Extruder slows to a crawl
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this is a cory XY with a Kracken head, 4 nozzles 4 extruders
All x/y/z/ movements are fine and at normal speed, but fore some reason the extruder will slow down to barely visible movement. stepper and wiring have been verified and known good.
a power cycle fixes the issue for a bit and then at random it slows down.
Config.g
; General preferences M575 P1 S1 B57600 ;connect a PanelDue to this port as of RRF 3.1.1 G90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"TronXY" ; set printer name M667 S1 ; select CoreXY mode ; Network ;M551 P"xxxx" ; set password M552 S1 ; enable network M586 P0 S1 ; enable HTTP M586 P1 S0 ; disable FTP M586 P2 S1 ; enable Telnet ; Drives ;Extruders M569 P3 S0 ; physical drive 1 goes backwards M569 P4 S0 ; physical drive 2 goes backwards M569 P6 S1 ; physical drive 3 goes fowards M569 P7 S1 ; physical drive 4 goes fowards ;X axis M569 P0 S1 ; physical drive 0 goes forwards ;Y axis M569 P1 S1 ; physical drive 1 goes forwards ;Z axis M569 P2 S0 ; physical drive 2 goes backwards M569 P5 S0 ; physical drive 5 goes backwards ; End Drives M584 X0 Y1 Z2:5 E3:4:6:7 ; set drive mapping M671 X410:-85 Y165:165 S10 ; leadscrews at left (connected to Z) and right (connected to E1) of X axis M208 X0:330 Y-5:340 ; X carriage moves from 0 to 330, Y bed goes from -5 to 330 M350 X16 Y16 Z16 E16:16:16:16 I1 ; configure microstepping with interpolation M92 X80.00 Y80.00 Z400.00 E142:142:142:142 ; set steps per mm M566 X900.00 Y900.00 Z12.00 E120.00:120.00:120.00:120.00 ; set maximum instantaneous speed changes (mm/min) M203 X18000.00 Y18000.00 Z180.00 E1200.00:1200.00:1200.00:1200.00 ; set maximum speeds (mm/min) M201 X3000.00 Y3000.00 Z100.00 E2500.00:2500.00:2500.00:2500.00 ; set accelerations (mm/s^2) M906 X950 Y950 Z1200 E950:950:950:950 I30 ; set motor currents (mA) and motor idle factor in per cent M84 S600 ; Set idle timeout ; Axis Limits M208 X0 Y0 Z0 S1 ; set axis minima M208 X330 Y320 Z400 S0 ; set axis maxima ; Endstops M574 X1 S1 P"xstop" ; configure active-low May need ! before pin name to invert signal, S0 Retired M574 Y1 S1 P"ystop" ; configure active-low May need ! before pin name to invert signal, S0 Retired M574 Z1 S2 P"zstop+e2stop" ; configure active-high endstops for low end on Z via pins zstop and e2stop ;Filament Sensors M591 D0 P2 C"!e0_stop" S1 ;Extruder 1(0) M591 D1 P2 C"!e1_stop" S1 ;Extruder 2(1) M591 D2 P2 C"!duex.e3stop" S1 ;Extruder 3(2).....!e3_stop M591 D3 P2 C"!duex.e4stop" S1 ;Extruder 4(3)..,...!e4_stop ;M581 P"e0stop" T1 C0 ;Any trigger number # greater than 1 causes the macro file sys/trigger#.g to be executed. ; Z-Probe M950 S0 C"duex.e6heat" ; create servo pin 0 for BLTouch M558 P9 C"zprobe.in+zprobe.mod" H5 F1500 T8000 ; set Z probe type to bltouch and the dive height + speeds G31 P500 X-20 Y57.7 Z1.05 ; set Z probe trigger value, offset and trigger height org=Z1.47 (positive number moves bed closer to nozzle) *************************************** M557 X0:330 Y0:330 S75 ; define mesh grid ; Heaters M308 S0 P"bedtemp" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin bedtemp M950 H0 C"bedheat" T0 ; create bed heater output on bedheat and map it to sensor 0 M143 H0 S120 ; set temperature limit for heater 0 to 120C M307 H0 B0 S1.00 ; disable bang-bang mode for the bed heater and set PWM limit M140 H0 ; map heated bed to heater 0 ; Heater Ex 1 M308 S1 P"e0temp" Y"thermistor" T100000 B4138 ; configure sensor 1 as thermistor on pin e0temp M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1 