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3.3B3 certain lines cause firmware reset

Scheduled Pinned Locked Moved
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  • undefined
    Alex.cr
    last edited by Alex.cr 24 Apr 2021, 13:25

    Potential bug report for 3.3B3.
    Running 3.3B3 on 6HC+3HC+SBC.
    The following lines in a macro will cause the firmware to reset as if M999 was called.

    if move.axes.0.machinePosition != 0 | move.axes.1.machinePosition != 0
    G91
    G1 Z10.0 F20000

    If I comment out these lines the macro runs no problem.

    I believe this is similar problem to what @deckingman mentioned in the main 3.3B3 release thread.

    If there is anything else you would like me to try, let me know.

    Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

    undefined undefined 2 Replies Last reply 24 Apr 2021, 13:43 Reply Quote 1
    • undefined
      DaveA @Alex.cr
      last edited by 24 Apr 2021, 13:43

      @alex-cr I'm just getting used to working with the object model so I may be out or order but I think the lines should be:

      if move.axes[0].machinePosition != 0 | move.axes[1].machinePosition != 0
      G91
      G1 Z10.0 F20000

      The object "axes" is an array so you need to use an array index to access the elements.

      undefined 1 Reply Last reply 24 Apr 2021, 15:01 Reply Quote 0
      • undefined
        Alex.cr @DaveA
        last edited by Alex.cr 24 Apr 2021, 15:01

        @davea

        Nice catch @DaveA! That fixed it.

        I guess now the only question is to whether that type of failure is supposed to trigger a firmware reset.

        Anyone have any ideas?

        Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

        undefined 1 Reply Last reply 24 Apr 2021, 15:12 Reply Quote 0
        • undefined
          DaveA @Alex.cr
          last edited by 24 Apr 2021, 15:12

          @alex-cr Maybe it's something in the greater context. If I create a macro using just the original 3 lines and run it I just get an error message but no reset.
          This is on a cartesian with Duet Maestro and 3.3b3. My delta with a Duet2 Ethernet is printing so I'm not going to try it right now.

          undefined 1 Reply Last reply 24 Apr 2021, 15:46 Reply Quote 0
          • undefined
            gloomyandy @DaveA
            last edited by 24 Apr 2021, 15:46

            @davea Are you running SBC? It could be a RRF/DSF difference?

            undefined 1 Reply Last reply 24 Apr 2021, 16:55 Reply Quote 0
            • undefined
              deckingman
              last edited by 24 Apr 2021, 16:37

              As my name was mentioned, the fault I'm experiencing is consistent in that reverting back to RRF3.2 fixes in and "upgrading to 3.3. causes it. I've repeated this a few times. There appears to be a reset of the main board (but not the expansion boards) which is bought about by running a macro which uses M116 to wait for heaters to attain their set temperatures. In my case, no conditional gcode is used in this particular macro and the machine is in stand alone mode (no SBC) running a 6HC main board and 3 expansion boards. So maybe a different fault to the OP.

              Ian
              https://somei3deas.wordpress.com/
              https://www.youtube.com/@deckingman

              1 Reply Last reply Reply Quote 0
              • undefined
                DaveA @gloomyandy
                last edited by 24 Apr 2021, 16:55

                @gloomyandy Nope, just a single Duet Maestro with no other expansion other than a 12864 display connected.

                undefined 1 Reply Last reply 24 Apr 2021, 19:56 Reply Quote 0
                • undefined
                  gloomyandy @DaveA
                  last edited by 24 Apr 2021, 19:56

                  @davea I think @Alex-cr said that he was using an SBC, so it could be why you have not been able to reproduce the problem (the handling of conditional gcode is different when using the SBC).

                  1 Reply Last reply Reply Quote 0
                  • undefined
                    dc42 administrators @Alex.cr
                    last edited by 24 Apr 2021, 20:36

                    @alex-cr please run M122 after it resets and post the response here.

