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Issues after prime

Scheduled Pinned Locked Moved Solved
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  • undefined
    Heartleander81
    last edited by 16 Aug 2021, 11:29

    When I make the first G1 move slower then F4000 ore the first G1 E-0.6 slower then F300 ore i delet the first G1 E-0.6, I doun't have the problem.

    All what I test the same issuse.

    Is any on my toolboard Config wrong?

    1 Reply Last reply Reply Quote 0
    • undefined
      Heartleander81
      last edited by 16 Aug 2021, 15:01

      I have install after 2 weeks the tool Board rev 1.1 with Accelerometer.
      The first prints All good. Over night came this isusse. Then I make any test and then, why ever was all good but only for 2 prints and the issuse was back.

      1 Reply Last reply Reply Quote 0
      • undefined
        Phaedrux Moderator @Heartleander81
        last edited by 16 Aug 2021, 16:21

        @heartleander81 said in Isusses after prime:

        G31 P500 X22.775 Y-5.21 Z0.00

        Your Z probe trigger height hasn't been measured yet.
        https://duet3d.dozuki.com/Wiki/Test_and_calibrate_the_Z_probe

        Please post the results of M122 and M122 B121

        Also send M98 P"config.g" and post the results.

        Can you also share your homing files?

        Z-Bot CoreXY Build | Thingiverse Profile

        undefined 2 Replies Last reply 16 Aug 2021, 16:26 Reply Quote 0
        • undefined
          Heartleander81 @Phaedrux
          last edited by 16 Aug 2021, 16:26

          @phaedrux
          Oh I have set it not to 0
          But then I load M501 for the right trigger height.

          Give me one Moment I Post it All.

          1 Reply Last reply Reply Quote 0
          • undefined
            Heartleander81
            last edited by Heartleander81 16 Aug 2021, 16:43

