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Z axis not homing

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  • undefined
    PRIOR123
    last edited by 31 Oct 2021, 10:03

    Hi there,

    Im having issues with my z homing. i repeatedly get this

    Error: in file macro line 5: M280: parameter 'P' too high

    I noticed that there was no M401 code in the homingall.g anyway i tried to manually put M401 into the console and it gave me the same error message.

    Can someone help me out on this?

    undefined 1 Reply Last reply 31 Oct 2021, 10:07 Reply Quote 0
    • undefined
      jay_s_uk @PRIOR123
      last edited by 31 Oct 2021, 10:07

      @prior123 it's probably your deployprobe.g that has an issue

      Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

      undefined 1 Reply Last reply 31 Oct 2021, 10:09 Reply Quote 0
      • undefined
        PRIOR123 @jay_s_uk
        last edited by 31 Oct 2021, 10:09

        @jay_s_uk so this is my deployprobe.g.

        ; deployprobe.g
        ; called to deploy a physical Z probe
        ;
        ; generated by RepRapFirmware Configuration Tool v3.3.5 on Sun Oct 31 2021 09:28:37 GMT+0000 (Greenwich Mean Time)
        M280 P64 S10 ; deploy BLTouch

        can you see anything?

        undefined undefined 2 Replies Last reply 31 Oct 2021, 10:21 Reply Quote 0
        • undefined
          jay_s_uk @PRIOR123
          last edited by 31 Oct 2021, 10:21

          @prior123 the P64 looks very odd. What number have you defined in your config?

          Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

          1 Reply Last reply Reply Quote 0
          • undefined
            PRIOR123 @PRIOR123
            last edited by 31 Oct 2021, 10:22

            @prior123

            Ive just changed it to

            M280 P0 S10 ; deploy BLTouch

            and seem to have worked however now the x axis is making a horrible noise and the same error message come out. however it does say its fully homed. Im properly confused now

            undefined 1 Reply Last reply 31 Oct 2021, 10:24 Reply Quote 0
            • undefined
              jay_s_uk @PRIOR123
              last edited by 31 Oct 2021, 10:24

              @prior123 have you got the x axis travelling further than total axis travel?
              If it fails to find the endstops on the first move but finds it on the second, that's usually when you get that message

              Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

              undefined 2 Replies Last reply 31 Oct 2021, 10:25 Reply Quote 0
              • undefined
                PRIOR123 @jay_s_uk
                last edited by 31 Oct 2021, 10:25

                @jay_s_uk

                you were right i was on +Xaxis not - (facepalm)

                Thank you

                1 Reply Last reply Reply Quote 1
                • undefined
                  PRIOR123 @jay_s_uk
                  last edited by 31 Oct 2021, 10:31

                  @jay_s_uk

                  Sorry to keep on but im now having an issue where the BOLD line isnt being read. The printer just keeps the x and Y axis by the end stops

                  G91 ; relative positioning
                  G1 H2 Z5 F6000 ; lift Z relative to current position
                  G1 H1 X230.5 Y235 F1800 ; move quickly to X and Y axis endstops and stop there (first pass)
                  G1 H2 X-5 Y-5 F6000 ; go back a few mm
                  G1 H1 X230.5 Y235 F360 ; move slowly to X and Y axis endstops once more (second pass)
                  G90 ; absolute positioning
                  G1 X-38 Y-10 F6000 ; go to first bed probe point and home Z
                  ;G1 X-100 Y-50 F6000 ; go to first bed probe point and home Z
                  G30 ; home Z by probing the bed

                  :s

                  undefined undefined 2 Replies Last reply 31 Oct 2021, 10:35 Reply Quote 0
                  • undefined
                    PRIOR123 @PRIOR123
                    last edited by 31 Oct 2021, 10:35

                    @prior123

                    if i put my finger in to make the printer think its homed the Z axis (on home all) im still getting this error too

                    G28
                    Error: in file macro line 5: M280: parameter 'P' too high

                    undefined 1 Reply Last reply 31 Oct 2021, 10:44 Reply Quote 0
                    • undefined
                      jay_s_uk @PRIOR123
                      last edited by 31 Oct 2021, 10:43

