• Tags
  • Documentation
  • Order
  • Register
  • Login
Duet3D Logo Duet3D
  • Tags
  • Documentation
  • Order
  • Register
  • Login

Need help diagnosing bad stepper output signal on Duet 3

Scheduled Pinned Locked Moved
Duet Hardware and wiring
3
19
641
Loading More Posts
  • Oldest to Newest
  • Newest to Oldest
  • Most Votes
Reply
  • Reply as topic
Log in to reply
This topic has been deleted. Only users with topic management privileges can see it.
  • undefined
    Rushmere3D @Noah
    last edited by 13 Feb 2021, 22:46

    @Noah

    If you run M98 P"config.g" again and it gives the same result as before, I think it's because you have multiple factors when you don't need them. If you tell the firmware the Z is 0.2:0.3:0.4 it knows to use one setting for all 3 steppers.

    Follow my adventures in 3D Printing, laser cutting and electronics. https://linktr.ee/Rushmere3D

    undefined 1 Reply Last reply 13 Feb 2021, 22:46 Reply Quote 0
    • undefined
      Phaedrux Moderator @Noah
      last edited by 13 Feb 2021, 22:46

      @Noah said in Need help diagnosing bad stepper output signal on Duet 3:

      M350 X16 Y16 Z16 E16:16:16 I1 to M350 X16 Y16 Z16:16:16 E16 I1

      The Z axis only needs a single entry as well. It's only when you have multiple extruder axis that each axis needs to be defined. The other axis with multiple motors all use the same settings since they aren't independent.

      So remove the multiple Z values as well.

      Z-Bot CoreXY Build | Thingiverse Profile

      1 Reply Last reply Reply Quote 1
      • undefined
        Phaedrux Moderator @Rushmere3D
        last edited by 13 Feb 2021, 22:46

        @Rushmere3D JYNX again!

        Z-Bot CoreXY Build | Thingiverse Profile

        undefined 1 Reply Last reply 13 Feb 2021, 22:47 Reply Quote 0
        • undefined
          Rushmere3D @Phaedrux
          last edited by 13 Feb 2021, 22:47

          @Phaedrux haha

          Follow my adventures in 3D Printing, laser cutting and electronics. https://linktr.ee/Rushmere3D

          1 Reply Last reply Reply Quote 0
          • undefined
            Noah
            last edited by 13 Feb 2021, 22:56

            ok, haha
            thank you so much for dealing with the noob over here. I corrected all of the lines after m671 to show only one value for X,Y,Z,E
            I was just copying what the RRF config tool gave me for the multiple E motors since it did not have any option to add extra Z motors.
            Z homing and G32 working perfect again, and I only have one data point for motor 5 now
            Fingers crossed.

            undefined 1 Reply Last reply 13 Feb 2021, 23:13 Reply Quote 0
            • undefined
              Noah
              last edited by 13 Feb 2021, 22:57

              as soon as the hotend heats up and it will let me send extrude and retract commands, I'll let you know if the ext motor is behaving any differently now

              1 Reply Last reply Reply Quote 0
              • undefined
                Noah
                last edited by 13 Feb 2021, 23:05

                Hahahaha Phaedrux & Rushmere You guy are amazing!!!
                wish I had asked a little sooner for someone to review my code... I really caused myself a couple of days of grief over here... I have good motor function on all motors now.
                Now, I am off to tune my extrusion steps and try a print!|

                Thank You both soooooo much

                Noah

                1 Reply Last reply Reply Quote 0
                • undefined
                  Noah
                  last edited by Noah 13 Feb 2021, 23:07

                  Proper config for others refernce

                  ; Drives
                  M569 P0.0 S1 ; physical drive 0.0 goes forwards
                  M569 P0.1 S1 ; physical drive 0.1 goes forwards
                  M569 P0.2 S1 ; physical drive 0.2 goes forwards
                  M569 P0.3 S1 ; physical drive 0.3 goes forwards
                  M569 P0.4 S1 ; physical drive 0.4 goes forwards
                  M569 P0.5 S1 ; physical drive 0.5 goes forwards
                  M584 X0.0 Y0.1 Z0.2:0.3:0.4 E0.5
                  M671 X-30.109:146.1:322.309 Y-10.413:317.797:-10.413 S50
                  M350 X16 Y16 Z16 E16 I1
                  M92 X160.00 Y160.00 Z1600.00 E873.00
                  M566 X1200.00 Y1200.00 Z30.00 E1800.00
                  M203 X18000.00 Y18000.00 Z1800.00 E3000.00
                  M201 X1600.00 Y1600.00 Z100.00 E2000.00
                  M906 X1200 Y1200 Z800 E950 I30
                  M84 S30

                  1 Reply Last reply Reply Quote 1
                  • undefined
                    Phaedrux Moderator @Noah
                    last edited by 13 Feb 2021, 23:13

                    Glad you got it sorted.

                    Z-Bot CoreXY Build | Thingiverse Profile

                    1 Reply Last reply Reply Quote 0
                    • undefined
                      Noah
                      last edited by 13 Feb 2021, 23:18

                      I still do have the
                      Error: in file macro line 21: M350: array too long, max length = 1

                      but only for the M350 line

                      That's strange... what doesn't it like about my M350 X16 Y16 Z16 E16 I1

                      1 Reply Last reply Reply Quote 0
                      • undefined
                        Phaedrux Moderator
                        last edited by 14 Feb 2021, 00:27

                        Please upload your actual config.g file

                        Z-Bot CoreXY Build | Thingiverse Profile

                        1 Reply Last reply Reply Quote 0
                        18 out of 19
                        • First post
                          18/19
                          Last post
                        Unless otherwise noted, all forum content is licensed under CC-BY-SA