                    Duet WiFi hardware designer and firmware engineer
                    Please do not ask me for Duet support via PM or email, use the forum
                    http://www.escher3d.com, https://miscsolutions.wordpress.com

                    undefined 1 Reply Last reply 24 Apr 2021, 21:00 Reply Quote 0
                    • undefined
                      Alex.cr @dc42
                      last edited by 24 Apr 2021, 21:00

                      @dc42

                      M122 after the reset.

                      m122
                      === Diagnostics ===
                      RepRapFirmware for Duet 3 MB6HC version 3.3beta3 (2021-04-22 16:28:03) running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode)
                      Board ID: 08DJM-956L2-G43S4-6J1FD-3SJ6T-TB6QH
                      Used output buffers: 1 of 40 (10 max)
                      === RTOS ===
                      Static ram: 149960
                      Dynamic ram: 62512 of which 0 recycled
                      Never used RAM 141720, free system stack 200 words
                      Tasks: SENSORS(delaying,0.0%,30) Linux(ready,8.0%,58) HEAT(delaying,0.0%,281) Move(notifyWait,0.0%,150) CanReceiv(notifyWait,0.0%,798) CanSender(notifyWait,0.0%,373) CanClock(delaying,0.0%,353) TMC(notifyWait,7.0%,93) MAIN(running,83.6%,924) IDLE(ready,1.3%,19), total 100.0%
                      Owned mutexes: HTTP(MAIN)
                      === Platform ===
                      Last reset 00:00:09 ago, cause: software
                      Last software reset at 2021-04-24 16:59, reason: MemoryProtectionFault mmarValid daccViol, none spinning, available RAM 137992, slot 0
                      Software reset code 0x4172 HFSR 0x00000000 CFSR 0x00000082 ICSR 0x00400004 BFAR 0x00000000 SP 0x2045ff60 Task Freestk 46595 bad marker
                      Stack: 297c0c72 297c0c2b 204326f8 00000000 00000000 0047b187 0047b19e 8100000e 00000000 20423c50 01144dd9 204248a0 00000000 20420084 00000000 20420088 01144dd9 00000004 00000001 204240b4 204240dc 004787b9 00000000 00000001 00000000 2042489c 00000000
                      Error status: 0x00
                      Aux0 errors 0,0,0
                      Aux1 errors 0,0,0
                      Step timer max interval 129
                      MCU temperature: min 25.7, current 25.8, max 39.5
                      Supply voltage: min 24.0, current 24.1, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                      12V rail voltage: min 12.1, current 12.2, max 12.2, under voltage events: 0
                      Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
                      Driver 0: position 0, standstill, reads 51264, writes 17 timeouts 0, SG min/max 0/0
                      Driver 1: position 0, standstill, reads 51264, writes 17 timeouts 0, SG min/max 0/0
                      Driver 2: position 0, standstill, reads 51265, writes 17 timeouts 0, SG min/max 0/0
                      Driver 3: position 0, standstill, reads 51265, writes 17 timeouts 0, SG min/max 0/0
                      Driver 4: position 0, standstill, reads 51265, writes 17 timeouts 0, SG min/max 0/0
                      Driver 5: position 0, standstill, reads 51265, writes 17 timeouts 0, SG min/max 0/0
                      Date/time: 2021-04-24 16:59:41
                      Slowest loop: 0.35ms; fastest: 0.05ms
                      === Storage ===
                      Free file entries: 10
                      SD card 0 not detected, interface speed: 37.5MBytes/sec
                      SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                      === Move ===
                      DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                      === MainDDARing ===
                      Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                      === AuxDDARing ===
                      Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                      === Heat ===
                      Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                      Heater 1 is on, I-accum = 0.0
                      === GCodes ===
                      Segments left: 0
                      Movement lock held by null
                      HTTP* is doing "M122" in state(s) 0
                      Telnet is idle in state(s) 0
                      File is idle in state(s) 0
                      USB is idle in state(s) 0
                      Aux is idle in state(s) 0
                      Trigger* is idle in state(s) 0
                      Queue is idle in state(s) 0
                      LCD is idle in state(s) 0
                      SBC is idle in state(s) 0
                      Daemon is idle in state(s) 0
                      Aux2 is idle in state(s) 0
                      Autopause is idle in state(s) 0
                      Code queue is empty.
                      === Filament sensors ===
                      Extruder 0 sensor: no data received
                      === CAN ===
                      Messages queued 92, send timeouts 0, received 141, lost 0, longest wait 1ms for reply type 6043, peak Tx sync delay 4, free buffers 49 (min 48)
                      === SBC interface ===
                      State: 4, failed transfers: 0
                      Last transfer: 1ms ago
                      RX/TX seq numbers: 38230/389
                      SPI underruns 0, overruns 0
                      Number of disconnects: 0, IAP RAM available 0x2cf4c
                      Buffer RX/TX: 0/0-0
                      === Duet Control Server ===
                      Duet Control Server v3.3-b3
                      Code buffer space: 4096
                      Configured SPI speed: 8000000 Hz
                      Full transfers per second: 38.29
                      Codes per second: 5.51
                      Maximum length of RX/TX data transfers: 3304/1492

                      Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

                      undefined 1 Reply Last reply 25 Apr 2021, 08:09 Reply Quote 0
                      • undefined
                        dc42 administrators @Alex.cr
                        last edited by 25 Apr 2021, 08:09

                        @alex-cr thanks, Please try the new firmware binary at https://www.dropbox.com/sh/6fdfjn7fpjnk3vv/AADWZIXsKn5B_GsTauCx8Nsna?dl=0. Ignore the .map file.

