[3.3 RC3] All tools heaters appears to be overpowered
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edit: i say error because the printer stopped my tool change in the middle of the Tpost1.g file where it undock the tool 1)
just upgraded from 3.3 rc2 to 3.3 rc3 to check if the bad command bug was fixed (short answer is no) and during a tool change i suddenly got this error on ALL 3 heaters (got 3 tools)
"Warning: Heater 1 appears to be over-powered. If left on at full power, its temperatur is predicted to reach 446C"and the same message for heater 2 with 646C and heater 3 with 723C.
all 3 heaters where configured with an active and stand by temperatures of 0C as i was just testing docking and undocking and if cables holders where messing with other tools.here are my M122 of both cards:
M122 B1 Diagnostics for board 1: Duet EXP3HC firmware version 3.3RC3 (2021-05-26 13:46:00) Bootloader ID: not available Never used RAM 158144, free system stack 4378 words Tasks: Move(notifyWait,0.0%,160) HEAT(delaying,0.0%,104) CanAsync(notifyWait,0.0%,69) CanRecv(notifyWait,0.0%,83) CanClock(notifyWait,0.0%,74) TMC(notifyWait,22.8%,63) MAIN(running,75.7%,303) IDLE(ready,0.0%,40) AIN(delaying,1.4%,263), total 100.0% Last reset 00:14:35 ago, cause: software Last software reset time unknown, reason: AssertionFailed, available RAM 159320, slot 0 Software reset code 0x0120 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x20004754 Task HEAT Freestk 142 bad marker Stack: 00000544 0002ebf8 000261ef 42000400 00022423 2002f020 00000000 2002f038 2000151c 00000000 0001d6c1 0002dde4 0002de9c 0002d4a0 00025035 2000159c 00000000 2002f020 00015609 00000000 000009c4 000009c4 a5a5a5a5 a5a5a5a5 a5a5a5a5 a5a5a5a5 00025035 Driver 0: position 0, 424.9 steps/mm, standstill, reads 34423, writes 6 timeouts 0, SG min/max not available, steps req 0 done 0 Driver 1: position 0, 917.4 steps/mm, standstill, reads 34423, writes 6 timeouts 0, SG min/max not available, steps req 0 done 0 Driver 2: position 0, 400.0 steps/mm, standstill, reads 34422, writes 6 timeouts 0, SG min/max not available, steps req 0 done 0 Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0 Peak sync jitter 0/8, peak Rx sync delay 181, resyncs 0/1, no step interrupt scheduled VIN: 23.8V, V12: 12.2V MCU temperature: min 36.7C, current 37.1C, max 37.6C Ticks since heat task active 72, ADC conversions started 875160, completed 875159, timed out 0, errs 0 Last sensors broadcast 0x0000000e found 3 77 ticks ago, loop time 0 CAN messages queued 8133, send timeouts 0, received 6090, lost 0, free buffers 37, min 37, error reg 0 dup 0, oos 0/0/0/0, bm 0, wbm 0 M122 B0 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.3RC3 (2021-05-26 12:29:42) running on Duet 3 MB6HC v1.01 or later (standalone mode) Board ID: 08DJM-956BA-NA3TN-6JTD8-3S86J-1UB2T Used output buffers: 1 of 40 (40 max) === RTOS === Static ram: 150784 Dynamic ram: 93660 of which 100 recycled Never used RAM 109648, free system stack 128 words Tasks: NETWORK(ready,27.8%,238) ETHERNET(notifyWait,0.1%,124) HEAT(delaying,0.0%,295) Move(notifyWait,0.0%,284) CanReceiv(notifyWait,0.0%,798) CanSender(notifyWait,0.0%,374) CanClock(delaying,0.0%,339) TMC(notifyWait,8.2%,90) MAIN(running,63.8%,924) IDLE(ready,0.0%,29), total 100.0% Owned mutexes: HTTP(MAIN) === Platform === Last reset 00:09:48 ago, cause: software Last software reset at 2021-05-29 16:09, reason: AssertionFailed, Platform spinning, available RAM 107008, slot 0 Software reset code 0x4120 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0040083c BFAR 0x00000000 SP 0x2045ff8c Task NETW Freestk 66282 ok Stack: 000002e8 004987e0 0047a12b 00000000 0047b725 0004ab15 00000004 00000001 20421a98 40000002 00000000 e000e000 004780a9 e000e000 00000000 00000000 0047356d 40000000 0dad37bb 10000000 ffffffed 00000000 00f00000 e000e000 c0000000 00000000 0047a0c5 Error status: 0x04 Aux0 errors 0,45,0 Aux1 errors 0,0,0 Step timer max interval 133 MCU temperature: min 43.1, current 43.2, max 44.0 Supply voltage: min 23.4, current 23.7, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.0, current 12.0, max 12.1, under voltage events: 0 Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0 Driver 0: position 57400, standstill, reads 59755, writes 20 timeouts 0, SG min/max 0/203 Driver 1: position 35400, standstill, reads 