M143 H1 S280 ; set temperature limit for heater 1 to 280C M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit ; Heater Ex 2 M308 S2 P"e1temp" Y"thermistor" T100000 B4138 ; configure sensor 2 as thermistor on pin e0temp M950 H2 C"e1heat" T2 ; create nozzle heater output on e0heat and map it to sensor 1 M143 H2 S280 ; set temperature limit for heater 1 to 280C M307 H2 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit ; Heater Ex 3 M308 S3 P"duex.e2temp" Y"thermistor" T100000 B4138 ; configure sensor 3 as thermistor on pin e0temp M950 H3 C"duex.e2heat" T3 ; create nozzle heater output on e0heat and map it to sensor 1 M143 H3 S280 ; set temperature limit for heater 1 to 280C M307 H3 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit ; Heater Ex 4 M308 S4 P"duex.e3temp" Y"thermistor" T100000 B4138 ; configure sensor 4 as thermistor on pin e0temp M950 H4 C"duex.e3heat" T4 ; create nozzle heater output on e0heat and map it to sensor 1 M143 H4 S280 ; set temperature limit for heater 1 to 280C M307 H4 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit ; End Heaters ; Fans M950 F0 C"fan0" ; create fan 0 on pin fan0 and set its frequency M106 P0 S0 H-1 C"Right_Fan" ; set fan 0 value. Thermostatic control is turned off M950 F1 C"fan1" ; create fan 1 on pin fan1 and set its frequency M106 P1 S0 H-1 C"Left_Fan" ; set fan 1 value. Thermostatic control is turned off M950 F7 C"duex.fan7" ; create fan 0 on pin fan0 and set its frequency M106 P7 S1 C"Rad_Fan" T45 H1:2:3:4 ; set fan 7 value. Thermostatic control is turned on for heaters 1 Thru 4 M950 F8 C"duex.fan8" ; create fan 0 on pin fan0 and set its frequency M106 P8 S1 C"Coolent_Pump" T45 H1:2:3:4 ; set pump 8 value. Thermostatic control is turned on for heaters 1 Thru 4 ; Tools ; nozzle map ; ; _______ ; | 3 | 1 | Nozzles are 20mm on center ; | ----- | ; | 4 | 2 | ; ------- ; front ;Tool 1 M563 P0 D0 H1 F0:1 ; define tool 0 G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures [R] to 0C ;Tool 2 M563 P1 D1 H2 F0:1 ; define tool 1 G10 P1 X0.65 Y-19.8 Z0 ; set tool 1 axis offsets G10 P1 R0 S0 ; set initial tool 0 active and standby temperatures to 0C ;Tool 3 M563 P2 D2 H3 F0:1 ; define tool 0 G10 P2 X-19.75 Y0 Z0 ; set tool 0 axis offsets G10 P2 R0 S0 ; set initial tool 0 active and standby temperatures to 0C ;Tool 4 M563 P3 D3 H4 F0:1 ; define tool 1 G10 P3 X-19.6 Y-20.4 Z0 ; set tool 1 axis offsets G10 P3 R0 S0 ; set initial tool 0 active and standby temperatures to 0C ; End Tools ; Custom settings are not defined M929 P"eventlog.txt" S1 ; start logging to file eventlog.txt M570 H1 P20 T20 S5 M570 H2 P20 T20 S5 M570 H3 P20 T20 S5 M570 H4 P20 T20 S5 ; Miscellaneous M912 P0 S-4.1 ; At cold boot Temp of cold extruder - Temp of cold MCU...may be negative M501 ; load saved parameters from non-volatile memory M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss ;T0 ; select first tool
M122 before power cycle
M122 === Diagnostics === RepRapFirmware for Duet 2 WiFi/Ethernet version 3.1.1 running on Duet WiFi 1.02 or later + DueX5 Board ID: 08DJM-9178L-L2MS8-6JTF4-3S86S-99GLP Used output buffers: 1 of 24 (16 max) === RTOS === Static ram: 27980 Dynamic ram: 96616 of which 52 recycled Exception stack ram used: 664 Never used ram: 5760 Tasks: NETWORK(ready,268) HEAT(blocked,1168) DUEX(suspended,160) MAIN(running,1228) IDLE(ready,80) Owned mutexes: === Platform === Last reset 01:20:32 ago, cause: power up Last software reset at 2021-05-08 21:46, reason: User, spinning module GCodes, available RAM 5872 bytes (slot 2) Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task