                      @prior123 can your printer even reach X-38 Y-10?
                      Post your config.g

                      Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                      undefined 1 Reply Last reply 31 Oct 2021, 10:45 Reply Quote 0
                      • undefined
                        jay_s_uk @PRIOR123
                        last edited by 31 Oct 2021, 10:44

                        @prior123 you may also want to check your retractprobe.g as well

                        Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                        undefined 1 Reply Last reply 31 Oct 2021, 10:46 Reply Quote 0
                        • undefined
                          PRIOR123 @jay_s_uk
                          last edited by 31 Oct 2021, 10:45

                          @jay_s_uk

                          ; Configuration file for Duet WiFi (firmware version 3)
                          ; executed by the firmware on start-up
                          ;
                          ; generated by RepRapFirmware Configuration Tool v3.2.3 on Tue Mar 16 2021 15:54:40 GMT+0000 (Greenwich Mean Time)

                          ; General preferences
                          G90 ; send absolute coordinates...
                          M83 ; ...but relative extruder moves
                          M550 P"" ; set printer name

                          ; Network
                          ;M551 P"" ; set password
                          M552 S1 ; enable network
                          M586 P0 S1 ; enable HTTP
                          M586 P1 S0 ; disable FTP
                          M586 P2 S0 ; disable Telnet

                          ; Drives
                          M569 P0 S1 ; physical drive 0 goes backwards
                          M569 P1 S1 ; physical drive 1 goes backwards
                          M569 P2 S1 ; physical drive 2 goes forwards
                          M569 P3 S0 ; physical drive 3 goes forwards
                          M584 X0 Y1 Z2 E3 ; set drive mapping
                          M350 X16 Y16 Z16 E16 I1 ; configure microstepping with interpolation
                          M92 X80.00 Y80.00 Z400.00 E93.00 ; set steps per mm
                          M566 X900.00 Y900.00 Z12.00 E1200.00 ; set maximum instantaneous speed changes (mm/min)
                          M203 X6000.00 Y6000.00 Z180.00 E1200.00 ; set maximum speeds (mm/min)
                          M201 X500.00 Y500.00 Z20.00 E250.00 ; set accelerations (mm/s^2)
                          M906 X600 Y600 Z600 E600 I30 ; set motor currents (mA) and motor idle factor in per cent
                          M84 S30 ; Set idle timeout

                          ; Axis Limits
                          M208 X-5.5 Y-10 Z0 S1 ; set axis minima
                          M208 X220 Y220 Z250 S0 ; set axis maxima

                          ; Endstops
                          M574 X1 S1 P"xstop" ; configure active-high endstop for low end on X via pin xstop
                          M574 Y1 S1 P"ystop" ; configure active-high endstop for low end on Y via pin ystop
                          M574 Z1 S2 ; configure Z-probe endstop for low end on Z

                          ; Z-Probe
                          M950 S0 C"exp.heater3" ; create servo pin 0 for BLTouch
                          M558 P9 C"^zprobe.in" H5 F120 T6000 ; set Z probe type to bltouch and the dive height + speeds
                          G31 P500 X-49 Y9 Z1.597 ; set Z probe trigger value, offset and trigger height
                          M557 X-15:165 Y20:230 S20 ; define mesh grid
                          ;M557 X5:205 Y5:165 S20 ; Define mesh grid

                          ; Heaters
                          M308 S0 P"bedtemp" Y"thermistor" T98801 B4185 ; configure sensor 0 as thermistor on pin bedtemp
                          M950 H0 C"bedheat" T0 ; create bed heater output on bedheat and map it to sensor 0
                          M307 H0 B0 S1.00 ; disable bang-bang mode for the bed heater and set PWM limit
                          M140 H0 ; map heated bed to heater 0
                          M143 H0 S120 ; set temperature limit for heater 0 to 120C
                          M308 S1 P"e0temp" Y"thermistor" T98801 B4185 ; configure sensor 1 as thermistor on pin e0temp
                          M950 H1 C"e0heat" T1 ; create nozzle heater output on e0heat and map it to sensor 1
                          M307 H1 B0 S1.00 ; disable bang-bang mode for heater and set PWM limit
                          M143 H1 S280 ; set temperature limit for heater 1 to 280C