59755, writes 20 timeouts 0, SG min/max 0/210 Driver 2: position 0, standstill, reads 59755, writes 20 timeouts 0, SG min/max 0/167 Driver 3: position 0, standstill, reads 59755, writes 20 timeouts 0, SG min/max 0/163 Driver 4: position 0, standstill, reads 59764, writes 11 timeouts 0, SG min/max 0/0 Driver 5: position 0, standstill, reads 59764, writes 11 timeouts 0, SG min/max 0/0 Date/time: 2021-05-29 16:19:01 Slowest loop: 27.31ms; fastest: 0.05ms === Storage === Free file entries: 10 SD card 0 detected, interface speed: 25.0MBytes/sec SD card longest read time 2.2ms, write time 2.9ms, max retries 0 === Move === DMs created 125, maxWait 87018ms, bed compensation in use: none, comp offset 0.000 === MainDDARing === Scheduled moves 16, completed moves 16, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === AuxDDARing === Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1 Heater 2 is on, I-accum = 0.0 === GCodes === Segments left: 0 Movement lock held by null HTTP is ready with "M122 B0" in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 Code queue is empty. === CAN === Messages queued 5346, send timeouts 0, received 7139, lost 0, longest wait 2ms for reply type 6024, peak Tx sync delay 271, free buffers 49 (min 48), ts 2945/2944/0 === Network === Slowest loop: 3.87ms; fastest: 0.02ms Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions HTTP sessions: 1 of 8 - Ethernet - State: active Error counts: 0 0 1 0 0 Socket states: 5 2 2 2 2 0 0 0 -
@psychotik2k3
This is just a warning. It’s not an error, it doesn’t stop you from doing anything. That is weird that you have not seen it prior to RC3.Out of curiosity, are all three of your tools the same physical setup?
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@alex-cr no they are all different, a bmg clone with nf crazy plus (mosquito clone)
a biqu H2 and a bondtech LGX FF
i got 2 types of thermistor and 3 different configurations for that.
and it's not only a warning as it stopped my tool change in the middle with the code of tpost1.g not finished. -
@psychotik2k3 said in [3.3 RC3] All tools heaters appears to be overpowered:
That looks like your board may have reset (so the messages will have been generated when re-reading your config.g file). The M122 is reporting a reset due to an AssertionFailed which I suspect @dc42 may want to take a look at. It may help for you to post your tool change macros. -
@gloomyandy of course here are my files and the complete config.
i launch the torture test macro. and it happened in the middle of the first T1[1_1622311463966_sys.zip](Uploading 100%) [0_1622311463964_macros.zip](Uploading 100%)
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You cannot upload zip files to the forum. Can you upload the .g files directly?
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@psychotik2k3 i had to rename my macros with a .g to be able to uplaod it. so it's allright that the macro file does not match the M98 exactly
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@dc42 any news about this bug and the bad command on the panel due ?
do you want some debug logs ?because for now the 3.3 is unusable as i got interruption even for a simple job taht cycle through my 3 tools.
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So you're getting bad command errors on the paneldue during prints?
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@phaedrux yes wasn't able to finish my torture_test_tool_change file
or sometimes even when just laucnhing a bed align through the button on the panel due -
This has been noted a few times in RRF3. There's something that makes it more sensitive to picking up interference as bad commands, or rather, it used to be rejected and now it's being interpreted as a bad command. In most cases improving the wiring for the Paneldue solved the problem.
Can you show us what your wiring is like for the Panel?
I've also asked DC42 to check the assertion failed error report.
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@phaedrux i do have a cable that's near motor but as i didn't had problem with 3.2 never thought it could be that.
gonna try to rewire elsewhere and wheck if it fixes or not.
an i suppose i have to do the same thing for the can bus wire between my mainboard and my h3c ? -
Which paneldue firmware version btw?
