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    3.3B3 certain lines cause firmware reset

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    • deckingmanundefined
      deckingman
      last edited by

      As my name was mentioned, the fault I'm experiencing is consistent in that reverting back to RRF3.2 fixes in and "upgrading to 3.3. causes it. I've repeated this a few times. There appears to be a reset of the main board (but not the expansion boards) which is bought about by running a macro which uses M116 to wait for heaters to attain their set temperatures. In my case, no conditional gcode is used in this particular macro and the machine is in stand alone mode (no SBC) running a 6HC main board and 3 expansion boards. So maybe a different fault to the OP.

      Ian
      https://somei3deas.wordpress.com/
      https://www.youtube.com/@deckingman

      1 Reply Last reply Reply Quote 0
      • DaveAundefined
        DaveA @gloomyandy
        last edited by

        @gloomyandy Nope, just a single Duet Maestro with no other expansion other than a 12864 display connected.

        gloomyandyundefined 1 Reply Last reply Reply Quote 0
        • gloomyandyundefined
          gloomyandy @DaveA
          last edited by

          @davea I think @Alex-cr said that he was using an SBC, so it could be why you have not been able to reproduce the problem (the handling of conditional gcode is different when using the SBC).

          1 Reply Last reply Reply Quote 0
          • dc42undefined
            dc42 administrators @Alex.cr
            last edited by

            @alex-cr please run M122 after it resets and post the response here.

            Duet WiFi hardware designer and firmware engineer
            Please do not ask me for Duet support via PM or email, use the forum
            http://www.escher3d.com, https://miscsolutions.wordpress.com

            Alex.crundefined 1 Reply Last reply Reply Quote 0
            • Alex.crundefined
              Alex.cr @dc42
              last edited by

              @dc42

              M122 after the reset.

              m122
              === Diagnostics ===
              RepRapFirmware for Duet 3 MB6HC version 3.3beta3 (2021-04-22 16:28:03) running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode)
              Board ID: 08DJM-956L2-G43S4-6J1FD-3SJ6T-TB6QH
              Used output buffers: 1 of 40 (10 max)
              === RTOS ===
              Static ram: 149960
              Dynamic ram: 62512 of which 0 recycled
              Never used RAM 141720, free system stack 200 words
              Tasks: SENSORS(delaying,0.0%,30) Linux(ready,8.0%,58) HEAT(delaying,0.0%,281) Move(notifyWait,0.0%,150) CanReceiv(notifyWait,0.0%,798) CanSender(notifyWait,0.0%,373) CanClock(delaying,0.0%,353) TMC(notifyWait,7.0%,93) MAIN(running,83.6%,924) IDLE(ready,1.3%,19), total 100.0%
              Owned mutexes: HTTP(MAIN)
              === Platform ===
              Last reset 00:00:09 ago, cause: software
              Last software reset at 2021-04-24 16:59, reason: MemoryProtectionFault mmarValid daccViol, none spinning, available RAM 137992, slot 0
              Software reset code 0x4172 HFSR 0x00000000 CFSR 0x00000082 ICSR 0x00400004 BFAR 0x00000000 SP 0x2045ff60 Task  Freestk 46595 bad marker
              Stack: 297c0c72 297c0c2b 204326f8 00000000 00000000 0047b187 0047b19e 8100000e 00000000 20423c50 01144dd9 204248a0 00000000 20420084 00000000 20420088 01144dd9 00000004 00000001 204240b4 204240dc 004787b9 00000000 00000001 00000000 2042489c 00000000
              Error status: 0x00
              Aux0 errors 0,0,0
              Aux1 errors 0,0,0
              Step timer max interval 129
              MCU temperature: min 25.7, current 25.8, max 39.5
              Supply voltage: min 24.0, current 24.1, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
              12V rail voltage: min 12.1, current 12.2, max 12.2, under voltage events: 0
              Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
              Driver 0: position 0, standstill, reads 51264, writes 17 timeouts 0, SG min/max 0/0
              Driver 1: position 0, standstill, reads 51264, writes 17 timeouts 0, SG min/max 0/0
              Driver 2: position 0, standstill, reads 51265, writes 17 timeouts 0, SG min/max 0/0
              Driver 3: position 0, standstill, reads 51265, writes 17 timeouts 0, SG min/max 0/0
              Driver 4: position 0, standstill, reads 51265, writes 17 timeouts 0, SG min/max 0/0
              Driver 5: position 0, standstill, reads 51265, writes 17 timeouts 0, SG min/max 0/0
              Date/time: 2021-04-24 16:59:41
              Slowest loop: 0.35ms; fastest: 0.05ms
              === Storage ===
              Free file entries: 10
              SD card 0 not detected, interface speed: 37.5MBytes/sec
              SD card longest read time 0.0ms, write time 0.0ms, max retries 0
              === Move ===
              DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000
              === MainDDARing ===
              Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
              === AuxDDARing ===
              Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
              === Heat ===
              Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
              Heater 1 is on, I-accum = 0.0
              === GCodes ===
              Segments left: 0
              Movement lock held by null
              HTTP* is doing "M122" in state(s) 0
              Telnet is idle in state(s) 0
              File is idle in state(s) 0
              USB is idle in state(s) 0
              Aux is idle in state(s) 0
              Trigger* is idle in state(s) 0
              Queue is idle in state(s) 0
              LCD is idle in state(s) 0
              SBC is idle in state(s) 0
              Daemon is idle in state(s) 0
              Aux2 is idle in state(s) 0
              Autopause is idle in state(s) 0
              Code queue is empty.
              === Filament sensors ===
              Extruder 0 sensor: no data received
              === CAN ===
              Messages queued 92, send timeouts 0, received 141, lost 0, longest wait 1ms for reply type 6043, peak Tx sync delay 4, free buffers 49 (min 48)
              === SBC interface ===
              State: 4, failed transfers: 0
              Last transfer: 1ms ago
              RX/TX seq numbers: 38230/389
              SPI underruns 0, overruns 0
              Number of disconnects: 0, IAP RAM available 0x2cf4c
              Buffer RX/TX: 0/0-0
              === Duet Control Server ===
              Duet Control Server v3.3-b3
              Code buffer space: 4096
              Configured SPI speed: 8000000 Hz
              Full transfers per second: 38.29
              Codes per second: 5.51
              Maximum length of RX/TX data transfers: 3304/1492
              

              Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

              dc42undefined 1 Reply Last reply Reply Quote 0
              • dc42undefined
                dc42 administrators @Alex.cr
                last edited by

                @alex-cr thanks, Please try the new firmware binary at https://www.dropbox.com/sh/6fdfjn7fpjnk3vv/AADWZIXsKn5B_GsTauCx8Nsna?dl=0. Ignore the .map file.

                Duet WiFi hardware designer and firmware engineer
                Please do not ask me for Duet support via PM or email, use the forum
                http://www.escher3d.com, https://miscsolutions.wordpress.com

                Alex.crundefined 2 Replies Last reply Reply Quote 1
                • Alex.crundefined
                  Alex.cr @dc42
                  last edited by

                  @dc42

                  Still have the controller reset after using the improper code.

                  M122 with the +1 firmware below:

                  m122
                  === Diagnostics ===
                  RepRapFirmware for Duet 3 MB6HC version 3.3beta3+1 (2021-04-25 09:09:09) running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode)
                  Board ID: 08DJM-956L2-G43S4-6J1FD-3SJ6T-TB6QH
                  Used output buffers: 1 of 40 (10 max)
                  === RTOS ===
                  Static ram: 150760
                  Dynamic ram: 62840 of which 0 recycled
                  Never used RAM 137736, free system stack 200 words
                  Tasks: SENSORS(delaying,0.0%,80) Linux(ready,7.2%,22) HEAT(delaying,0.0%,325) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,891) CanSender(notifyWait,0.0%,373) CanClock(delaying,0.0%,353) TMC(notifyWait,7.2%,93) MAIN(running,84.6%,924) IDLE(ready,0.8%,19), total 100.0%
                  Owned mutexes: HTTP(MAIN)
                  === Platform ===
                  Last reset 00:00:14 ago, cause: software
                  Last software reset at 2021-04-25 10:40, reason: StackOverflow, none spinning, available RAM 137344, slot 1
                  Software reset code 0x4112 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0040080e BFAR 0x00000000 SP 0x2045ffbc Task � Freestk 46418 bad marker
                  Stack: 20432a18 20432a4c 0047b1b9 00000000 0049d3d4 00415495 0047a829 20432a44 20424bbc 00000000 00f00000 e000e000 c0000000 00000000 0047a945 0047a6cc 21000000 ffffffff ffffffff ffffffff ffffffff ffffffff ffffffff ffffffff ffffffff ffffffff ffffffff
                  Error status: 0x00
                  Aux0 errors 0,0,0
                  Aux1 errors 0,0,0
                  Step timer max interval 127
                  MCU temperature: min 23.3, current 23.8, max 37.1
                  Supply voltage: min 24.0, current 24.1, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                  12V rail voltage: min 12.1, current 12.2, max 12.2, under voltage events: 0
                  Heap OK, handles allocated/used 99/3, heap memory allocated/used/recyclable 2048/62/10, gc cycles 0
                  Driver 0: position 0, standstill, reads 14157, writes 17 timeouts 0, SG min/max 0/0
                  Driver 1: position 0, standstill, reads 14157, writes 17 timeouts 0, SG min/max 0/0
                  Driver 2: position 0, standstill, reads 14158, writes 17 timeouts 0, SG min/max 0/0
                  Driver 3: position 0, standstill, reads 14158, writes 17 timeouts 0, SG min/max 0/0
                  Driver 4: position 0, standstill, reads 14158, writes 17 timeouts 0, SG min/max 0/0
                  Driver 5: position 0, standstill, reads 14158, writes 17 timeouts 0, SG min/max 0/0
                  Date/time: 2021-04-25 10:40:54
                  Slowest loop: 0.44ms; fastest: 0.06ms
                  === Storage ===
                  Free file entries: 10
                  SD card 0 not detected, interface speed: 37.5MBytes/sec
                  SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                  === Move ===
                  DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                  === MainDDARing ===
                  Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                  === AuxDDARing ===
                  Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                  === Heat ===
                  Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                  Heater 1 is on, I-accum = 0.0
                  === GCodes ===
                  Segments left: 0
                  Movement lock held by null
                  HTTP* is doing "M122" in state(s) 0
                  Telnet is idle in state(s) 0
                  File is idle in state(s) 0
                  USB is idle in state(s) 0
                  Aux is idle in state(s) 0
                  Trigger* is idle in state(s) 0
                  Queue is idle in state(s) 0
                  LCD is idle in state(s) 0
                  SBC is idle in state(s) 0
                  Daemon is idle in state(s) 0
                  Aux2 is idle in state(s) 0
                  Autopause is idle in state(s) 0
                  Code queue is empty.
                  === Filament sensors ===
                  Extruder 0 sensor: no data received
                  === CAN ===
                  Messages queued 137, send timeouts 0, received 204, lost 0, longest wait 1ms for reply type 6042, peak Tx sync delay 4, free buffers 49 (min 48)
                  === SBC interface ===
                  State: 4, failed transfers: 0
                  Last transfer: 2ms ago
                  RX/TX seq numbers: 4674/575
                  SPI underruns 0, overruns 0
                  Number of disconnects: 0, IAP RAM available 0x2cc2c
                  Buffer RX/TX: 0/0-0
                  === Duet Control Server ===
                  Duet Control Server v3.3-b3
                  Code buffer space: 4096
                  Configured SPI speed: 8000000 Hz
                  Full transfers per second: 32.68
                  Codes per second: 4.28
                  Maximum length of RX/TX data transfers: 3308/988
                  