                        Duet WiFi hardware designer and firmware engineer
                        Please do not ask me for Duet support via PM or email, use the forum
                        http://www.escher3d.com, https://miscsolutions.wordpress.com

                        undefined 2 Replies Last reply 25 Apr 2021, 14:41 Reply Quote 1
                        • undefined
                          Alex.cr @dc42
                          last edited by 25 Apr 2021, 14:41

                          @dc42

                          Still have the controller reset after using the improper code.

                          M122 with the +1 firmware below:

                          m122
                          === Diagnostics ===
                          RepRapFirmware for Duet 3 MB6HC version 3.3beta3+1 (2021-04-25 09:09:09) running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode)
                          Board ID: 08DJM-956L2-G43S4-6J1FD-3SJ6T-TB6QH
                          Used output buffers: 1 of 40 (10 max)
                          === RTOS ===
                          Static ram: 150760
                          Dynamic ram: 62840 of which 0 recycled
                          Never used RAM 137736, free system stack 200 words
                          Tasks: SENSORS(delaying,0.0%,80) Linux(ready,7.2%,22) HEAT(delaying,0.0%,325) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,891) CanSender(notifyWait,0.0%,373) CanClock(delaying,0.0%,353) TMC(notifyWait,7.2%,93) MAIN(running,84.6%,924) IDLE(ready,0.8%,19), total 100.0%
                          Owned mutexes: HTTP(MAIN)
                          === Platform ===
                          Last reset 00:00:14 ago, cause: software
                          Last software reset at 2021-04-25 10:40, reason: StackOverflow, none spinning, available RAM 137344, slot 1
                          Software reset code 0x4112 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0040080e BFAR 0x00000000 SP 0x2045ffbc Task � Freestk 46418 bad marker
                          Stack: 20432a18 20432a4c 0047b1b9 00000000 0049d3d4 00415495 0047a829 20432a44 20424bbc 00000000 00f00000 e000e000 c0000000 00000000 0047a945 0047a6cc 21000000 ffffffff ffffffff ffffffff ffffffff ffffffff ffffffff ffffffff ffffffff ffffffff ffffffff
                          Error status: 0x00
                          Aux0 errors 0,0,0
                          Aux1 errors 0,0,0
                          Step timer max interval 127
                          MCU temperature: min 23.3, current 23.8, max 37.1
                          Supply voltage: min 24.0, current 24.1, max 24.1, under voltage events: 0, over voltage events: 0, power good: yes
                          12V rail voltage: min 12.1, current 12.2, max 12.2, under voltage events: 0
                          Heap OK, handles allocated/used 99/3, heap memory allocated/used/recyclable 2048/62/10, gc cycles 0
                          Driver 0: position 0, standstill, reads 14157, writes 17 timeouts 0, SG min/max 0/0
                          Driver 1: position 0, standstill, reads 14157, writes 17 timeouts 0, SG min/max 0/0
                          Driver 2: position 0, standstill, reads 14158, writes 17 timeouts 0, SG min/max 0/0
                          Driver 3: position 0, standstill, reads 14158, writes 17 timeouts 0, SG min/max 0/0
                          Driver 4: position 0, standstill, reads 14158, writes 17 timeouts 0, SG min/max 0/0
                          Driver 5: position 0, standstill, reads 14158, writes 17 timeouts 0, SG min/max 0/0
                          Date/time: 2021-04-25 10:40:54
                          Slowest loop: 0.44ms; fastest: 0.06ms
                          === Storage ===
                          Free file entries: 10
                          SD card 0 not detected, interface speed: 37.5MBytes/sec
                          SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                          === Move ===
                          DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                          === MainDDARing ===
                          Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                          === AuxDDARing ===
                          Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                          === Heat ===
                          Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                          Heater 1 is on, I-accum = 0.0
                          === GCodes ===
                          Segments left: 0
                          Movement lock held by null
                          HTTP* is doing "M122" in state(s) 0
                          Telnet is idle in state(s) 0
                          File is idle in state(s) 0
                          USB is idle in state(s) 0
                          Aux is idle in state(s) 0
                          Trigger* is idle in state(s) 0
                          Queue is idle in state(s) 0
                          LCD is idle in state(s) 0
                          SBC is idle in state(s) 0
                          Daemon is idle in state(s) 0
                          Aux2 is idle in state(s) 0
                          Autopause is idle in state(s) 0
                          Code queue is empty.
                          === Filament sensors ===
                          Extruder 0 sensor: no data received
                          === CAN ===
                          Messages queued 137, send timeouts 0, received 204, lost 0, longest wait 1ms for reply type 6042, peak Tx sync delay 4, free buffers 49 (min 48)
                          === SBC interface ===
                          State: 4, failed transfers: 0
                          Last transfer: 2ms ago
                          RX/TX seq numbers: 4674/575
                          SPI underruns 0, overruns 0
                          Number of disconnects: 0, IAP RAM available 0x2cc2c
                          Buffer RX/TX: 0/0-0
                          === Duet Control Server ===
                          Duet Control Server v3.3-b3
                          Code buffer space: 4096
                          Configured SPI speed: 8000000 Hz
                          Full transfers per second: 32.68
                          Codes per second: 4.28
                          Maximum length of RX/TX data transfers: 3308/988