                          ; Fans
                          M950 F0 C"fan0" Q500 ; create fan 0 on pin fan0 and set its frequency
                          M106 P0 C"Part Cooling" S0 H-1 ; set fan 0 name and value. Thermostatic control is turned off
                          M950 F1 C"fan1" Q500 ; create fan 1 on pin fan1 and set its frequency
                          M106 P1 C"Heatsink/Hotend" S1 H1 T45 ; set fan 1 name and value. Thermostatic control is turned on
                          M950 F2 C"fan2" Q500 ; create fan 2 on pin fan2 and set its frequency
                          M106 P2 C"PartCooling" S1 H1 T45 ; set fan 2 name and value. Thermostatic control is turned on

                          ; Tools
                          M563 P0 S"PrintHead01" D0 H1 F0 ; define tool 0
                          G10 P0 X0 Y0 Z0 ; set tool 0 axis offsets
                          G10 P0 R0 S0 ; set initial tool 0 active and standby temperatures to 0C

                          ; Custom settings are not defined

                          ; Miscellaneous
                          M575 P1 S1 B57600 ; enable support for PanelDue
                          M501 ; load saved parameters from non-volatile memory
                          M911 S10 R11 P"M913 X0 Y0 G91 M83 G1 Z3 E-5 F1000" ; set voltage thresholds and actions to run on power loss
                          T0 ; select first tool

                          1 Reply Last reply Reply Quote 0
                          • undefined
                            PRIOR123 @jay_s_uk
                            last edited by 31 Oct 2021, 10:46

                            @jay_s_uk This has stopped the warning sign! thank you

                            undefined 1 Reply Last reply 31 Oct 2021, 10:48 Reply Quote 0
                            • undefined
                              jay_s_uk @PRIOR123
                              last edited by 31 Oct 2021, 10:48

                              @prior123 all sorted now?

                              Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                              undefined 1 Reply Last reply 31 Oct 2021, 10:50 Reply Quote 0
                              • undefined
                                PRIOR123 @jay_s_uk
                                last edited by 31 Oct 2021, 10:50

                                @jay_s_uk

                                the homing error is fixed but the x and y positioning when homing the Z via home all isnt working

                                undefined 1 Reply Last reply 31 Oct 2021, 11:00 Reply Quote 0
                                • undefined
                                  jay_s_uk @PRIOR123
                                  last edited by 31 Oct 2021, 11:00

                                  @prior123 because you're in absolute mode. Surely X-38 Y-10 is off your bed or even outside your axis limits

                                  Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                                  undefined 1 Reply Last reply 31 Oct 2021, 11:03 Reply Quote 0
                                  • undefined
                                    PRIOR123 @jay_s_uk
                                    last edited by 31 Oct 2021, 11:03

                                    @jay_s_uk so should i comment out that line then? sorry im pretty unknown when it comes to programming

                                    undefined 1 Reply Last reply 31 Oct 2021, 11:07 Reply Quote 0
                                    • undefined
                                      jay_s_uk @PRIOR123
                                      last edited by 31 Oct 2021, 11:07

                                      @prior123 well where do you want the nozzle to move to when you do the G30?

                                      Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                                      undefined 1 Reply Last reply 31 Oct 2021, 11:10 Reply Quote 0
                                      • undefined
                                        PRIOR123 @jay_s_uk
                                        last edited by 31 Oct 2021, 11:10

                                        @jay_s_uk probably X-60 and Y-10

                                        But i just changed that in the homeall.g and it doesnt seem to be doing anything

                                        undefined 1 Reply Last reply 31 Oct 2021, 11:17 Reply Quote 0
                                        • undefined
                                          jay_s_uk @PRIOR123
                                          last edited by 31 Oct 2021, 11:17

                                          @prior123 how? That's way outside your bed limits set in M208 in your config

                                          Owns various duet boards and is the main wiki maintainer for the Teamgloomy LPC/STM32 port of RRF. Assume I'm running whatever the latest beta/stable build is

                                          undefined 1 Reply Last reply 31 Oct 2021, 12:14 Reply Quote 0
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