                  Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

                  1 Reply Last reply Reply Quote 0
                  • Alex.crundefined
                    Alex.cr @dc42
                    last edited by

                    @dc42

                    I am also running into a problem with variables on the SBC controlled machine. I am not super surprised as it just got implemented. Merely documenting the issue. Everything below runs fin on a D2wifi.

                    The following line in my daemon.g also cause a firmware reset:

                    set global.printcomplete = state.upTime - global.printstoptime 
                    

                    The two global variables are defined in config.g. They show up in the object model correctly. I just cannot do math with them. I can set them without issue as follows:

                    set global.printcomplete = state.upTime
                    

                    To be clear i am still using the 3.3b3+1 firmware for this as well.

                    Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

                    dc42undefined 1 Reply Last reply Reply Quote 0
                    • dc42undefined
                      dc42 administrators @Alex.cr
                      last edited by

                      @alex-cr Please post your config.g file.

                      Duet WiFi hardware designer and firmware engineer
                      Please do not ask me for Duet support via PM or email, use the forum
                      http://www.escher3d.com, https://miscsolutions.wordpress.com

                      Alex.crundefined 1 Reply Last reply Reply Quote 0
                      • Alex.crundefined
                        Alex.cr @dc42
                        last edited by Alex.cr

                        @dc42

                        As requested

                        ; Configuration file for Duet 3 (firmware version 3)
                        ; executed by the firmware on start-up
                        ;
                        ;Voron 2.4 config 350x350x350mm
                        ;Hardware: Duet3 6HC+3HC, mosquito hotend, 
                        
                        ; General preferences
                        G90                                                ; send absolute coordinates...
                        M83                                                ; ...but relative extruder moves
                        ;M550 P"Voron"                                     ; set printer name
                        M669 K1 										   ; switch to CoreXY mode
                        
                        M80										           ; turn off ATX supply for safety (and trigger button on DWC)
                        G4 S3                                              ; wait for Canbus to stabilize 
                        ; --- drive map ---
                        ;    _______
                        ;   | 3 | 4 |
                        ;   | ----- |
                        ;   | 2 | 5 |
                        ;    -------
                        ;     front
                        
                        ; Drives
                        M569 P0.0 S0                                       ; physical drive 0.0 goes forwards (A Stepper)
                        M569 P0.1 S0                                       ; physical drive 0.1 goes forwards (B Stepper)
                        M569 P0.2 S0                                       ; physical drive 0.2 goes forwards
                        M569 P0.3 S1                                       ; physical drive 0.3 goes backwards
                        M569 P0.4 S0                                       ; physical drive 0.4 goes forwards
                        M569 P0.5 S1                                       ; physical drive 0.5 goes backwards
                        M569 P1.0 S0                                       ; physical drive 1.0 goes forwards (E Stepper)
                        
                        M584 X0.1 Y0.0 Z0.2:0.3:0.4:0.5 E1.0               ; set drive mapping
                        M350 X16 Y16 Z16 E16 I1                            ; configure microstepping with interpolation
                        M92 X80.00 Y80.00 Z400.0 E417.075                   ; set steps per mm (E415 baseline BMG)
                        M906 X1200 Y1200 Z1200 E800 I50                    ; set motor currents (mA) and motor idle factor in per cent
                        M84 S120                                           ; Set idle timeout
                        