            Config.g

            ; Configuration file for Duet 3 (firmware version 3)
            ; executed by the firmware on start-up
            ;
            ; generated by RepRapFirmware Configuration Tool v3.1.4 on Wed Aug 26 2020 16:14:58 GMT+0200 (Mitteleuropäische Sommerzeit)
            ; General preferences
            G90 ; send absolute coordinates...
            M83 ; ...but relativ extruder moves
            M550 P"Duet3" ; set printer name
            M912 P0 S-2 ; setzt CPU Temp korrektur
            M669 K1 ;switch to core X/Y mode
            G4 S2
            ; Drives
            M569 P0.1 S0 D2 ; X physical drive 0.1 goes backwards
            M569 P0.2 S0 D2 ; Y physical drive 0.2 goes backwards
            M569 P0.0 S1 ; Z1 physical drive 0.0 goes forwards
            M569 P0.4 S1 ; Z2 physical drive 0.4 goes forwards
            M569 P0.3 S1 ; Z3 physical drive 0.3 goes forwards
            M569 P0.5 S1 ; physical drive 0.5 goes forwards
            M569 P20.0 S1 D2 ; E physical drive 0.0 Driver0 tool goard goes forwards
            M584 X0.1 Y0.2 Z0.0:0.4:0.3 E20.0 ; set drivers mapping
            M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
            M92 X80.40 Y80.40 Z800.00 E717.97 ; set steps per mm
            M566 X1250.00 Y1250.00 Z200.00 E1000.00 ; set maximum instantaneous speed changes (mm/min)
            M203 X30000.00 Y30000.00 Z600.00 E16000.00 ; set maximum speeds (mm/min)
            M201 X3000.00 Y3000.00 Z200.00 E2000.00 ; set accelerations (mm/s^2)
            M906 X1150 Y1150 Z1050 E750 I50 ; set motor currents (mA) and motor idle factor in per cent
            M84 S120 ; Set idle timeout
            ; Axis Limits
            M208 X0 Y0 Z-1 S1 ; set axis minima
            M208 X305 Y300 Z295 S0 ; set axis maxima
            ; Endstops
            M574 X1 S1 P"20.io1.in" ; configure active-high endstop for low end on X via pin 1.io1.in
            M574 Y1 S1 P"io1.in" ; configure active-high endstop for low end on Y via pin io1.in
            M574 Z1 S2
            ; Z-Probe
            M950 S0 C"20.io0.out" ; create servo pin 1.io0.out for BLTouch
            M558 P9 C"^20.io0.in" H3 A10 S0.005 F700 T6000 ; set Z probe type to bltouch and the dive height + speeds old H5 F200 T4000
            G31 P500 X22.775 Y-5.21 Z0.00 ; set Z probe trigger value, offset and trigger height
            M557 X30:285 Y11:266 S25.5 ; define mesh grid
            M671 X-21.018:155.191:331.4 Y-20.717:307.493:-20.717 S50 ; Z lift Point Position
            ; Heaters
            M308 S0 A"Bett" P"temp0" Y"thermistor" T100000 B4138 ; configure sensor 0 as thermistor on pin temp0
            M950 H0 C"out0" T0 ; create bed heater output on out0 and map it to sensor 0
            M307 H0 B0 R0.139 C807.2 D40.94 S1.00 V24.8 ; disable bang-bang mode for the bed heater and set PWM limit
            M140 H0 ; qmap heated bed to heater 0
            M143 H0 S140 ; set temperature limit for heater 0 to 120C
            M308 S1 A"Vulcano" P"20.temp0" Y"thermistor" T100000 B4725 C7.060000e-8 ; configure sensor 1 as thermistor on pin temp1
            M950 H1 C"20.out0" T1 ; create nozzle heater output on 20.out0 and map it to sensor 1
            M307 H1 B0 R2.775 C211.7:169.1 D3.87 S1.00 V24.7 ; disable bang-bang mode for heater and set PWM limit
            M308 S2 A"Elektro" P"temp3" Y"thermistor" T100000 B4100 ; configure sensor 1 as thermistor on pin temp1
            M308 S3 Y"mcu-temp" A"MCU" ; configure sensor 4 as thermistor on pin e1temp
            M308 S4 Y"drivers" A"Stepper" ; configure sensor 3 as temperature warning and overheat flags on Duet
            M308 S5 A"Raspi" P"temp2" Y"thermistor" T100000 B4138 ; Raspi cooling Fan
            ; Fans
            M950 F1 C"20.out2" Q500 ; create fan 1 on pin 20.out2 and set its frequency
            M106 P1 C"Hotend" S1 H1 T50 ; set fan 1 name and value. Thermostatic control is turned on
            M950 F0 C"out4" Q8000 ; create fan 0 on pin out4 and set its frequency
            M106 P0 C"Bauteil1" S0 H-1 ; set fan 0 name and value. Thermostatic control is turned off
            M950 F2 C"out9" Q500
            M106 P2 H5 T50:60 ; create fan 2 on pin out8 and set its frequency
            M950 F3 C"out8" Q500
            M106 P3 H3:4 T45:60 ; set fan 3 value
            M563 P0 S"Vulcano" D0 H1 F0 ; define tool 0
            G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
            G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C
            M955 P20.0 I10 ;Accelerometer 20:0 type LIS3DH with orientation 10 samples at 1344Hz with 10-bit resolution
            M564 S1 H0
            M150 X1
            ; Miscellaneous
            M575 P1 S3 B115200 ;57600 enable Display
            M911 S21 R22 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
            M501 ; load saved parameters from non-volatile memory

            Homeall.g

            ; homeall
            G91 ; relative mode
            G1 Z5 F600
            G1 H1 Y-340 F6000 ; course home X
            G1 Y4 F6000
            G1 H1 Y-10 F600 ; fime home X
            G1 Y100 F6000
            G1 H1 X-340 F6000 ; course home Y
            G1 X4 F5000 ; move away from the endstops
            G1 H1 X-10 F600 ; fine home Y
            G90 ; back to absolute mode
            ; The following code assumes you are using a Z probe to do Z homing.
            ; Adjust the XY coordinates in the following to place the Z probe over a suitable spot,
            ; preferably near the centre of the bed if your Z probe supports that
            G1 X131.4 Y139.4 F6000
            M401
            G30