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@psychotik2k3 please try the new firmware .bin file at https://www.dropbox.com/sh/nmpsl9a3jfsumm5/AAA6adSjEcd1AM_j5_tVberGa?dl=0. I expect this to fix the asssertion failure.
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@dc42 ok i will try that because i rerouted my panel due wires and canbus cable to be away from motor and motor cables and it fixed nothing.
here is the point where the panel due is the closest to a motor/wire motor: -
@dc42 seems better but i still faced one on "home all" after a reset, and i faced a warning message "M9 command is not supported" at the end of a G32 (14:46) initiated from the bed button on the panel due.
and i just have a reset of the whole board in the middle of a movement.
so it seems a little better but still not good.here is the debug log i have and the M122 for both cards
05/06/2021, 14:53:49 M122 B0 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.3RC3+3 (2021-06-04 09:11:55) running on Duet 3 MB6HC v1.01 or later (standalone mode) Board ID: 08DJM-956BA-NA3TN-6JTD8-3S86J-1UB2T Used output buffers: 1 of 40 (20 max) === RTOS === Static ram: 150896 Dynamic ram: 93376 of which 100 recycled Never used RAM 109820, free system stack 188 words Tasks: NETWORK(ready,29.3%,254) ETHERNET(notifyWait,0.1%,124) HEAT(delaying,0.0%,325) Move(notifyWait,0.0%,352) CanReceiv(notifyWait,0.0%,774) CanSender(notifyWait,0.0%,373) CanClock(delaying,0.0%,349) TMC(notifyWait,7.1%,90) MAIN(running,63.1%,924) IDLE(ready,0.2%,29), total 100.0% Owned mutexes: HTTP(MAIN) === Platform === Last reset 00:00:52 ago, cause: software Last software reset at 2021-06-05 14:52, reason: AssertionFailed, Platform spinning, available RAM 106704, slot 1 Software reset code 0x4120 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0042783c BFAR 0x00000000 SP 0x2045ff8c Task NETW Freestk 66282 ok Stack: 000002e8 00498a28 0047a2eb 00000000 0047b8e5 187c4844 2042e320 20428338 20421b10 40000002 00000000 e000e000 004781e1 204298d8 00000000 00000000 00473689 00004858 187c484a 10000000 ffffffed 00000000 00f00000 e000e000 c0000000 00000000 0047a285 Error status: 0x00 Aux0 errors 0,0,0 Step timer max interval 132 MCU temperature: min 40.8, current 41.3, max 41.5 Supply voltage: min 23.4, current 23.7, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.0, current 12.0, max 12.1, under voltage events: 0 Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0 Driver 0: position 0, standstill, reads 33373, writes 15 timeouts 0, SG min/max 0/0 Driver 1: position 0, standstill, reads 33373, writes 15 timeouts 0, SG min/max 0/0 Driver 2: position 0, standstill, reads 33373, writes 15 timeouts 0, SG min/max 0/0 Driver 3: position 0, standstill, reads 33373, writes 15 timeouts 0, SG min/max 0/0 Driver 4: position 0, standstill, reads 33378, writes 11 timeouts 0, SG min/max 0/0 Driver 5: position 0, standstill, reads 33378, writes 11 timeouts 0, SG min/max 0/0 Date/time: 2021-06-05 14:53:48 Slowest loop: 6.43ms; fastest: 0.05ms === Storage === Free file entries: 10 SD card 0 detected, interface speed: 25.0MBytes/sec SD card longest read time 2.1ms, write time 2.0ms, max retries 0 === Move === DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000 === MainDDARing === Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === AuxDDARing === Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1 Heater 2 is on, I-accum = 0.0 === GCodes === Segments left: 0 Movement lock held by null HTTP is ready with "M122 B0" in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 Code queue is empty. === CAN === Messages queued 510, send timeouts 0, received 670, lost 0, longest wait 1ms for reply type 6018, peak Tx sync delay 59, free buffers 49 (min 48), ts 265/264/0 === Network === Slowest loop: 2.88ms; fastest: 0.02ms Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions HTTP