                        ; Accelerations and speed
                        M98 P"/macros/print_scripts/speed_normal.g"
                        
                        
                        ; Axis Limits
                        M208 X0 Y0 Z0 S1                                    ; set axis minima
                        M208 X350.0 Y350.0 Z330.0 S0                        ; set axis maxima
                        
                        ; Endstops
                        M574 X2 S1 P"0.io2.in"                               ; configure active-high endstop for high end on X via pin io2.in
                        M574 Y2 S1 P"0.io1.in"                               ; configure active-high endstop for high end on Y via pin io1.in
                        M574 Z1 S1 P"0.io3.in"                              			     ; 
                        
                        ; BLTouch
                        ;M950 S0 C"0.io7.out"                                 ; create servo pin 0 for BLTouch
                        ;M558 P9 C"^0.io6.in" H5 A3 S0.005 F120 T9000        ; set Z probe type to bltouch and the dive height + speeds (probe 3 times and average)
                        ;G31  P25 X0.0 Y23.23 z3.5
                        
                        ; Nozzle Height sensor
                        ;M558 P8 C"^0.io3.in" H5 A1 F120 T9000 K0             ; set Z probe type to unfiltered digital and the dive height + speeds 
                        ;G31 K0 P500 Z-4.0	
                        
                        ;NPN NO switch
                        M558 P5 C"!^0.io7.in" T18000 F600 H5 A3 S0.01 B0 R0.2 K0
                        G31 K0 P25 X0.0 Y25.0 z2.458					         ; set Z probe trigger value, offset and trigger height, 
                        M557 X25:325 Y25:325 S100                          	 ; define mesh grid
                        					  		    
                        ; Bed leveling
                        M671 X-70:-70:420:420 Y-10:460:460:-10 S20         ; Define Z belts locations (Front_Left, Back_Left, Back_Right, Front_Right)
                        
                        ; Heaters
                        ;bed heater - dual sensor config 
                        ;hex stud thermistor: https://www.amazon.com/gp/product/B07Q5MKSLS/ref=ppx_yo_dt_b_asin_title_o00_s00?ie=UTF8&psc=1
                        M308 S0 P"0.temp0" Y"thermistor" T100000 B3950 C0.0 A"Build Plate Temp" ; configure sensor 0 as thermistor on pin temp0 
                        ;Built in Keenovo sensor
                        M308 S1 P"0.temp1" Y"thermistor" T100000 B4725 C7.06e-8 A"Bed Heater Temp" ; configure sensor 0 as thermistor on pin temp1
                        M950 H0 C"0.out0" T0 Q60                                ; create bed heater output on out0 and map it to sensor 0
                        M307 H0 B0 S1.0                                   ; disable bang-bang mode for the bed heater and set PWM limit
                        ;M307 H0 R0.450 C420.1 D1.06 S1.00 
                        M307 H0 R0.153 C1735.5 D31.48 S1.00 
                        M140 H0                                            ; map heated bed to heater 0
                        M143 H0 S120                                       ; set temperature limit for build plate to 120C
                        M143 H0 T1 P1 S125 A2                             ; Monitor heater thermistor, if temp goes above 125C temporarily turn off
                        M143 H0 T1 P2 S132 A3                             ; Monitor heater thermistor, if temp goes above 132C cut "atx" supply
                        
                        
                        ;Extruder T0 heater
                        ;Slice Engineering 50W heater+ E3d PT100
                        M308 S2 P"1.spi.cs0" Y" rtd-max31865" A"T0" 	;configure sensor 2 as PT100 on SPI
                        M950 H1 C"1.out0" T2                                 ; create nozzle heater output on out1 and map it to sensor 2
                        M307 H1 B0 S1.00                                   ; disable bang-bang mode for the nozzle heater and set PWM limit
                        M307 H1 R2.995 C180.5:160.8 D2.60 S1.00 V24.1
                        M143 H1 S300                                       ; set temperature limit for heater 1 to 300C
                        
                        ;Chamber Monitors
                        ;Thermisors below: https://www.amazon.com/gp/product/B07D9LSKWK/ref=ppx_yo_dt_b_asin_title_o03_s00?ie=UTF8&psc=1
                        M308 S3 P"1.temp1" Y"thermistor" T100000 B4725 C7.06e-8 A"Chamber Upper Temp"
                        M308 S4 P"0.temp2" Y"thermistor" T100000 B4725 C7.06e-8 A"Chamber Gantry Temp"  ; configure sensor 2 as thermistor on pin temp2	
                        M308 S5 P"0.temp3" Y"thermistor" T100000 B4725 C7.06e-8 A"Z Motor4 Temp"  ; Epoxied to stepper 4	
                        M308 S10 P"0.spi.cs1" Y"dht22"       A"Chamber Lower Temp"    ; define DHT22 temperature sensor
                        M308 S11 P"S10.1"     Y"dhthumidity" A"Chamber Hum[%]"  ; Attach DHT22 humidity sensor to secondary output of temperature sensor
                        
                        
                        ;mcu calibration
                        M308 S7 Y"mcu-temp" A"MCU"                               ; configure MCU as sensor 3
                        M912 P0 S-13.6                                     ; set CPU temp correction
                        