MAIN Error status: 0 MCU temperature: min 24.6, current 32.4, max 33.5 Supply voltage: min 12.3, current 12.5, max 12.8, under voltage events: 0, over voltage events: 0, power good: yes Driver 0: standstill, SG min/max 0/1023 Driver 1: standstill, SG min/max 0/1023 Driver 2: standstill, SG min/max not available Driver 3: standstill, SG min/max not available Driver 4: standstill, SG min/max not available Driver 5: standstill, SG min/max not available Driver 6: standstill, SG min/max not available Driver 7: standstill, SG min/max not available Driver 8: standstill, SG min/max not available Driver 9: standstill, SG min/max not available Date/time: 2021-05-10 18:57:54 Cache data hit count 4294967295 Slowest loop: 59.96ms; fastest: 0.15ms I2C nak errors 2, send timeouts 336010, receive timeouts 3, finishTimeouts 336010, resets 336015 === Storage === Free file entries: 9 SD card 0 detected, interface speed: 20.0MBytes/sec SD card longest read time 3.2ms, write time 34.6ms, max retries 0 === Move === Hiccups: 0(0), FreeDm: 169, MinFreeDm: 119, MaxWait: 442195ms Bed compensation in use: mesh, comp offset -0.166 === MainDDARing === Scheduled moves: 28339, completed moves: 28339, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1 === AuxDDARing === Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1 === Heat === Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1 Heater 0 is on, I-accum = 0.0 Heater 4 is on, I-accum = 0.2 === GCodes === Segments left: 0 Movement lock held by null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is ready with "M408 S0 R41" in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 Daemon is idle in state(s) 0 Autopause is idle in state(s) 0 Code queue is empty. === Network === Slowest loop: 46.45ms; fastest: 0.00ms Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions HTTP sessions: 1 of 8 - WiFi - Network state is active WiFi module is connected to access point Failed messages: pending 0, notready 0, noresp 0 WiFi firmware version 1.23 WiFi MAC address cc:50:e3:e3:ac:2c WiFi Vcc 3.36, reset reason Unknown WiFi flash size 4194304, free heap 21912 WiFi IP address 192.168.0.125 WiFi signal strength -38dBm, reconnections 0, sleep mode modem Socket states: 0 0 0 0 0 0 0 0 === Filament sensors === Extruder 0 sensor: ok Extruder 1 sensor: ok Extruder 2 sensor: no filament Extruder 3 sensor: no filament === DueX === Read count 93, 1.15 reads/min 5/10/2021, 6:48:35 PM m92 Steps/mm: X: 80.000, Y: 80.000, Z: 400.000, E: 142.000:142.000:142.000:142.000
M122 after power cycle
M122 === Diagnostics === RepRapFirmware for Duet 2 WiFi/Ethernet version 3.1.1 running on Duet WiFi 1.02 or later + DueX5 Board ID: 08DJM-9178L-L2MS8-6JTF4-3S86S-99GLP Used output buffers: 3 of 24 (16 max) === RTOS === Static ram: 27980 Dynamic ram: 96416 of which 52 recycled Exception stack ram used: 552 Never used ram: 6072 Tasks: NETWORK(ready,348) HEAT(blocked,1224) DUEX(suspended,160) MAIN(running,1816) IDLE(ready,80) Owned mutexes: WiFi(NETWORK) === Platform === Last reset 00:01:20 ago, cause: power up Last software reset at 2021-05-08 21:46, reason: User, spinning module GCodes, available RAM 5872 bytes (slot 2) Software reset code 0x0003 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0441f000 BFAR 0xe000ed38 SP 0xffffffff Task MAIN Error status: 0 MCU temperature: min 30.8, current 32.5, max 32.8 Supply voltage: min 12.3, current 12.5, max 12.7, under voltage events: 0, over voltage events: 0, power good: yes Driver 0: standstill, SG min/max 0/204 Driver 1: standstill, SG min/max 0/0 Driver 