            M122

            === Diagnostics ===
            RepRapFirmware for Duet 3 MB6HC version 3.3 (2021-06-15 21:45:47) running on Duet 3 MB6HC v1.01 or later (SBC mode)
            Board ID: 08DJM-9P63L-DJ3T8-6J1DA-3SD6P-KV4H9
            Used output buffers: 1 of 40 (11 max)
            === RTOS ===
            Static ram: 150904
            Dynamic ram: 62268 of which 212 recycled
            Never used RAM 140808, free system stack 184 words
            Tasks: SBC(ready,16.0%,338) HEAT(delaying,0.0%,325) Move(notifyWait,0.1%,284) CanReceiv(notifyWait,0.0%,774) CanSender(notifyWait,0.0%,374) CanClock(delaying,0.0%,339) TMC(notifyWait,24.0%,59)
            MAIN(running,59.8%,922) IDLE(ready,0.0%,29), total 100.0%
            Owned mutexes: HTTP(MAIN)
            === Platform ===
            Last reset 04:34:37 ago, cause: reset button
            Last software reset at 2021-08-15 16:22, reason: User, none spinning, available RAM 137520, slot 1
            Software reset code 0x0012 HFSR 0x00000000 CFSR 0x00000000 ICSR 0x0440f000 BFAR 0x00000000 SP 0x00000000 Task SBC Freestk 0 n/a
            Error status: 0x00
            Aux0 errors 0,0,0
            Step timer max interval 166
            MCU temperature: min 42.3, current 46.6, max 46.8
            Supply voltage: min 25.0, current 25.0, max 25.1, under voltage events: 0, over voltage events: 0, power good: yes
            12V rail voltage: min 12.0, current 12.1, max 12.2, under voltage events: 0
            Heap OK, handles allocated/used 0/0, heap memory allocated/used/recyclable 0/0/0, gc cycles 0
            Driver 0: position 0, standstill, reads 33617, writes 19 timeouts 0, SG min/max 0/143
            Driver 1: position 0, standstill, reads 33621, writes 15 timeouts 0, SG min/max 0/0
            Driver 2: position 40000, standstill, reads 33621, writes 15 timeouts 0, SG min/max 0/0
            Driver 3: position 0, standstill, reads 33618, writes 19 timeouts 0, SG min/max 0/153
            Driver 4: position 0, standstill, reads 33618, writes 19 timeouts 0, SG min/max 0/158
            Driver 5: position 0, standstill, reads 33626, writes 11 timeouts 0, SG min/max 0/0
            Date/time: 2021-08-16 18:30:16
            Slowest loop: 0.79ms; fastest: 0.04ms
            === Storage ===
            Free file entries: 10
            SD card 0 not detected, interface speed: 37.5MBytes/sec
            SD card longest read time 0.0ms, write time 0.0ms, max retries 0
            === Move ===
            DMs created 125, maxWait 89292ms, bed compensation in use: none, comp offset 0.000
            === MainDDARing ===
            Scheduled moves 2, completed moves 2, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 2], CDDA state -1
            === AuxDDARing ===
            Scheduled moves 0, completed moves 0, hiccups 0, stepErrors 0, LaErrors 0, Underruns [0, 0, 0], CDDA state -1
            === Heat ===
            Bed heaters = 0 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1 -1, chamberHeaters = -1 -1 -1 -1
            === GCodes ===
            Segments left: 0
            Movement lock held by null
            HTTP* is doing "M122" in state(s) 0
            Telnet is idle in state(s) 0
            File is idle in state(s) 0
            USB is idle in state(s) 0
            Aux is idle in state(s) 0
            Trigger* is idle in state(s) 0
            Queue is idle in state(s) 0
            LCD is idle in state(s) 0
            SBC is idle in state(s) 0
            Daemon is idle in state(s) 0
            Aux2 is idle in state(s) 0
            Autopause is idle in state(s) 0
            Code queue is empty.
            === CAN ===
            Messages queued 148116, received 197133, lost 0, longest wait 2ms for reply type 6049, peak Tx sync delay 176, free buffers 49 (min 48), ts 82389/82388/0
            Tx timeouts 0,0,0,0,0,0
            === SBC interface ===
            State: 4, failed transfers: 1, checksum errors: 0
            Last transfer: 0ms ago
            RX/TX seq numbers: 64954/64954
            SPI underruns 0, overruns 0
            Disconnects: 0, timeouts: 0, IAP RAM available 0x2c810
            Buffer RX/TX: 0/0-0
            === Duet Control Server ===
            Duet Control Server v3.3.0 Code buffer space: 4096 Configured SPI speed: 8000000Hz
            Full transfers per second: 35.83, max wait times: 28.7ms/0.0ms
            Codes per second: 0.01
            Maximum length of RX/TX data transfers: 2568/808