                        
                        ; Fans/LEDs
                        ;part cooling fan
                        M950 F0 C"1.out7" Q500                             ; create fan 0 on pin out1 and set its frequency
                        M106 P0 S0 H-1 L2 C"Part fan"                                   ; set fan 0 value. Thermostatic control is turned off
                        ;main extruder heater cooling fan
                        M950 F1 C"1.out6" Q500                               ; create fan 1 on pin 20.out1 and set its frequency
                        M106 P1 S255 H2 T45 C"Extruder fan"                                 ; set fan 1 value. Thermostatic control is turned on
                        ;Electronic cooling fan
                        M950 F2 C"0.out7" Q100                              ; create fan 2 on pin out7 and set its frequency
                        ;M106 P2 S.25 H-1 C"MCU fans"
                        M106 P2 L0.25 X1 H7 T26:32 C"MCU fans"                                   ; set fan 2 value. Thermostatic control is turned on
                        ;Main LEDs
                        M950 F3 C"0.out4" Q500                               ; create fan 3 on pin out4 and set its frequency
                        M106 P3 S0 H-1 C"Lights"                                    ; set fan 3 value. Thermostatic control is turned off
                        ;Filter fan
                        M950 F4 C"1.out8" Q100                                ; create fan 4 on pin out8 and set its frequency
                        M106 P4 S0 H-1 C"Filter Fan"                                   ; set fan 4 value. Thermostatic control is turned off
                        
                        
                        ; Tools
                        M563 P0 S"Tool 0" D0 H1 F0                         ; define tool 0
                        G10 P0 X0 Y0 Z0                                    ; set tool 0 axis offsets
                        G10 P0 R0 S0                                       ; set initial tool 0 active and standby temperatures to 0C
                        M591 D0 P7 C"1.io0.in" S1 E25 L2.1 R70:130          ; create filament monitor for Tool 0
                        M572 D0 S0.00                                      ; default pressure advance for Tool 0
                        M592 D0 A0.0 B0.00 L0.2                            ; Nonlinear extrusion Tool 0
                        ;M593 F34.48                                        ; Cancel ringing
                        
                        ;Work Offsets:
                        G10L2P1 X0.0Y0.0Z0.0  ;Set G54 offset to be machine coordinates
                        G10L2P7 X230.2Y349.5Z0.0  ;use G59.1 for tool height probing Z zero is top of the setter when not pressed
                        G10L2P8 X100.0Y344.5Z5.0  ;use G59.2 for nozzle cleaning, center of brush, top of brush
                        
                        ; Motor Stall Detect
                        M915 X S10 F1 H200 R1
                        M915 Y S10 F1 H200 R1
                        M915 Z S10 F1 H200 R1
                        
                        ;global varialle delcare
                        global gantryLevel = 0
                        global printstoptime = 0
                        global printcomplete = 0
                        global holdtime = 0
                        
                        
                        ; Miscellaneous
                        M115
                        M115 B1										   ;Check status of Can-FD exansion board
                        M911 S19 R22 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
                        M207 S0.4 R0.0 F3600 T3600 Z1.0                    ; set default retraction settings
                        
                        G54
                        T0                                                 ; select first tool
                        ;G31 K0 												;select Bltouch by default
                        M106 P3 S255 									   ; turn on lights
                        ;M564 H0 S0; Allow movement outside of max/min and allow movment without homing
                        
                        ;Random Notes---------------------------------------------------------------------------------------------------------------------
                        ;wget -q https://pkg.duet3d.com/duet3d.gpg
                        ;wget -q https://pkg.duet3d.com/duet3d-unstable.list
                        ;sudo mv duet3d.gpg /etc/apt/trusted.gpg.d/
                        ;sudo mv duet3d-unstable.list /etc/apt/sources.list.d/duet3d-unstable.list
                        ;sudo chown root:root /etc/apt/trusted.gpg.d/duet3d.gpg
                        ;sudo chown root:root /etc/apt/sources.list.d/duet3d-unstable.list
                        ;sudo rm /etc/apt/sources.list.d/duet3d.list
                        ;sudo apt-get update
                        ;sudo apt-get upgrade
                        ;(may need: sudo apt-get dist-upgrade) 
                        
                        ;Webcam
                        ;https://forum.duet3d.com/topic/13604/duet-3-raspberry-pi-camera/6
                        ;full interface http://voron.local:8080/
                        ;minimal interface http://voron.local:8080/html/min.php
                        
                        ;accelerometer setup
                        ;adafruit lis3dh 
                        ;SDI (MOSI) is SDA(on board)
                        ;SPI.cs3 is CS
                        ;SPI.cs2 is INT
                        
                        ;M955 P0 C"spi.cs2+spi.cs3"
                        
                        

                        Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

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                        • dc42undefined
                          dc42 administrators @Alex.cr
                          last edited by dc42

                          @alex-cr thanks. I've updated the firmware binary at https://www.dropbox.com/sh/6fdfjn7fpjnk3vv/AADWZIXsKn5B_GsTauCx8Nsna?dl=0. Please try that one. Whether your daemon.g file succeeds or crashes, please post a new M122 report after running it.

