0:1 H1:2 X0:3 F0:2 S"Copy"              ; define tool 2 Copy
                G10 P2 X95 Y0 U-95 S0 R0                         ; set tool 2 axis offsets (WAS 105)
                M567 P2 E1:1         
                M568 P2 S1 ; turn on mixing for tool 2           ; set mix ratio 100% on both extruders
                
                M501                                             ; Record
                
                M575 P1 S1 B57600                                ;Panel due
                
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                • martin7404undefined
                  martin7404 @3DPrintingWorld
                  last edited by

                  @3DPrintingWorld Before your post I thought 0.15 was from the magnetic mat and steel sheet. Before the update, I was with 3.0. The 3 Z motors are new , but my Z print calibration is within 0.02mm so the steps are correct For G32 I do it 2 times from the beginning

                  Muldex IDEX Duet2+Duex5
                  Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
                  Sapphire Pro with Duet2, with closed-loop motors
                  custom high temp E3D tool changer with Duet2+Duex

                  1 Reply Last reply Reply Quote 0
                  • Vetiundefined
                    Veti
                    last edited by

                    @3DPrintingWorld said in Error: bad Command XXX W/RRF 3.2 and leveling issue:

                    M92 X100.00 U100.00 Y100.00:100.00 Z1096:1096:1096 E415.00:655.00

                    z does not allow for more than one value

                    remove them from M566 M92 M203 M201 and M906

                    what i did for the bed leveling to see if the adjustments were correct is look at the heightmap before and after a g32.

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                    • martin7404undefined
                      martin7404
                      last edited by martin7404

                      Anyway, the manual says it will take the first one, so no problem. Also as stated it was working fine before the firmware update.
                      What G32 has to do with the heightmap, that is made with g29 probing. G32 just levels the bed on 3 points

                      Muldex IDEX Duet2+Duex5
                      Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
                      Sapphire Pro with Duet2, with closed-loop motors
                      custom high temp E3D tool changer with Duet2+Duex

                      fcwiltundefined 3DPrintingWorldundefined 2 Replies Last reply Reply Quote 0
                      • fcwiltundefined
                        fcwilt @martin7404
                        last edited by fcwilt

                        @3DPrintingWorld said in Error: bad Command XXX W/RRF 3.2 and leveling issue:

                        @martin7404

                        Also as stated it was working fine before the firmware update.

                        I have no idea if this is related but it might be.

                        On my 3 Z stepper printer each Z stepper has it's own end stop sensor. The Z steppers are on the Duex 5 board.

                        I home Z using the end stop sensors which have been carefully adjusted to result in the bed being very nearly level.

                        I then use G32 to perform the final bed leveling.

                        Under 3.1.1 everything worked fine for months and months of use. I recently upgraded to 3.2.0.

                        Under 3.2.0 Z homing frequently failed as one of the Z steppers would fail to stop when it's end stop sensor was triggered.

                        Since I could not rely on the Z homing I never moved on to the next step of using G32 so I cannot say if that would have worked or not.

                        Frederick

                        Printers: a E3D MS/TC setup and a RatRig Hybrid. Using Duet 3 hardware running 3.4.6

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                        • 3DPrintingWorldundefined
                          3DPrintingWorld @martin7404
                          last edited by

                          @martin7404 said in Error: bad Command XXX W/RRF 3.2 and leveling issue:

                          Anyway, the manual says it will take the first one, so no problem.

                          I'll take them out to neaten it up anyways.

                          Agreed, the height map should not have anything to do with it. Right now the height map is cleared and I'm just trying to get the bed level to the nozzle.

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                          • martin7404undefined
                            martin7404
                            last edited by

                            I played a little with G32 . Strange
                            After initial tramming twice with G32
                            Here is 5 more made one after other

                            2/8/2021, 12:50:52 PM	g32
                            Leadscrew adjustments made: 0.007 -0.004 -0.028, points used 3, (mean, deviation) before (-0.008, 0.010) after (-0.000, 0.000)
                            2/8/2021, 12:36:06 PM	G32 bed probe heights: 0.003 -0.006 -0.020, mean -0.008, deviation from mean 0.009
                            2/8/2021, 12:35:43 PM	g32
                            Leadscrew adjustments made: -0.000 -0.007 0.017, points used 3, (mean, deviation) before (0.003, 0.008) after (-0.000, 0.000)
                            2/8/2021, 12:32:41 PM	G32 bed probe heights: 0.008 -0.006 0.013, mean 0.005, deviation from mean 0.008
                            2/8/2021, 12:32:18 PM	g32
                            Leadscrew adjustments made: -0.008 -0.007 0.018, points used 3, (mean, deviation) before (0.000, 0.009) after (0.000, 0.000)
                            2/8/2021, 12:31:32 PM	G32 bed probe heights: 0.009 -0.006 0.014, mean 0.005, deviation from mean 0.008
                            2/8/2021, 12:31:09 PM	g32
                            Leadscrew adjustments made: 0.092 -0.021 -0.039, points used 3, (mean, deviation) before (0.018, 0.044) after (-0.000, 0.000)
                            2/8/2021, 12:29:59 PM	G32 bed probe heights: 0.060 -0.013 -0.019, mean 0.010, deviation from mean 0.036
                            2/8/2021, 12:29:36 PM	g32
                            Leadscrew adjustments made: -0.110 -0.019 0.009, points used 3, (mean, deviation) before (-0.046, 0.038) after (0.000, 0.000)
                            