                          Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

                          1 Reply Last reply Reply Quote 0
                          • undefined
                            Alex.cr @dc42
                            last edited by 25 Apr 2021, 15:37

                            @dc42

                            I am also running into a problem with variables on the SBC controlled machine. I am not super surprised as it just got implemented. Merely documenting the issue. Everything below runs fin on a D2wifi.

                            The following line in my daemon.g also cause a firmware reset:

                            set global.printcomplete = state.upTime - global.printstoptime

                            The two global variables are defined in config.g. They show up in the object model correctly. I just cannot do math with them. I can set them without issue as follows:

                            set global.printcomplete = state.upTime

                            To be clear i am still using the 3.3b3+1 firmware for this as well.

                            Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

                            undefined 1 Reply Last reply 25 Apr 2021, 18:12 Reply Quote 0
                            • undefined
                              dc42 administrators @Alex.cr
                              last edited by 25 Apr 2021, 18:12

                              @alex-cr Please post your config.g file.

                              Duet WiFi hardware designer and firmware engineer
                              Please do not ask me for Duet support via PM or email, use the forum
                              http://www.escher3d.com, https://miscsolutions.wordpress.com

                              undefined 1 Reply Last reply 25 Apr 2021, 18:15 Reply Quote 0
                              • undefined
                                Alex.cr @dc42
                                last edited by Alex.cr 25 Apr 2021, 18:15