2: standstill, SG min/max not available Driver 3: standstill, SG min/max not available Driver 4: standstill, SG min/max not available Driver 5: standstill, SG min/max not available Driver 6: standstill, SG min/max not available Driver 7: standstill, SG min/max not available Driver 8: standstill, SG min/max not available Driver 9: standstill, SG min/max not available Date/time: 2021-05-10 19:04:40 Cache data hit count 132628069 Slowest loop: 9.84ms; fastest: 0.15ms I2C nak errors 0, send timeouts 0, receive timeouts 0, finishTimeouts 0, resets 0 === Storage === Free file entries: 9 SD card 0 detected, interface speed: 20.0MBytes/sec SD card longest read time 2.5ms, write time 15.1ms, max retries 0 === Move === Hiccups: 0(0), FreeDm: 169, MinFreeDm: 167, MaxWait: 23195ms Bed compensation in use: none, comp offset 0.000 === MainDDARing === Scheduled moves: 11, completed moves: 11, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1 === AuxDDARing === Scheduled moves: 0, completed moves: 0, StepErrors: 0, LaErrors: 0, Underruns: 0, 0 CDDA state: -1 === Heat === Bed heaters = 0 -1 -1 -1, chamberHeaters = -1 -1 -1 -1 Heater 4 is on, I-accum = 0.2 === GCodes === Segments left: 0 Movement lock held by null HTTP is idle in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 Daemon is idle in state(s) 0 Autopause is idle in state(s) 0 Code queue is empty. === Network === Slowest loop: 45.72ms; fastest: 0.00ms Responder states: HTTP(2) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions HTTP sessions: 1 of 8 - WiFi - Network state is active WiFi module is connected to access point Failed messages: pending 0, notready 0, noresp 0 WiFi firmware version 1.23 WiFi MAC address cc:50:e3:e3:ac:2c WiFi Vcc 3.36, reset reason Unknown WiFi flash size 4194304, free heap 18384 WiFi IP address 192.168.0.125 WiFi signal strength -38dBm, reconnections 0, sleep mode modem Socket states: 0 4 0 0 0 0 0 0 === Filament sensors === Extruder 0 sensor: ok Extruder 1 sensor: ok Extruder 2 sensor: ok Extruder 3 sensor: ok === DueX === Read count 1, 0.74 reads/min
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@htrabbit said in Extruder slows to a crawl:
All x/y/z/ movements are fine and at normal speed, but fore some reason the extruder will slow down to barely visible movement.
Is this during a print? or when?
Can you show a video of the behaviour?
If it's during a print can you share the gcode file? -
@phaedrux
this happens during print initially, and then remains in this error state till power cyclefile is too big to upload(5mb) tried to zip and rar it still wont upload(server error
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You can rename the zip file as .txt and upload it.
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@phaedrux
rename to .zip
single_joycon_grip.txt -
it has happened to other files as well, this one was failing after layer 30ish and i stopped print at layer 47,
while it was in error state i tested a new stepper , and a new cable, neither fixed the issue.
the steppper was activated,(could not manually turn the stepper by hand. ) it was turning just super slow, could barely detect movement.
power cycled duet and it was like it never happened.could cura be getting funky? hmmm.
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@htrabbit when it happens again, please send the following commands, without parameters;
M92
M350
M221Then check that the M92 and M350 values reported for the extruder are the same values that you configured in config.g and that M221 still reports the extrusion factor as 100%.