sessions: 1 of 8 - Ethernet - State: active Error counts: 0 0 0 0 0 Socket states: 5 2 2 2 2 0 0 0 M122 B1 Diagnostics for board 1: Duet EXP3HC firmware version 3.3RC3 (2021-05-26 13:46:00) Bootloader ID: not available Never used RAM 158144, free system stack 4392 words Tasks: Move(notifyWait,0.0%,160) HEAT(delaying,0.0%,101) CanAsync(notifyWait,0.0%,69) CanRecv(notifyWait,0.0%,83) CanClock(notifyWait,0.0%,74) TMC(notifyWait,22.8%,63) MAIN(running,75.7%,303) IDLE(ready,0.0%,40) AIN(delaying,1.4%,263), total 100.0% Last reset 00:10:05 ago, cause: software Last software reset time unknown, reason: AssertionFailed, available RAM 159320, slot 0 Software reset code 0x0120 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x20004754 Task HEAT Freestk 142 bad marker Stack: 00000544 0002ebf8 000261ef 42000400 00022423 2002f020 00000000 2002f038 2000151c 00000000 0001d6c1 0002dde4 0002de9c 0002d4a0 00025035 2000159c 00000000 2002f020 00015609 00000000 000009c4 000009c4 a5a5a5a5 a5a5a5a5 a5a5a5a5 a5a5a5a5 00025035 Driver 0: position 0, 424.9 steps/mm, standstill, reads 45106, writes 23 timeouts 0, SG min/max 0/0, steps req 0 done 0 Driver 1: position 0, 917.4 steps/mm, standstill, reads 45109, writes 23 timeouts 0, SG min/max 0/0, steps req 0 done 0 Driver 2: position 0, 400.0 steps/mm, standstill, reads 45113, writes 23 timeouts 0, SG min/max 0/0, steps req 0 done 0 Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0 Peak sync jitter 0/8, peak Rx sync delay 180, resyncs 0/1, no step interrupt scheduled VIN: 23.8V, V12: 12.2V MCU temperature: min 36.5C, current 36.7C, max 37.1C Ticks since heat task active 61, ADC conversions started 605593, completed 605593, timed out 0, errs 0 Last sensors broadcast 0x0000000e found 3 66 ticks ago, loop time 0 CAN messages queued 7384, send timeouts 0, received 5562, lost 0, free buffers 37, min 37, error reg 210000 dup 0, oos 0/0/0/0, bm 0, wbm 0 2021-06-05 14:43:58 [info] Event logging started at level debug 2021-06-05 14:43:58 [info] Running: Duet 3 MB6HC v1.01 or later: 3.3RC3+3 (2021-06-04 09:11:54) 2021-06-05 14:44:55 [debug] X homed: true Y Homed: true 2021-06-05 14:44:55 [debug] Homing Z axis 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:17 [debug] {"err":-1} 2021-06-05 14:45:31 [debug] G32 bed probe heights: 0.023, mean 0.023, deviation from mean 0.000 2021-06-05 14:46:04 [warn] Leadscrew adjustments made: -0.021 0.081, points used 2, (mean, deviation) before (0.030, 0.032) after (-0.000, 0.000) 2021-06-05 14:46:04 [debug] Leadscrew adjustments made: -0.021 0.081, points used 2, (mean, deviation) before (0.030, 0.032) after (-0.000, 0.000) 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:04 [debug] {"err":-1} 2021-06-05 14:46:05 [warn] Warning: M9: Command is not supported 2021-06-05 14:51:02 [debug] Writing to file: /sys/SetTool.g 2021-06-05 14:51:35 [debug] X homed: true Y Homed: true 2021-06-05 14:51:35 [debug] Homing Z axis 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:51:56 [debug] {"err":-1} 2021-06-05 14:52:07 [debug] Writing to file: /sys/SetTool.g 2021-06-05 14:52:15 [debug] iteration: 0 2021-06-05 14:52:20 [debug] Writing to file: /sys/SetTool.g 2021-06-05 14:52:42 [debug] Writing to file: /sys/SetTool.g 2021-06-05 14:53:18 [info] Event logging started at level debug 2021-06-05 14:53:18 [info] Running: Duet 3 MB6HC v1.01 or later: 3.3RC3+3 (2021-06-04 09:11:54) 2021-06-05 14:53:26 [info] Event logging stopped -
@psychotik2k3 thanks. The M122 B1 report shows that the EXP3HC reset 10 minutes before you generated the report. Was that board already running 3.3RC3 at that time?
PS - I've put new main board firmware at https://www.dropbox.com/sh/nmpsl9a3jfsumm5/AAA6adSjEcd1AM_j5_tVberGa?dl=0 to fix the cause of the main board reset.
PPS - I've also put new EXP3HC firmware at the same location, in case a fix in it is relevant to the assertion failure.