            M122 B20

            M122 B20
            Diagnostics for board 20:
            Duet TOOL1LC firmware version 3.3 (2021-06-15 16:12:58)
            Bootloader ID: SAMC21 bootloader version 2.3 (2021-01-26b1)
            Never used RAM 2680, free system stack 2789 words
            Tasks: Move(notifyWait,0.0%,153) HEAT(delaying,0.5%,107) CanAsync(notifyWait,0.0%,65) CanRecv(notifyWait,0.0%,76) CanClock(notifyWait,0.1%,65) ACCEL(notifyWait,0.0%,61) TMC(notifyWait,8.6%,57)
            MAIN(running,75.8%,352) IDLE(ready,0.0%,27) AIN(delaying,15.0%,142), total 100.0%
            Last reset 04:44:52 ago, cause: software
            Last software reset data not available
            Driver 0: position 0, 718.0 steps/mm, standstill, SG min/max 0/0, read errors 0, write errors 1, ifcnt 71, reads 26324, writes 12, timeouts 6, DMA errors 0, failedOp 0x41, steps req 0 done 0
            Moves scheduled 0, completed 0, in progress 0, hiccups 0, step errors 0, maxPrep 0, maxOverdue 0, maxInc 0, mcErrs 0, gcmErrs 0
            Peak sync jitter 0/6, peak Rx sync delay 217, resyncs 0/0, no step interrupt scheduled
            VIN: 25.3V
            MCU temperature: min 44.0C, current 44.7C, max 48.8C
            Ticks since heat task active 126, ADC conversions started 17092120, completed 17092119, timed out 0, errs 0
            Last sensors broadcast 0x00000002 found 1 130 ticks ago, loop time 0
            CAN messages queued 203765, send timeouts 66, received 153030, lost 0, free buffers 37, min 37, error reg 100000 Last cancelled message type 4512 dest 127
            dup 0, oos 0/0/0/0, bm 0, wbm 0, rxMotionDelay 0
            Accelerometer detected: yes, status: 00
            I2C bus errors 0, naks 0, other errors 0

            M98 P"config.g"

            M98 P"config.g"
            Accelerometer 20:0 with orientation 10 samples at 1344Hz with 10-bit resolution
            1 Reply Last reply Reply Quote 0
            • undefined
              Heartleander81
              last edited by Heartleander81 16 Aug 2021, 16:47

              ; config-override.g file generated in response to M500 at 2021-01-25 11:01
              ; Z-Probe
              G31 P500 Z4.35 ; for trigger height
              1 Reply Last reply Reply Quote 0
              • undefined
                Heartleander81 @Phaedrux
                last edited by 16 Aug 2021, 17:08

                @phaedrux

                Ok I hope that is all what you need

                1 Reply Last reply Reply Quote 0
                • undefined
                  Phaedrux Moderator @Heartleander81
                  last edited by 16 Aug 2021, 20:33

                  @heartleander81 said in Isusses after prime:

                  G32 G29 S1 P "hightmap.csv"

                  What do you have in bed.g?

                  Have you tried with mesh compensation disabled?