                                @dc42

                                As requested

                                ; Configuration file for Duet 3 (firmware version 3)
                                ; executed by the firmware on start-up
                                ;
                                ;Voron 2.4 config 350x350x350mm
                                ;Hardware: Duet3 6HC+3HC, mosquito hotend,
                                ; General preferences
                                G90 ; send absolute coordinates...
                                M83 ; ...but relative extruder moves
                                ;M550 P"Voron" ; set printer name
                                M669 K1 ; switch to CoreXY mode
                                M80 ; turn off ATX supply for safety (and trigger button on DWC)
                                G4 S3 ; wait for Canbus to stabilize
                                ; --- drive map ---
                                ; _______
                                ; | 3 | 4 |
                                ; | ----- |
                                ; | 2 | 5 |
                                ; -------
                                ; front
                                ; Drives
                                M569 P0.0 S0 ; physical drive 0.0 goes forwards (A Stepper)
                                M569 P0.1 S0 ; physical drive 0.1 goes forwards (B Stepper)
                                M569 P0.2 S0 ; physical drive 0.2 goes forwards
                                M569 P0.3 S1 ; physical drive 0.3 goes backwards
                                M569 P0.4 S0 ; physical drive 0.4 goes forwards
                                M569 P0.5 S1 ; physical drive 0.5 goes backwards
                                M569 P1.0 S0 ; physical drive 1.0 goes forwards (E Stepper)
                                M584 X0.1 Y0.0 Z0.2:0.3:0.4:0.5 E1.0 ; set drive mapping
                                M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
                                M92 X80.00 Y80.00 Z400.0 E417.075 ; set steps per mm (E415 baseline BMG)
                                M906 X1200 Y1200 Z1200 E800 I50 ; set motor currents (mA) and motor idle factor in per cent
                                M84 S120 ; Set idle timeout
                                ; Accelerations and speed
                                M98 P"/macros/print_scripts/speed_normal.g"
                                ; Axis Limits
                                M208 X0 Y0 Z0 S1 ; set axis minima
                                M208 X350.0 Y350.0 Z330.0 S0 ; set axis maxima
                                ; Endstops
                                M574 X2 S1 P"0.io2.in" ; configure active-high endstop for high end on X via pin io2.in
                                M574 Y2 S1 P"0.io1.in" ; configure active-high endstop for high end on Y via pin io1.in
                                M574 Z1 S1 P"0.io3.in" ;
                                ; BLTouch
                                ;M950 S0 C"0.io7.out" ; create servo pin 0 for BLTouch
                                ;M558 P9 C"^0.io6.in" H5 A3 S0.005 F120 T9000 ; set Z probe type to bltouch and the dive height + speeds (probe 3 times and average)
                                ;G31 P25 X0.0 Y23.23 z3.5
                                ; Nozzle Height sensor
                                ;M558 P8 C"^0.io3.in" H5 A1 F120 T9000 K0 ; set Z probe type to unfiltered digital and the dive height + speeds
                                ;G31 K0 P500 Z-4.0
                                ;NPN NO switch
                                M558 P5 C"!^0.io7.in" T18000 F600 H5 A3 S0.01 B0 R0.2 K0
                                G31 K0 P25 X0.0 Y25.0 z2.458 ; set Z probe trigger value, offset and trigger height,
                                M557 X25:325 Y25:325 S100 ; define mesh grid
                                ; Bed leveling
                                M671 X-70:-70:420:420 Y-10:460:460:-10 S20 ; Define Z belts locations (Front_Left, Back_Left, Back_Right, Front_Right)
                                ; Heaters
                                ;bed heater - dual sensor config
                                ;hex stud thermistor: https://www.amazon.com/gp/product/B07Q5MKSLS/ref=ppx_yo_dt_b_asin_title_o00_s00?ie=UTF8&psc=1
                                M308 S0 P"0.temp0" Y"thermistor" T100000 B3950 C0.0 A"Build Plate Temp" ; configure sensor 0 as thermistor on pin temp0
                                ;Built in Keenovo sensor
                                M308 S1 P"0.temp1" Y"thermistor" T100000 B4725 C7.06e-8 A"Bed Heater Temp" ; configure sensor 0 as thermistor on pin temp1
                                M950 H0 C"0.out0" T0 Q60 ; create bed heater output on out0 and map it to sensor 0
                                M307 H0 B0 S1.0 ; disable bang-bang mode for the bed heater and set PWM limit
                                ;M307 H0 R0.450 C420.1 D1.06 S1.00
                                M307 H0 R0.153 C1735.5 D31.48 S1.00
                                M140 H0 ; map heated bed to heater 0
                                M143 H0 S120 ; set temperature limit for build plate to 120C
                                M143 H0 T1 P1 S125 A2 ; Monitor heater thermistor, if temp goes above 125C temporarily turn off
                                M143 H0 T1 P2 S132 A3 ; Monitor heater thermistor, if temp goes above 132C cut "atx" supply
                                ;Extruder T0 heater
                                ;Slice Engineering 50W heater+ E3d PT100
                                M308 S2 P"1.spi.cs0" Y" rtd-max31865" A"T0" ;configure sensor 2 as PT100 on SPI
                                M950 H1 C"1.out0" T2 ; create nozzle heater output on out1 and map it to sensor 2
                                M307 H1 B0 S1.00 ; disable bang-bang mode for the nozzle heater and set PWM limit
                                M307 H1 R2.995 C180.5:160.8 D2.60 S1.00 V24.1
                                M143 H1 S300 ; set temperature limit for heater 1 to 300C
                                ;Chamber Monitors