                          Duet WiFi hardware designer and firmware engineer
                          Please do not ask me for Duet support via PM or email, use the forum
                          http://www.escher3d.com, https://miscsolutions.wordpress.com

                          Alex.crundefined pkosundefined 2 Replies Last reply Reply Quote 0
                          • Alex.crundefined
                            Alex.cr @dc42
                            last edited by

                            @dc42

                            Good news, the latest +1 appears to have fixed the firmware crashes.
                            Unfortunately the line in deamon.g that was causing the crash is now throwing the following alarm.

                            ; daemon.g
                            
                            set global.holdtime = state.upTime
                            set global.printcomplete = state.upTime - global.printstoptime 
                            

                            Screenshot 2021-04-25 204953.jpg

                            The global variable "printstoptime" is fully defined according to the object model.

                            And as requested here is the M122.

                            m122
                            === Diagnostics ===
                            RepRapFirmware for Duet 3 MB6HC version 3.3beta3+1 (2021-04-25 21:40:09) running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode)
                            Board ID: 08DJM-956L2-G43S4-6J1FD-3SJ6T-TB6QH
                            Used output buffers: 1 of 40 (10 max)
                            === RTOS ===
                            Static ram: 150800
                            Dynamic ram: 64488 of which 176 recycled
                            Never used RAM 135872, free system stack 178 words
                            Tasks: SENSORS(delaying,0.0%,70) Linux(resourceWait:,5.7%,266) HEAT(delaying,0.0%,281) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,773) CanSender(notifyWait,0.0%,373) CanClock(delaying,0.0%,341) TMC(notifyWait,7.2%,93) MAIN(running,87.0%,924) IDLE(ready,0.0%,29), total 100.0%
                            Owned mutexes: HTTP(MAIN)
                            === Platform ===
                            Last reset 00:10:34 ago, cause: software
                            Last software reset at 2021-04-25 20:42, reason: User, none spinning, available RAM 135872, slot 0
                            Software reset code 0x0012 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0x00000000 Task Linu Freestk 0 n/a
                            Error status: 0x00
                            Aux0 errors 0,0,0
                            Aux1 errors 0,0,0
                            Step timer max interval 134
                            MCU temperature: min 24.9, current 25.5, max 39.7
                            Supply voltage: min 3.1, current 24.0, max 24.1, under voltage events: 1, over voltage events: 0, power good: yes
                            12V rail voltage: min 0.4, current 12.2, max 12.2, under voltage events: 0
                            Heap OK, handles allocated/used 99/4, heap memory allocated/used/recyclable 2048/64/0, gc cycles 0
                            Driver 0: position 0, standstill, reads 58281, writes 28 timeouts 0, SG min/max 0/0
                            Driver 1: position 0, standstill, reads 58281, writes 28 timeouts 0, SG min/max 0/0
                            Driver 2: position 0, standstill, reads 58281, writes 28 timeouts 0, SG min/max 0/0
                            Driver 3: position 0, standstill, reads 58281, writes 28 timeouts 0, SG min/max 0/0
                            Driver 4: position 0, standstill, reads 58281, writes 28 timeouts 0, SG min/max 0/0
                            Driver 5: position 0, standstill, reads 58282, writes 28 timeouts 0, SG min/max 0/0
                            Date/time: 2021-04-25 20:53:14
                            Slowest loop: 0.68ms; fastest: 0.04ms
                            === Storage ===
                            Free file entries: 10
                            SD card 0 not detected, interface speed: 37.5MBytes/sec
                            SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                            === Move ===
                            DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                            === MainDDARing ===
                            Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                            === AuxDDARing ===
                            Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                            === Heat ===
                            Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                            Heater 1 is on, I-accum = 0.0
                            === GCodes ===
                            Segments left: 0
                            Movement lock held by null
                            HTTP* is doing "M122" in state(s) 0
                            Telnet is idle in state(s) 0
                            File is idle in state(s) 0
                            USB is idle in state(s) 0
                            Aux is idle in state(s) 0
                            Trigger* is idle in state(s) 0
                            Queue is idle in state(s) 0
                            LCD is idle in state(s) 0
                            SBC is idle in state(s) 0
                            Daemon is idle in state(s) 0
                            Aux2 is idle in state(s) 0
                            Autopause is idle in state(s) 0
                            Code queue is empty.
                            === Filament sensors ===
                            Extruder 0 sensor: no data received
                            === CAN ===
                            Messages queued 5699, send timeouts 15, received 7849, lost 0, longest wait 1ms for reply type 6042, peak Tx sync delay 45775, free buffers 49 (min 48)
                            Last cancelled message type 30 dest 127
                            === SBC interface ===
                            State: 4, failed transfers: 0
                            Last transfer: 1ms ago
                            RX/TX seq numbers: 23043/23043
                            SPI underruns 0, overruns 0
                            Number of disconnects: 0, IAP RAM available 0x2c594
                            Buffer RX/TX: 0/0-0
                            === Duet Control Server ===
                            Duet Control Server v3.3-b3
                            Code buffer space: 4096
                            Configured SPI speed: 8000000 Hz
                            Full transfers per second: 36.43
                            Codes per second: 0.15
                            Maximum length of RX/TX data transfers: 5740/936
                            

                            Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

                            dc42undefined 1 Reply Last reply Reply Quote 0
                            • dc42undefined
                              dc42 administrators @Alex.cr
                              last edited by dc42

                              @alex-cr thanks. As you are using SBC I'll ask @chrishamm to look at why the global variable isn't found.