                  Z-Bot CoreXY Build | Thingiverse Profile

                  undefined 1 Reply Last reply 16 Aug 2021, 20:40 Reply Quote 0
                  • undefined
                    Heartleander81 @Phaedrux
                    last edited by 16 Aug 2021, 20:40

                    @phaedrux

                    ; bed.g
                    ; called to perform automatic bed compensation via G32
                    ;
                    ; generated by RepRapFirmware Configuration Tool v3.1.4 on Wed Aug 26 2020 16:14:58 GMT+0200 (Mitteleuropäische Sommerzeit)
                    M561 ; clear any bed transform
                    G29 S2 ; clear bed high map
                    G28 ; home
                    M401
                    G30 P0 X25.159 Y16.257 Z-99999 ; probe near a leadscrew
                    G30 P1 X25.159 Y266.257 Z-99999 ; new
                    G30 P2 X285.159 Y266.257 Z-99999 ; x154.53 old
                    G30 P3 X285.159 Y16.257 Z-99999 S3 ; probe near a leadscrew and calibrate 3 motors
                    G28Z
                    M402

                    If I edit the G-code that it does everything at z-height, say 5mm, then it's the same with the X-axis. runs on stops - extruder is doing something - X axis continues to run. As mentioned, if I delete or comment out the first Retract G1 E-0.6000 F1200 from the sliced ​​file, there are no problems with the X axis or the extruder

                    undefined 1 Reply Last reply 16 Aug 2021, 20:45 Reply Quote 0
                    • undefined
                      Phaedrux Moderator @Heartleander81
                      last edited by 16 Aug 2021, 20:45

                      @heartleander81 said in Isusses after prime:

                      if I delete or comment out the first Retract G1 E-0.6000 F1200 from the sliced ​​file, there are no problems with the X axis or the extruder

                      This still very much sounds like it's in absolute extrusion mode and it's pausing while it's trying to move the extruder to undo all of the previous extrusion commands.

                      Z-Bot CoreXY Build | Thingiverse Profile

                      undefined 1 Reply Last reply 16 Aug 2021, 20:49 Reply Quote 0
                      • undefined
                        Heartleander81
                        last edited by 16 Aug 2021, 20:46

                        I apologize if my sentences read clumsily or unkindly. I work with google translators because my english is very bad. I am very, very grateful for the help that I am getting because I am slowly becoming desperate.

                        1 Reply Last reply Reply Quote 0
                        • undefined
                          Heartleander81 @Phaedrux
                          last edited by 16 Aug 2021, 20:49

                          @phaedrux
                          ok i understand that and is understandable. but why is he doing this? in the start code it runs great in the M83 and after that I no longer give an M82 command. I switched Simplify3D to M83 and the sliced ​​code also looks like it.

                          1 Reply Last reply Reply Quote 0
                          • undefined
                            Phaedrux Moderator @Heartleander81
                            last edited by 16 Aug 2021, 20:52

                            @heartleander81 said in Isusses after prime:

                            M955 P20.0 I10

                            Can you try commenting out the accelerometer command?

                            Z-Bot CoreXY Build | Thingiverse Profile

                            undefined 2 Replies Last reply 16 Aug 2021, 20:54 Reply Quote 0
                            • undefined
                              Heartleander81 @Phaedrux
                              last edited by 16 Aug 2021, 20:54

                              @phaedrux
                              Have I do yesterday. But with M82.

                              I can try it in 30 min.

                              1 Reply Last reply Reply Quote 0
                              • undefined
                                Heartleander81 @Phaedrux
                                last edited by 16 Aug 2021, 21:02

                                @phaedrux

                                Is the same

                                1 Reply Last reply Reply Quote 0
                                • undefined
                                  Phaedrux Moderator
                                  last edited by 16 Aug 2021, 22:34

                                  your video is very short and a little confusing to me. It looks like it goes into slow motion? Is that to show the stuttering? Can you upload a new video that's a bit longer and doesn't go to slow mo? Describe for us exactly at what point each piece of gcode is executing from the time you hit print to the time you see the problem.