                                ;Thermisors below: https://www.amazon.com/gp/product/B07D9LSKWK/ref=ppx_yo_dt_b_asin_title_o03_s00?ie=UTF8&psc=1
                                M308 S3 P"1.temp1" Y"thermistor" T100000 B4725 C7.06e-8 A"Chamber Upper Temp"
                                M308 S4 P"0.temp2" Y"thermistor" T100000 B4725 C7.06e-8 A"Chamber Gantry Temp" ; configure sensor 2 as thermistor on pin temp2
                                M308 S5 P"0.temp3" Y"thermistor" T100000 B4725 C7.06e-8 A"Z Motor4 Temp" ; Epoxied to stepper 4
                                M308 S10 P"0.spi.cs1" Y"dht22" A"Chamber Lower Temp" ; define DHT22 temperature sensor
                                M308 S11 P"S10.1" Y"dhthumidity" A"Chamber Hum[%]" ; Attach DHT22 humidity sensor to secondary output of temperature sensor
                                ;mcu calibration
                                M308 S7 Y"mcu-temp" A"MCU" ; configure MCU as sensor 3
                                M912 P0 S-13.6 ; set CPU temp correction
                                ; Fans/LEDs
                                ;part cooling fan
                                M950 F0 C"1.out7" Q500 ; create fan 0 on pin out1 and set its frequency
                                M106 P0 S0 H-1 L2 C"Part fan" ; set fan 0 value. Thermostatic control is turned off
                                ;main extruder heater cooling fan
                                M950 F1 C"1.out6" Q500 ; create fan 1 on pin 20.out1 and set its frequency
                                M106 P1 S255 H2 T45 C"Extruder fan" ; set fan 1 value. Thermostatic control is turned on
                                ;Electronic cooling fan
                                M950 F2 C"0.out7" Q100 ; create fan 2 on pin out7 and set its frequency
                                ;M106 P2 S.25 H-1 C"MCU fans"
                                M106 P2 L0.25 X1 H7 T26:32 C"MCU fans" ; set fan 2 value. Thermostatic control is turned on
                                ;Main LEDs
                                M950 F3 C"0.out4" Q500 ; create fan 3 on pin out4 and set its frequency
                                M106 P3 S0 H-1 C"Lights" ; set fan 3 value. Thermostatic control is turned off
                                ;Filter fan
                                M950 F4 C"1.out8" Q100 ; create fan 4 on pin out8 and set its frequency
                                M106 P4 S0 H-1 C"Filter Fan" ; set fan 4 value. Thermostatic control is turned off
                                ; Tools
                                M563 P0 S"Tool 0" D0 H1 F0 ; define tool 0
                                G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
                                G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C
                                M591 D0 P7 C"1.io0.in" S1 E25 L2.1 R70:130 ; create filament monitor for Tool 0
                                M572 D0 S0.00 ; default pressure advance for Tool 0
                                M592 D0 A0.0 B0.00 L0.2 ; Nonlinear extrusion Tool 0
                                ;M593 F34.48 ; Cancel ringing
                                ;Work Offsets:
                                G10L2P1 X0.0Y0.0Z0.0 ;Set G54 offset to be machine coordinates
                                G10L2P7 X230.2Y349.5Z0.0 ;use G59.1 for tool height probing Z zero is top of the setter when not pressed
                                G10L2P8 X100.0Y344.5Z5.0 ;use G59.2 for nozzle cleaning, center of brush, top of brush
                                ; Motor Stall Detect
                                M915 X S10 F1 H200 R1
                                M915 Y S10 F1 H200 R1
                                M915 Z S10 F1 H200 R1
                                ;global varialle delcare
                                global gantryLevel = 0
                                global printstoptime = 0
                                global printcomplete = 0
                                global holdtime = 0
                                ; Miscellaneous
                                M115
                                M115 B1 ;Check status of Can-FD exansion board
                                M911 S19 R22 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
                                M207 S0.4 R0.0 F3600 T3600 Z1.0 ; set default retraction settings
                                G54
                                T0 ; select first tool
                                ;G31 K0 ;select Bltouch by default
                                M106 P3 S255 ; turn on lights
                                ;M564 H0 S0; Allow movement outside of max/min and allow movment without homing
                                ;Random Notes---------------------------------------------------------------------------------------------------------------------
                                ;wget -q https://pkg.duet3d.com/duet3d.gpg
                                ;wget -q https://pkg.duet3d.com/duet3d-unstable.list
                                ;sudo mv duet3d.gpg /etc/apt/trusted.gpg.d/
                                ;sudo mv duet3d-unstable.list /etc/apt/sources.list.d/duet3d-unstable.list
                                ;sudo chown root:root /etc/apt/trusted.gpg.d/duet3d.gpg
                                ;sudo chown root:root /etc/apt/sources.list.d/duet3d-unstable.list
                                ;sudo rm /etc/apt/sources.list.d/duet3d.list
                                ;sudo apt-get update
                                ;sudo apt-get upgrade
                                ;(may need: sudo apt-get dist-upgrade)
                                ;Webcam
                                ;https://forum.duet3d.com/topic/13604/duet-3-raspberry-pi-camera/6
                                ;full interface http://voron.local:8080/
                                ;minimal interface http://voron.local:8080/html/min.php
                                ;accelerometer setup
                                ;adafruit lis3dh
                                ;SDI (MOSI) is SDA(on board)
                                ;SPI.cs3 is CS
                                ;SPI.cs2 is INT
                                ;M955 P0 C"spi.cs2+spi.cs3"