                              Duet WiFi hardware designer and firmware engineer
                              Please do not ask me for Duet support via PM or email, use the forum
                              http://www.escher3d.com, https://miscsolutions.wordpress.com

                              Alex.crundefined 1 Reply Last reply Reply Quote 0
                              • Alex.crundefined
                                Alex.cr @dc42
                                last edited by

                                @dc42

                                Not a problem. Just doing my best to beta test!

                                Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

                                chrishammundefined 1 Reply Last reply Reply Quote 0
                                • chrishammundefined
                                  chrishamm administrators @Alex.cr
                                  last edited by

                                  @alex-cr This problem had to do with the space after the variable name. To work-around this problem you can remove spaces before the '=' from your daemon.g.

                                  I've got a fix ready for this, thanks for your report.

                                  Duet software engineer

                                  1 Reply Last reply Reply Quote 0
                                  • tristanryerparkeundefined
                                    tristanryerparke
                                    last edited by tristanryerparke

                                    Hey @dc42 I installed the firmware you linked to as I was having the same issue as the OP, I'm running MB6HC with SBC. It solved some issues but others came up. I thought that possibly these new issues were related to my TOOL1LC and 2x EXP3HC being not on the "dropbox" firmware too, so I uploaded and installed those versions with M997. The installations took an abnormally long time to complete.
                                    After installing I am unable to communicate with any of the expansion boards and they all flash with this pattern:
                                    3s Pause, three flashes, 1s pause, very fast single flash, 3s pause, four flashes, repeated.
                                    I tried to downgrade the firmwares back to 3.3beta1 from the github, but am unable to communicate with the boards. "Response Timeout" from M997. I tried the reset procedures but the issue persisted. M112 B{tried for all three boards} gave the same Response Timeout error.
                                    All boards appear in the object model browser but list "null" for all values except CAN address.
                                    I can document the issue further when I am with the machine tomorrow, and or create a new thread if you think that would be better.
                                    Cheers,
                                    T

                                    dc42undefined 1 Reply Last reply Reply Quote 0
                                    • dc42undefined
                                      dc42 administrators @tristanryerparke
                                      last edited by dc42

                                      @tristanryerparke said in 3.3B3 certain lines cause firmware reset:

                                      After installing I am unable to communicate with any of the expansion boards and they all flash with this pattern:
                                      3s Pause, three flashes, 1s pause, very fast single flash, 3s pause, four flashes, repeated.

                                      That indicates that the boards are trying to download firmware from the main board, but the main board doesn't have it in the right place. Most likely the firmware files are in the /sys folder on the SD card but not in the /firmware folder which is where the main board will look for them when running 3.3beta3.

                                      Check that you are running Duet Web Control 3.3beta, then upload the tool board and expansion board firmware files again.

                                      Duet WiFi hardware designer and firmware engineer
                                      Please do not ask me for Duet support via PM or email, use the forum
                                      http://www.escher3d.com, https://miscsolutions.wordpress.com

                                      tristanryerparkeundefined 1 Reply Last reply Reply Quote 0
                                      • tristanryerparkeundefined
                                        tristanryerparke @dc42
                                        last edited by

                                        @dc42 Files were in /firmware and /sys which was why I was really worried originally. Seemed to be a problem with boards retrieving firmware from the Pi4 SD card. I solved the issue by going into standalone mode and restarting the machine. Then the boards were able to request firmware and sync.
                                        All set now,
                                        Thanks

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                                        • pkosundefined
                                          pkos @dc42
                                          last edited by

                                          @dc42 I seem to be having a similar issue.

                                          I downloaded the 3HC and 6HC files from dropbox, uploaded it to the board.

                                          I'm trying to get the accelerometer to work with the printer, so what I did was this:

                                          1. Home
                                          2. Level gantry (Voron 2.4)
                                          3. Send m955 to set up the accelerometer (the response seems to ignore I10 I am sending and keeps reporting orientation 20).
                                          4. Set movement to relative with G91
                                          5. Trigger the command from the docs with:
                                          G1 X-50 G4 S2 M956 P0.0 S5000 A0 G4 P10 G1 X50 F20000
                                          
                                          1. Printer moves by -50, then resets. This happens every time now. It doesn't matter if I have the accelerometer hooked up via SPI or i2c. Always happens.