If you power off/on and reprint the same file, does the problem recur at exactly the same place in the print?
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Can you send M98 P"config.g" and see if there are any errors?
Does it still happen with logging turned off?
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@dc42 if i reprint it does not happen in the same spot , if at all.
i will check what you asked when it happens again. thanx
i will report back here. -
@phaedrux the heater 0 line is weird, and i dont use logging....i think
M98 P"config.g" HTTP is enabled on port 80 FTP is enabled on port 21 TELNET is enabled on port 23 Error: Invalid use of P parameter Warning: Heater 0 appears to be over-powered. If left on at full power, its temperature is predicted to reach 365C
Here is my config.g
; Configuration file for Duet WiFi (firmware version 3) ; executed by the firmware on start-up ; ; ; General preferences M575 P1 S1 B57600 ;connect a PanelDue to this port as of RRF 3.1.1 G90 ; send absolute coordinates... M83 ; ...but relative extruder moves M550 P"TronXY" ; set printer name M667 S1 ; select CoreXY mode ; Network ;M551 P"2001" ; set password M552 S1 ; enable network M586 P0 S1 ; enable HTTP M586 P1 S1 ; S0 disable FTP, S1 Enable M586 P2 S1 ; enable Telnet ; Drives ;Extruders M569 P3 S0 ; physical drive 1 goes backwards M569 P4 S0 ; physical drive 2 goes backwards M569 P6 S1 ; physical drive 3 goes fowards M569 P7 S1 ; physical drive 4 goes fowards ;X axis M569 P0 S1 ; physical drive 0 goes forwards ;Y axis M569 P1 S1 ; physical drive 1 goes forwards ;Z axis M569 P2 S0 ; physical drive 2 goes backwards M569 P5 S0 ; physical drive 5 goes backwards ; End Drives M584 X0 Y1 Z2:5 E3:4:6:7 ; set drive mapping M671 X410:-85 Y165:165 S10 ; leadscrews at left (connected to Z) and right (connected to E1) of X axis M208 X0:330 Y-5:340 ; X carriage moves from 0 to 330, Y bed goes from -5 to 330 M350 X16 Y16 Z16 E16:16:16:16 I1 ; configure microstepping with interpolation M92 X80.00 Y80.00 Z400.00 E142:142:142:142 ; set steps per mm M566 X900.00 Y900.00 Z12.00 E120.00:120.00:120.00:120.00 ; set maximum instantaneous speed changes (mm/min) M203 X18000.00 Y18000.00 Z180.00 E1200.00:1200.00:1200.00:1200.00 ; set maximum speeds (mm/min) M201 X3000.00 Y3000.00 Z100.00 E2500.00:2500.00:2500.00:2500.00 ; set accelerations (mm/s^2) M906 X950 Y950 Z1200 E950:950:950:950 I30 ; set motor currents (mA) and motor idle factor in per cent M84 S600 ; Set idle timeout ; Axis Limits M208 X0 Y0 Z0 S1 ; set axis minima M208 X330 Y320 Z400 S0 ; set axis maxima ; Endstops M574 X1 S1 P"xstop" ; configure active-low May need ! before pin name to invert signal, S0 Retired M574 Y1 S1 P"ystop" ; configure active-low May need ! before pin name to invert signal, S0 Retired M574 Z1 S2 P"zstop+e2stop" ; configure active-high endstops for low end on Z via pins zstop and e2stop ;Filament Sensors M591 D0 P2 C"!e0_stop" S1 ;Extruder 1(0) M591 D1 P2 C"!e1_stop" S1 ;Extruder 2(1) M591 D2 P2 C"!duex.e3stop" S1 ;Extruder 3(2).....!e3_stop M591 D3 P2 C"!duex.e4stop" S1 ;Extruder 4(3)..,...!e4_stop ;M581 P"e0stop" T1 C0 ;Any trigger number # greater than 1 causes the macro file sys/trigger#.g to be executed. ; Z-Probe M950 S0 C"duex.e6heat" ; create servo pin 0 for BLTouch M558 P9 C"zprobe.in+zprobe.mod" H5 F1500 T8000 ; set Z probe type to bltouch and the dive height + speeds G31 P500 X-20 Y57.7 Z1.05 ; set Z probe trigger value, offset and trigger height org=Z1.47 (positive number moves bed closer to nozzle) *************************************** M557 X0:330 Y0:330 S75 ; define mesh