                                  Z-Bot CoreXY Build | Thingiverse Profile

                                  undefined 2 Replies Last reply 17 Aug 2021, 05:34 Reply Quote 0
                                  • undefined
                                    Heartleander81 @Phaedrux
                                    last edited by Phaedrux 17 Aug 2021, 05:34

                                    @phaedrux

                                    https://youtu.be/lhOgw-MZr2o

                                    This Video is without slow motion and with Sound.

                                    G90
                                    M83
                                    M106 S0
                                    M140 S50
                                    M190 S50
                                    M104 S240 T0
                                    M109 S240 T0
                                    T0
                                    M98 P"startGcode"
                                    G92 E0.0
                                    ; process CR3D 0.4
                                    ; layer 1, Z = 0.200
                                    T0
                                    G1 E-0.6000 F1200 ; if I comment out this line then the error is not there.
                                    ; feature skirt
                                    ; tool H0.200 W0.440
                                    G1 Z0.200 F600
                                    G1 X19.489 Y53.567 F12600
                                    G1 E0.6000 F1200
                                    G1 X280.511 Y53.567 E8.9768 F1800
                                    ; layer end
                                    T0
                                    M98 P"endGcode"
                                    G32
                                    G29 S1 P"heightmap.csv"
                                    G1 X5 Y5 Z30 F6000.0
                                    G1 E40 F600
                                    G1 E40 F200
                                    G1 Y20 F2000
                                    G1 Y50 Z0.2 F2000
                                    G1 Y90 E20 F300
                                    G1 Y120 F1200
                                    1 Reply Last reply Reply Quote 0
                                    • undefined
                                      Heartleander81 @Phaedrux
                                      last edited by 17 Aug 2021, 18:59

                                      @phaedrux
                                      Is that video better?

                                      1 Reply Last reply Reply Quote 0
                                      • undefined
                                        Phaedrux Moderator
                                        last edited by 17 Aug 2021, 19:16

                                        Yes I think so. At what point in the gcode stream does the video start?

                                        It looks like it's just finished homing, or is that it finishing G32?, moves to the corner, purges some filament, then draws a purge line, and moves to start another line across the bed.

                                        What is in M98 P"startGcode" ?

                                        Is it this?

                                        G32
                                        G29 S1 P"heightmap.csv"
                                        G1 X5 Y5 Z30 F6000.0
                                        G1 E40 F600
                                        G1 E40 F200
                                        G1 Y20 F2000
                                        G1 Y50 Z0.2 F2000
                                        G1 Y90 E20 F300
                                        G1 Y120 F1200

                                        @heartleander81 said in Isusses after prime:

                                        G28Z

                                        What do you have in homez.g?

                                        Z-Bot CoreXY Build | Thingiverse Profile

                                        undefined 1 Reply Last reply 17 Aug 2021, 19:28 Reply Quote 0
                                        • undefined
                                          Heartleander81 @Phaedrux
                                          last edited by 17 Aug 2021, 19:28

                                          @phaedrux
                                          Yes that is my startcode

                                          The video start after finish G32.

                                          After the the Purge line goes X to 110 and from ther Point start the slicing Part with G1 E-0.600 F1200 and on the next move to print Point start ist the issuse.
                                          I think I See at dwc Motor E run to Zero and back without 0.6mm
                                          From E100 to E0 to E99.4

                                          ; homez.g
                                          ; called to home the Z axis
                                          ;
                                          ; generated by RepRapFirmware Configuration Tool v3.1.4 on Wed Aug 26 2020 16:14:58 GMT+0200 (Mitteleuropäische Sommerzeit)
                                          ;G91 ; relative positioning
                                          ;G1 Z5 F600 ; lift Z relative to current position
                                          ;G90 ;
                                          G1 X129.4 Y139.4 F3000 ;
                                          M401
                                          G30 ; Do a single probe to home our Z axis
                                          M402
                                          ;G90
                                          ; Uncomment the following lines to lift Z after probing
                                          ;G1 X0 Y0 F6000 ; lift Z relative to current position
                                          ;G1 Z5 F600
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