                                Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

                                undefined 1 Reply Last reply 25 Apr 2021, 20:44 Reply Quote 0
                                • undefined
                                  dc42 administrators @Alex.cr
                                  last edited by dc42 25 Apr 2021, 20:44

                                  @alex-cr thanks. I've updated the firmware binary at https://www.dropbox.com/sh/6fdfjn7fpjnk3vv/AADWZIXsKn5B_GsTauCx8Nsna?dl=0. Please try that one. Whether your daemon.g file succeeds or crashes, please post a new M122 report after running it.

                                  Duet WiFi hardware designer and firmware engineer
                                  Please do not ask me for Duet support via PM or email, use the forum
                                  http://www.escher3d.com, https://miscsolutions.wordpress.com

                                  undefined undefined 2 Replies Last reply 26 Apr 2021, 00:55 Reply Quote 0
                                  • undefined
                                    Alex.cr @dc42
                                    last edited by 26 Apr 2021, 00:55

                                    @dc42

                                    Good news, the latest +1 appears to have fixed the firmware crashes.
                                    Unfortunately the line in deamon.g that was causing the crash is now throwing the following alarm.

                                    ; daemon.g
                                    set global.holdtime = state.upTime
                                    set global.printcomplete = state.upTime - global.printstoptime

                                    Screenshot 2021-04-25 204953.jpg

                                    The global variable "printstoptime" is fully defined according to the object model.

                                    And as requested here is the M122.