grid ; Heaters M308 S0 P"bedtemp" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin bedtemp M950 H0 C"bedheat" T0 ; create bed heater output on bedheat and map it to sensor 0 M143 H0 S120 ; set temperature limit for heater 0 to 120C M307 H0 B0 S1.00 ; disable bang-bang mode for the bed heater and set PWM limit M140 H0 ; map heated bed to heater 0 ; Heater Ex 1 M308 S1 P"e0temp" Y"thermistor" T100000 B4138 ; configure sensor 1 as thermistor on pin e0temp M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1 M143 H1 S280 ; set temperature limit for heater 1 to 280C M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit ; Heater Ex 2 M308 S2 P"e1temp" Y"thermistor" T100000 B4138 ; configure sensor 2 as thermistor on pin e0temp M950 H2 C"e1heat" T2 ; create nozzle heater output on e0heat and map it to sensor 1 M143 H2 S280 ; set temperature limit for heater 1 to 280C M307 H2 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit ; Heater Ex 3 M308 S3 P"duex.e2temp" Y"thermistor" T100000 B4138 ; configure sensor 3 as thermistor on pin e0temp M950 H3 C"duex.e2heat" T3 ; create nozzle heater output on e0heat and map it to sensor 1 M143 H3 S280 ; set temperature limit for heater 1 to 280C M307 H3 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit ; Heater Ex 4 M308 S4 P"duex.e3temp" Y"thermistor" T100000 B4138 ; configure sensor 4 as thermistor on pin e0temp M950 H4 C"duex.e3heat" T4 ; create nozzle heater output on e0heat and map it to sensor 1 M143 H4 S280 ; set temperature limit for heater 1 to 280C M307 H4 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit ; End Heaters ; Fans M950 F0 C"fan0" ; create fan 0 on pin fan0 and set its frequency M106 P0 S0 H-1 C"Right_Fan" ; set fan 0 value. Thermostatic control is turned off M950 F1 C"fan1" ; create fan 1 on pin fan1 and set its frequency M106 P1 S0 H-1 C"Left_Fan" ; set fan 1 value. Thermostatic control is turned off M950 F7 C"duex.fan7" ; create fan 0 on pin fan0 and set its frequency M106 P7 S1 C"Rad_Fan" T45 H1:2:3:4 ; set fan 7 value. Thermostatic control is turned on for heaters 1 Thru 4 M950 F8 C"duex.fan8" ; create fan 0 on pin fan0 and set its frequency M106 P8 S1 C"Coolent_Pump" T45 H1:2:3:4 ; set pump 8 value. Thermostatic control is turned on for heaters 1 Thru 4 ; Tools ; nozzle map ; ; _______ ; | 3 | 1 | Nozzles are 20mm on center ; | ----- | ; | 4 | 2 | ; ------- ; front ;Tool 1 M563 P0 D0 H1 F0:1 ; define tool 0 G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures [R] to 0C ;Tool 2 M563 P1 D1 H2 F0:1 ; define tool 1 G10 P1 X0.65 Y-19.8 Z0 ; set tool 1 axis offsets G10 P1 R0 S0 ; set initial tool 1 active and standby temperatures to 0C ;Tool 3 M563 P2 D2 H3 F0:1 ; define tool 2 G10 P2 X-19.75 Y0 Z0 ; set tool 2 axis offsets G10 P2 R0 S0 ; set initial tool 2 active and standby temperatures to 0C ;Tool 4 M563 P3 D3 H4 F0:1 ; define tool 3 G10 P3 X-19.6 Y-20.4 Z0 ; set tool 3 axis offsets G10 P3 R0 S0 ; set initial tool 3 active and standby temperatures to 0C ; End Tools ; Custom settings are not defined M929 P"eventlog.txt" S1 ; start logging to file eventlog.txt M570 H1 P20 T20 S5 M570 H2 P20 T20 S5 M570 H3 P20 T20 S5 M570 H4 P20 T20 S5 ; Miscellaneous M912 P0 S-4.1 ; At cold boot Temp of cold extruder - Temp of cold MCU...may be negative M501 ; load saved parameters from non-volatile memory M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss ;T0 ; select first tool
i found a log file for the event, see below