                            Muldex IDEX Duet2+Duex5
                            Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
                            Sapphire Pro with Duet2, with closed-loop motors
                            custom high temp E3D tool changer with Duet2+Duex

                            1 Reply Last reply Reply Quote 0
                            • Vetiundefined
                              Veti
                              last edited by

                              post a picture of the mesh bed leveling

                              1 Reply Last reply Reply Quote 0
                              • martin7404undefined
                                martin7404
                                last edited by

                                81eb957a-e35d-4f1b-850b-3c616d15081c-image.png

                                Muldex IDEX Duet2+Duex5
                                Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
                                Sapphire Pro with Duet2, with closed-loop motors
                                custom high temp E3D tool changer with Duet2+Duex

                                1 Reply Last reply Reply Quote 0
                                • martin7404undefined
                                  martin7404
                                  last edited by

                                  So I roll back to 3.1.1 and the heatmap is consistent, the tramming is working kind of. the deviation can be due to magnetic mat + steel sheet

                                  Muldex IDEX Duet2+Duex5
                                  Custom CoreXY 600x400 Hemera , Duet3+Toolboard+1HCL closed loop
                                  Sapphire Pro with Duet2, with closed-loop motors
                                  custom high temp E3D tool changer with Duet2+Duex

                                  3DPrintingWorldundefined 1 Reply Last reply Reply Quote 0
                                  • 3DPrintingWorldundefined
                                    3DPrintingWorld @martin7404
                                    last edited by

                                    @martin7404 said in Error: bad Command XXX W/RRF 3.2 and leveling issue:

                                    So I roll back to 3.1.1

                                    Surprised that made a difference, it didn't do anything for me when I reverted.

                                    The leveling seems very consistent, just not level. I'm gong to try putting incorrect locations into the M671 to see if I can trick it into leveling properly. The front right corner is high so I'm going to move that point out further in the X until the bed is level. If I adjust just this motor by hand it seems to fall into level so it should work.

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                                    • 3DPrintingWorldundefined
                                      3DPrintingWorld
                                      last edited by

                                      The two front motors are aligned in the X axis so I physically swapped motors, and switched the rotation direction in the config so they run in the correct direction. Now when it corrects for level it should be backwards, but it levels it exactly the same! Left back corner low, right front corner high.

                                      I also moved the front right motor location in the M671 over as much as 350mm, but it has no effect and levels exactly the same! Left back corner low, right front corner high.

                                      How can making these changes have no effect on level? The results should be all jacked up but nothing I do seems to have any effect on the outcome. At the same time, I don't understand how its correcting to the same bad plan every time even though I've giving it bad information.

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                                      • Phaedruxundefined
                                        Phaedrux Moderator
                                        last edited by

                                        @3DPrintingWorld said in Error: bad Command XXX W/RRF 3.2 and leveling issue:

                                        I don't understand how its correcting to the same bad plan every time even though I've giving it bad information.

                                        Are the files you are editing the actual files being used? Occasionally someone will edit a macro file in the macros folder without realizing the file they should be editing is actually in the sys folder. Could it be something like that happening here?

                                        Z-Bot CoreXY Build | Thingiverse Profile

                                        3DPrintingWorldundefined 1 Reply Last reply Reply Quote 0
                                        • 3DPrintingWorldundefined
                                          3DPrintingWorld @Phaedrux
                                          last edited by

                                          @Phaedrux Ha, you got to give me more credit then that. Yes, I'm modifying the config file in my systems folder. I know because I also swapped the left and right stepper motors and if I don't update the directions in the config one of the motors will be rotating in the wrong direction. Speaking that, like it says here. When I swap the X motors it should be leveling the opposite but I swapped the motors but its still identically off level.

                                          swap.png

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                                          • Phaedruxundefined
                                            Phaedrux Moderator
                                            last edited by

                                            I had to ask. It happens sometimes.

                                            Z-Bot CoreXY Build | Thingiverse Profile

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