                                    m122
                                    === Diagnostics ===
                                    RepRapFirmware for Duet 3 MB6HC version 3.3beta3+1 (2021-04-25 21:40:09) running on Duet 3 MB6HC v0.6 or 1.0 (SBC mode)
                                    Board ID: 08DJM-956L2-G43S4-6J1FD-3SJ6T-TB6QH
                                    Used output buffers: 1 of 40 (10 max)
                                    === RTOS ===
                                    Static ram: 150800
                                    Dynamic ram: 64488 of which 176 recycled
                                    Never used RAM 135872, free system stack 178 words
                                    Tasks: SENSORS(delaying,0.0%,70) Linux(resourceWait:,5.7%,266) HEAT(delaying,0.0%,281) Move(notifyWait,0.0%,350) CanReceiv(notifyWait,0.0%,773) CanSender(notifyWait,0.0%,373) CanClock(delaying,0.0%,341) TMC(notifyWait,7.2%,93) MAIN(running,87.0%,924) IDLE(ready,0.0%,29), total 100.0%
                                    Owned mutexes: HTTP(MAIN)
                                    === Platform ===
                                    Last reset 00:10:34 ago, cause: software
                                    Last software reset at 2021-04-25 20:42, reason: User, none spinning, available RAM 135872, slot 0
                                    Software reset code 0x0012 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00400000 BFAR 0x00000000 SP 0x00000000 Task Linu Freestk 0 n/a
                                    Error status: 0x00
                                    Aux0 errors 0,0,0
                                    Aux1 errors 0,0,0
                                    Step timer max interval 134
                                    MCU temperature: min 24.9, current 25.5, max 39.7
                                    Supply voltage: min 3.1, current 24.0, max 24.1, under voltage events: 1, over voltage events: 0, power good: yes
                                    12V rail voltage: min 0.4, current 12.2, max 12.2, under voltage events: 0
                                    Heap OK, handles allocated/used 99/4, heap memory allocated/used/recyclable 2048/64/0, gc cycles 0
                                    Driver 0: position 0, standstill, reads 58281, writes 28 timeouts 0, SG min/max 0/0
                                    Driver 1: position 0, standstill, reads 58281, writes 28 timeouts 0, SG min/max 0/0
                                    Driver 2: position 0, standstill, reads 58281, writes 28 timeouts 0, SG min/max 0/0
                                    Driver 3: position 0, standstill, reads 58281, writes 28 timeouts 0, SG min/max 0/0
                                    Driver 4: position 0, standstill, reads 58281, writes 28 timeouts 0, SG min/max 0/0
                                    Driver 5: position 0, standstill, reads 58282, writes 28 timeouts 0, SG min/max 0/0
                                    Date/time: 2021-04-25 20:53:14
                                    Slowest loop: 0.68ms; fastest: 0.04ms
                                    === Storage ===
                                    Free file entries: 10
                                    SD card 0 not detected, interface speed: 37.5MBytes/sec
                                    SD card longest read time 0.0ms, write time 0.0ms, max retries 0
                                    === Move ===
                                    DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000
                                    === MainDDARing ===
                                    Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                    === AuxDDARing ===
                                    Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
                                    === Heat ===
                                    Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
                                    Heater 1 is on, I-accum = 0.0
                                    === GCodes ===
                                    Segments left: 0
                                    Movement lock held by null
                                    HTTP* is doing "M122" in state(s) 0
                                    Telnet is idle in state(s) 0
                                    File is idle in state(s) 0
                                    USB is idle in state(s) 0
                                    Aux is idle in state(s) 0
                                    Trigger* is idle in state(s) 0
                                    Queue is idle in state(s) 0
                                    LCD is idle in state(s) 0
                                    SBC is idle in state(s) 0
                                    Daemon is idle in state(s) 0
                                    Aux2 is idle in state(s) 0
                                    Autopause is idle in state(s) 0
                                    Code queue is empty.
                                    === Filament sensors ===
                                    Extruder 0 sensor: no data received
                                    === CAN ===
                                    Messages queued 5699, send timeouts 15, received 7849, lost 0, longest wait 1ms for reply type 6042, peak Tx sync delay 45775, free buffers 49 (min 48)
                                    Last cancelled message type 30 dest 127
                                    === SBC interface ===
                                    State: 4, failed transfers: 0
                                    Last transfer: 1ms ago
                                    RX/TX seq numbers: 23043/23043
                                    SPI underruns 0, overruns 0
                                    Number of disconnects: 0, IAP RAM available 0x2c594
                                    Buffer RX/TX: 0/0-0
                                    === Duet Control Server ===
                                    Duet Control Server v3.3-b3
                                    Code buffer space: 4096
                                    Configured SPI speed: 8000000 Hz
                                    Full transfers per second: 36.43
                                    Codes per second: 0.15
                                    Maximum length of RX/TX data transfers: 5740/936

                                    Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

                                    undefined 1 Reply Last reply 26 Apr 2021, 08:49 Reply Quote 0
                                    • undefined
                                      dc42 administrators @Alex.cr
                                      last edited by dc42 26 Apr 2021, 08:49

                                      @alex-cr thanks. As you are using SBC I'll ask @chrishamm to look at why the global variable isn't found.

                                      Duet WiFi hardware designer and firmware engineer
                                      Please do not ask me for Duet support via PM or email, use the forum
                                      http://www.escher3d.com, https://miscsolutions.wordpress.com

                                      undefined 1 Reply Last reply 26 Apr 2021, 23:57 Reply Quote 0
                                      • undefined
                                        Alex.cr @dc42
                                        last edited by 26 Apr 2021, 23:57

                                        @dc42

                                        Not a problem. Just doing my best to beta test!

                                        Voron2.4/Duet3 SBC+6HC+3HC+1LC+1HCL(x2) - Delta/Duet2 Wifi - CubePro/Duet2 Wifi+Duex5 - Laser/Duet3 Mini5+ - Cel Robox - U̶p̶3̶0̶0̶+/D̶u̶e̶t̶3̶ ̶6̶H̶C̶+̶LC1̶ - F̶T̶-̶5̶/̶D̶u̶e̶t̶2̶ ̶W̶i̶f̶i̶ - S̶o̶l̶i̶d̶o̶o̶d̶l̶e̶

                                        chrishammundefined 1 Reply Last reply 27 Apr 2021, 19:09 Reply Quote 0
                                        • chrishammundefined
                                          chrishamm administrators @Alex.cr
                                          last edited by 27 Apr 2021, 19:09

                                          @alex-cr This problem had to do with the space after the variable name. To work-around this problem you can remove spaces before the '=' from your daemon.g.

                                          I've got a fix ready for this, thanks for your report.

                                          Duet software engineer

                                          1 Reply Last reply Reply Quote 0
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