power up + 00:03:22 HTTP client 192.168.0.100 login succeeded 2021-05-10 17:40:44 Date and time set at power up + 00:03:22 2021-05-10 17:50:50 HTTP client 192.168.0.100 login succeeded 2021-05-10 17:50:58 HTTP client 192.168.0.100 disconnected 2021-05-10 17:50:58 Started printing file 0:/gcodes/single_joycon_grip+_Txy-PLA-02mm-@17-50.gcode 2021-05-10 17:51:50 Leadscrew adjustments made: -0.144 -0.091, points used 2, (mean, deviation) before (-0.116, 0.014) after (0.000, 0.000) 2021-05-10 17:51:50 Warning: Skipping grid point (0.0, 0.0) because Z probe cannot reach it 2021-05-10 17:51:51 Warning: Skipping grid point (75.0, 0.0) because Z probe cannot reach it 2021-05-10 17:51:51 Warning: Skipping grid point (150.0, 0.0) because Z probe cannot reach it 2021-05-10 17:51:51 Warning: Skipping grid point (225.0, 0.0) because Z probe cannot reach it 2021-05-10 17:51:51 Warning: Skipping grid point (300.0, 0.0) because Z probe cannot reach it 2021-05-10 17:53:10 20 points probed, min error 0.013, max error 0.400, mean 0.179, deviation 0.120 Height map saved to file 0:/sys/heightmap.csv 2021-05-10 18:27:25 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:27:44 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:28:27 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:28:48 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:29:29 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:29:50 Warning: motor phase A may be disconnected reported by driver(s) 7 2021-05-10 18:29:50 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:30:34 Warning: motor phase A may be disconnected reported by driver(s) 7 2021-05-10 18:30:34 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:31:08 Warning: motor phase A may be disconnected reported by driver(s) 7 2021-05-10 18:31:08 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:31:38 Warning: motor phase A may be disconnected reported by driver(s) 7 2021-05-10 18:31:38 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:31:56 Warning: motor phase A may be disconnected reported by driver(s) 7 2021-05-10 18:31:56 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:32:17 Warning: motor phase A may be disconnected reported by driver(s) 7 2021-05-10 18:32:17 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:34:22 Warning: motor phase A may be disconnected reported by driver(s) 7 2021-05-10 18:34:22 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:34:40 Warning: motor phase A may be disconnected reported by driver(s) 7 2021-05-10 18:34:40 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:35:21 Resume state saved 2021-05-10 18:35:21 Extruder 2 reports no filament 2021-05-10 18:35:21 Warning: motor phase A may be disconnected reported by driver(s) 7 2021-05-10 18:35:21 Warning: motor phase B may be disconnected reported by driver(s) 1 7 2021-05-10 18:35:26 Printing paused at X134.3 Y165.3 Z9.7 2021-05-10 18:37:20 Warning: motor phase B may be disconnected reported by driver(s) 7 2021-05-10 18:47:00 Cancelled printing file 0:/gcodes/single_joycon_grip+_Txy-PLA-02mm-@17-50.gcode, print time was 0h 44m
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@htrabbit said in Extruder slows to a crawl:
2021-05-10 18:34:40 Warning: motor phase A may be disconnected reported by driver(s) 7 2021-05-10 18:34:40 Warning: motor phase B may be disconnected reported by driver(s) 7
Seems like a wiring issue maybe?
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@htrabbit you have 4 extruders configured, on drivers 3, 4, 6 and 7. Which extruder is failing? Is it the one connected to driver 7, which is reporting the phase errors?
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@htrabbit don't unplug the stepper while it's powered. You'll damage the driver.