                                          M122 from after the board boots up is as follows:

                                          m122 b0
                                          === Diagnostics ===
                                          RepRapFirmware for Duet 3 MB6HC version 3.3RC1 (2021-05-01 09:12:50) running on Duet 3 MB6HC v0.6 or 1.0 (standalone mode)
                                          Board ID: 08DJM-956L2-G43S4-6JKDA-3SJ6T-1B6GH
                                          Used output buffers: 3 of 40 (19 max)
                                          === RTOS ===
                                          Static ram: 150680
                                          Dynamic ram: 92772 of which 116 recycled
                                          Never used RAM 107768, free system stack 200 words
                                          Tasks: NETWORK(ready,15.7%,218) ETHERNET(notifyWait,0.1%,117) HEAT(delaying,0.0%,345) Move(notifyWait,0.0%,352) CanReceiv(notifyWait,0.0%,911) CanSender(notifyWait,0.0%,373) CanClock(delaying,0.0%,350) TMC(notifyWait,7.2%,93) MAIN(running,76.1%,924) IDLE(ready,0.9%,29), total 100.0%
                                          Owned mutexes: HTTP(MAIN)
                                          === Platform ===
                                          Last reset 00:00:12 ago, cause: software
                                          Last software reset at 2021-05-01 12:14, reason: HeatTaskStuck, Platform spinning, available RAM 105784, slot 2
                                          Software reset code 0x4140 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0040080f BFAR 0x00000000 SP 0x2043be24 Task ACCE Freestk 334 ok
                                          Stack: 00448065 0044805a 610f0000 00000000 407ad03f b5fbe847 bf6d6ea8 00000000 42e80000 f81d6400 3f5cc44b 15873197 3ec9dc39 37533333 43d697a0 00000000 422ba3c7 42288192 00000000 60000010 2043b7c1 2043b7a0 2043b7c1 000000e8 000000ef 00000003 20423f00
                                          Error status: 0x00
                                          Aux0 errors 0,0,0
                                          Aux1 errors 0,0,0
                                          Step timer max interval 133
                                          MCU temperature: min 41.7, current 42.6, max 42.8
                                          Supply voltage: min 24.0, current 24.0, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                                          12V rail voltage: min 12.1, current 12.1, max 12.2, under voltage events: 0
                                          Heap OK, handles allocated/used 99/2, heap memory allocated/used/recyclable 2048/26/0, gc cycles 0
                                          Driver 0: position 0, standstill, reads 1504, writes 14 timeouts 0, SG min/max 0/0
                                          Driver 1: position 0, standstill, reads 1504, writes 14 timeouts 0, SG min/max 0/0
                                          Driver 2: position 0, standstill, reads 1505, writes 14 timeouts 0, SG min/max 0/0
                                          Driver 3: position 0, standstill, reads 1505, writes 14 timeouts 0, SG min/max 0/0
                                          Driver 4: position 0, standstill, reads 1505, writes 14 timeouts 0, SG min/max 0/0
                                          Driver 5: position 0, standstill, reads 1505, writes 14 timeouts 0, SG min/max 0/0
                                          Date/time: 2021-05-01 12:15:23
                                          Slowest loop: 5.60ms; fastest: 0.05ms
                                          === Storage ===
                                          Free file entries: 10
                                          SD card 0 detected, interface speed: 25.0MBytes/sec
                                          SD card longest read time 3.4ms, write time 0.0ms, max retries 0
                                          === Move ===
                                          DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                                          === MainDDARing ===
                                          Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                          === AuxDDARing ===
                                          Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                          === Heat ===
                                          Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                          === GCodes ===
                                          Segments left: 0
                                          Movement lock held by null
                                          HTTP is ready with "m122 b0" in state(s) 0
                                          Telnet is idle in state(s) 0
                                          File is idle in state(s) 0
                                          USB is idle in state(s) 0
                                          Aux is idle in state(s) 0
                                          Trigger is idle in state(s) 0
                                          Queue is idle in state(s) 0
                                          LCD is idle in state(s) 0
                                          SBC is idle in state(s) 0
                                          Daemon is idle in state(s) 0
                                          Aux2 is idle in state(s) 0
                                          Autopause is idle in state(s) 0
                                          Code queue is empty.
                                          === CAN ===
                                          Messages queued 97, send timeouts 0, received 57, lost 0, longest wait 1ms for reply type 6042, peak Tx sync delay 206, free buffers 49 (min 48)
                                          === Network ===
                                          Slowest loop: 9.48ms; fastest: 0.02ms
                                          Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions
                                          HTTP sessions: 2 of 8
                                          - Ethernet -
                                          State: active
                                          Error counts: 0 0 1 0 0
                                          Socket states: 5 2 2 2 2 0 0 0
                                          

                                          Voron 2.4 (Duet 3 6HC + 3HC standalone), Voron SW (Duet 3 mini 5+ standalone), Voron Trident (Duet 3 mini 5+ standalone), Voron 0.1

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                                          • dc42undefined
                                            dc42 administrators @pkos
                                            last edited by

                                            We hope to release 3.3RC1 later today. It includes fixes for these stack overflow issues.

                                            Duet WiFi hardware designer and firmware engineer
                                            Please do not ask me for Duet support via PM or email, use the forum
                                            http://www.escher3d.com, https://miscsolutions.wordpress.com

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