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@dc42 thanks i gonna try that. i think the board was resetted 10 minutes ago by me on a general abort. but yes it was already in RC3.
i get back to 3.2.2 to do some tests so i go back to this new rc3+1 -
@dc42 ok just get back from 3.2.2 to your 3.3 rc3+1, updated dwc, then sdiap then mb6hc, then H3C. power off and on.
jsut after power up here are my M122 for the boards05/06/2021, 18:18:43 M122 B0 === Diagnostics === RepRapFirmware for Duet 3 MB6HC version 3.3RC3+4 (2021-06-05 16:20:17) running on Duet 3 MB6HC v1.01 or later (standalone mode) Board ID: 08DJM-956BA-NA3TN-6JTD8-3S86J-1UB2T Used output buffers: 3 of 40 (20 max) === RTOS === Static ram: 150896 Dynamic ram: 93272 of which 112 recycled Never used RAM 109912, free system stack 200 words Tasks: NETWORK(ready,29.1%,266) ETHERNET(notifyWait,0.1%,124) HEAT(delaying,0.0%,331) Move(notifyWait,0.0%,352) CanReceiv(notifyWait,0.0%,799) CanSender(notifyWait,0.0%,373) CanClock(delaying,0.0%,340) TMC(notifyWait,7.2%,93) MAIN(running,63.4%,924) IDLE(ready,0.1%,29), total 100.0% Owned mutexes: HTTP(MAIN) === Platform === Last reset 00:01:51 ago, cause: power up Last software reset details not available Error status: 0x00 Aux0 errors 0,0,0 Step timer max interval 130 MCU temperature: min 39.0, current 43.4, max 43.5 Supply voltage: min 23.4, current 23.7, max 24.0, under voltage events: 0, over voltage events: 0, power good: yes 12V rail voltage: min 12.0, current 12.1, max 12.1, under voltage events: 0 Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0 Driver 0: position 0, standstill, reads 32474, writes 15 timeouts 0, SG min/max 0/0 Driver 1: position 0, standstill, reads 32474, writes 15 timeouts 0, SG min/max 0/0 Driver 2: position 0, standstill, reads 32474, writes 15 timeouts 0, SG min/max 0/0 Driver 3: position 0, standstill, reads 32474, writes 15 timeouts 0, SG min/max 0/0 Driver 4: position 0, standstill, reads 32478, writes 11 timeouts 0, SG min/max 0/0 Driver 5: position 0, standstill, reads 32479, writes 11 timeouts 0, SG min/max 0/0 Date/time: 2021-06-05 18:18:43 Slowest loop: 3.71ms; fastest: 0.05ms === Storage === Free file entries: 10 SD card 0 detected, interface speed: 25.0MBytes/sec SD card longest read time 2.2ms, write time 0.0ms, max retries 0 === Move === DMs created 125, maxWait 0ms, bed compensation in use: none, comp offset 0.000 === MainDDARing === Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === AuxDDARing === Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1 === Heat === Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1 === GCodes === Segments left: 0 Movement lock held by null HTTP is ready with "M122 B0" in state(s) 0 Telnet is idle in state(s) 0 File is idle in state(s) 0 USB is idle in state(s) 0 Aux is idle in state(s) 0 Trigger is idle in state(s) 0 Queue is idle in state(s) 0 LCD is idle in state(s) 0 SBC is idle in state(s) 0 Daemon is idle in state(s) 0 Aux2 is idle in state(s) 0 Autopause is idle in state(s) 0 Code queue is empty. === CAN === Messages queued 1035, send timeouts 0, received 1366, lost 0, longest wait 1ms for reply type 6042, peak Tx sync delay 277, free buffers 49 (min 48), ts 557/556/0 === Network === Slowest loop: 2.99ms; fastest: 0.02ms Responder states: HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) HTTP(0) FTP(0) Telnet(0), 0 sessions Telnet(0), 0 sessions HTTP sessions: 1 of 8 - Ethernet - State: active Error counts: 0 0 1 0 0 Socket states: 5 2 2 2 2 0 0 0 M122 B1 Diagnostics for board 1: Duet EXP3HC firmware version 3.3RC3+1 (2021-05-29 10:22:51) Bootloader ID: not available Never used RAM 158144, free system stack 4400 words Tasks: Move(notifyWait,0.0%,160) HEAT(delaying,0.0%,117) CanAsync(notifyWait,0.0%,69) CanRecv(notifyWait,0.0%,83) CanClock(notifyWait,0.0%,74) TMC(notifyWait,22.8%,63) MAIN(running,75.7%,303) IDLE(ready,0.0%,40) AIN(delaying,1.4%,263), total 100.0% Last reset 00:02:17 ago, cause: power up Last software reset time unknown, reason: AssertionFailed, available RAM 159320, slot 0 Software reset code 0x0120 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x00000000 BFAR 0xe000ed38 SP 0x20004754 Task HEAT Freestk 142 bad marker Stack: 00000544 0002ebf8 000261ef 42000400 00022423 2002f020 00000000 2002f038 2000151c 00000000 0001d6c1 0002dde4 0002de9c 0002d4a0 00025035 2000159c 00000000 2002f020 00015609 00000000 000009c4 000009c4 a5a5a5a5 a5a5a5a5 a5a5a5a5 a5a5a5a5 00025035 Driver 0: position 0, 424.9 steps/mm, standstill, reads 44381, writes 17 timeouts 0, SG min/max 0/0, steps req 0 done 0 Driver 1: position 0, 917.4 steps/mm, standstill, reads 44383, writes 17 timeouts 0, SG min/max 0/0, steps req 0 done 0 Driver 2: position 0, 400.0 steps/mm, standstill, reads 44387, writes 17 timeouts 0, SG min/max 0/0, steps req 0 done 0 Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0 Peak sync jitter 0/7, peak Rx sync delay 178, resyncs 0/0, no step interrupt scheduled VIN: 23.8V, V12: 12.2V MCU temperature: min 37.3C, current 37.8C, max 37.9C Ticks since heat task active 216, ADC conversions started 137304, completed 137303, timed out 0, errs 0 Last sensors broadcast 0x0000000e found 3 221 ticks ago, loop time 0 CAN messages queued 1707, send timeouts 0, received 1274, lost 0, free buffers 37, min 37, error reg 110000 dup 0, oos 0/0/0/0, bm 0, wbm 0 but after that i faced a bad command just at the end of my home all once the home is finished , i was able to reproduce the bad command if i do some stuffs movement tool change etc and if i do a home all again.
here is the error and the home all gcode:
Homeall.g
; homeall.g ; called to home all axes ; ; generated by RepRapFirmware Configuration Tool v3.2.3 on Thu May 13 2021 17:38:36 GMT+0200 (heure d’été d’Europe centrale) G91 ; relative positioning M98 P"retractprobe.g" G1 H2 Z5 F6000 ; lift Z relative to current position G1 H1 X-358 F1800 ; move quickly to X axis endstop and stop there (first pass) G1 X5 F6000 ; go back a few mm G1 H1 X-358 F360 ; move slowly to X axis endstop once more (second pass) G1 X179 F6000 ; go to the middle G1 H1 Y369 F1800 ; move quickly to Y axis endstop and stop there (first pass) G1 Y-5 F6000 ; go back a few mm G1 H1 Y369 F360 ; move slowly to Y axis endstop once more (second pass) G1 Y-50 F6000 ; go back a 50 mm to leave belts G90 ; absolute positioning M98 P"homez.g" ; Uncomment the following lines to lift Z after probing ;G91 ; relative positioning ;G1 Z5 F100 ; lift Z relative to current position ;G90 ; absolute positioning HomeZ.g
; homez.g ; called to home the Z axis ; ; generated by RepRapFirmware Configuration Tool v3.2.3 on Thu May 13 2021 17:38:36 GMT+0200 (heure d’été d’Europe centrale) M98 P"retractprobe.g" ; force a retract in case of restart when pin deployed echo "X homed:", (move.axes[0].homed=true), " Y Homed:", (move.axes[1].homed=true) if (move.axes[0].homed=false ) echo "homing X axis" M98 P"homex.g" if (move.axes[1].homed=false ) echo "homing Y axis" M98 P"homey.g" echo "Homing Z axis" M400 G91 ; relative positioning G1 H2 Z5 F6000 ; lift Z relative to current position G90 ; absolute positioning ; go to middle of bed G1 X{155 - sensors.probes[0].offsets[0]} Y{155 - sensors.probes[0].offsets[1]} F6000 M558 F250 ; Set the probing speed G30 M558 F30 ; Set the probing speed G30 ; Uncomment the following lines to lift Z after probing G91 ; relative positioning G1 Z5 F100 ; lift Z relative to current position G90 ; absolute positioning